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37-003-22315

Well Details

Well ID: 37-003-22315
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Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Findlay Township
Operator Name: CNX GAS CO LLC
Well Pad ID: 151158
Farm/Lease Name: ACAA 4B
License Status:
Spud Date:
Permit Date: 2014-11-03
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 40.479978
Longitude: -80.237206

For data sources see[1][2][3]

Well History

Date Event
2014-11-03 New Permit Application
2015-01-23 Performed Spud Operation
2017-08-01 MOD
2017-09-21 MOD

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2015 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2016 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2017 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2019 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2019 CNX GAS CO LLC Other Oil & Gas Wastes 19.33 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW019

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2332442 Primary Facility 2014-12-23 Preoperation Inspection No Violations Noted Our preoperation inspection of CNX ACAA 4 Well Pad for well 4A-4L
2337590 Primary Facility 2015-01-16 Follow-up Inspection No Violations Noted Follow up inspection to check on progress of E&S controls from 12/23/14.
2342060 Primary Facility 2015-01-29 Drilling/Alteration No Violations Noted THE CONDUCTOR IS IN AND COVERED. THE SITE IS OK.
2356933 Primary Facility 2015-04-01 Administrative/File Review In Compliance with Policy On Monday March 31st 2015, Consol Energy representative Benjamin Leightner reported a Hammer Oil spill of one gallon that was immediately cleaned up and removed. This appears to be in compliance with department spill policy.
2367306 Primary Facility 2015-05-04 Routine/Complete Inspection No Violations Noted
2367356 Primary Facility 2015-04-01 Drilling/Alteration No Violations Noted 80' OF 20" CONDUCTOR IS IN. THE TOP HOLE RIG HAS LEFT THE SITE.
2665561 Primary Facility 2017-11-30 Complaint Inspection No Violations Noted Well appears to be drilled but not completed. Department records indicate the well was spud on 1/23/2015. No well apparatus observed. Cellar covered with a large steel plate. No production equipment observed. No gas production units on well pad.

For data sources see[7]

References