X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-003-01262

Well Details

Well ID: 37-003-01262
Loading map...
Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Franklin Park Borough
Operator Name: UNKNOWN OPR
Well Pad ID:
Farm/Lease Name: ANTAKI
License Status: Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.557447
Longitude: -80.086522

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
2014-09-04 NEWLY DRILLED

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2415770 Primary Facility 2015-06-10 Routine/Complete Inspection No Adverse Event or Action Reported Followup routine inspection to check vent for integrity and if gas was venting. Vent is intact, no gas was noted.
2511756 Primary Facility 2016-07-22 Routine/Complete Inspection Adverse Events or Actions Reported Visited site w/ Scott Sabocheck to inspect vent & surrounding area for gas. Dead areas in yard were venting stray gas, vent did not appear to be venting gas. No gas detected further up driveway or toward house. No gas detected from water well.
2511768 Primary Facility 2016-07-26 Routine/Complete Inspection Adverse Events or Actions Reported Met w/ Scott Sabocheck, Rich Freese & Yost Drilling to discuss options at site for mitigation & elimination of stray gas. Vent was venting today. Soil tested positive for gas. Four test holes were created and flagged for routine testing:Test hole "A" - 20% gas. Test hole "B" - 10% gas. Test hole "C" - 10% gas. Test hole "D" - 0% gas
2511773 Primary Facility 2016-08-03 Routine/Complete Inspection Adverse Events or Actions Reported Visited site to get gas readings from test holes:Test hole "A" - 11-12 % gas, 100% LEL, no water in hole.Test hole "B" - 0% gas, hole partially water-filled.Test hole "C" - 2-3% gas, 65-70% LEL, hole partially water-filled.Test hole "D" - 0% gas/LEL, no water in hole.
2511776 Primary Facility 2016-08-15 Routine/Complete Inspection Adverse Events or Actions Reported Visited site shortly after moderate rain. Yard areound vent was bubbling noticeably in many places, including two spots across the driveway near the vent. Test hole "C" was actively bubbling gas, test holes "A", "B" & "D" were not bubbling. Too water-saturated to take gas readings from test holes, but stray gas was made obvious by the amount of bubbling visible in the yard.
2511779 Primary Facility 2016-08-17 Routine/Complete Inspection Adverse Events or Actions Reported Visited site to attempt to capture stray gas escaping from yard using a garbage bag placed over the most active area of venting. After ~ 1/2 hour the bag was partially inflated and tested 78% gas inside.
2511790 Primary Facility 2016-08-18 Routine/Complete Inspection Adverse Events or Actions Reported Met w/ representatives from Peoples Gas to discuss stray gas situation. All their lines in area have been replaced w/ new plastic. Met w/ Nick's Well Plugging, Groundwater Resources & KU Resources to discuss stray gas remediation options at site. Scott Sabocheck & Rich Freese were on site for all activities. We collected gas samples from the vent stack and from the yard to be submitted to Isotech for analysis.
2514371 Primary Facility 2016-08-24 Routine/Partial Inspection Adverse Events or Actions Reported Took gas readigs from four original test holes. (A new hole close to vent tested 80% steady gas.) Test hole "A": 7-8% gas, Test hole "B": 4-5% gas, Test hole "C": 8% gas, Test hole "D": 0% gas.
2516901 Primary Facility 2016-08-31 Routine/Partial Inspection Adverse Events or Actions Reported Doug Catalano brought methane imaging camera to site and "photographed" stray gas emitting from yard and vent. Scott Sabocheck and Rich Freese were also on site.
2520278 Primary Facility 2016-09-14 Routine/Partial Inspection Adverse Events or Actions Reported Lawn is gassing strongly from "C"(closest to vent stack & well), can be heard gurgling. Test hole "A": 2-3% gas, Test hole "B": 3% gas, Test hole "C": 87% gas (sustained), Test hole "D": 0% gas.
2527681 Primary Facility 2016-10-13 Routine/Partial Inspection Adverse Events or Actions Reported Visited site to take gas readings at test holes: Test Hole "A": 5% gas, Test Hole "B:: 5-40% gas, Test Hole "C": 88-90% gas sustained, Test Hole "D": 0% gas. A test hole further into yard in dead grass: 3-7% gas. Hole near house: 0% gas.
2527843 Primary Facility 2016-09-30 Routine/Partial Inspection Adverse Events or Actions Reported Visited site to take gas readings at test holes (several holes were filled w/ water and new holes were made): Test Hole "A": 8% gas, Test Hole "B: 35-40% gas, 35% sustained , Test Hole "C": 75-80% gas sustained (bubbling profusely after recent heavy rains), Test Hole "D": 0% gas. A test hole further into yard in dead grass: 2% gas. Hole near house: 0% gas. Discussed future plans for site with landowner, methane detection, trenched mitigation system & eventual well plugging.
2534527 Primary Facility 2016-10-20 Routine/Partial Inspection Adverse Events or Actions Reported Visited site to take gas readings at test holes and other locations. Test hole "A": 3% gas, Test Hole "B": 10% gas, Test hole "C": 86% gas, Test hole "D": 0% gas. Area in yard away from well vent: 20% gas. Area near sewer cleanout closer to house: 2% gas, 30-35% LEL (this is the first time gas has been detected here).
2534534 Primary Facility 2016-11-01 Routine/Complete Inspection Adverse Events or Actions Reported Visited site to take stray gas readings: Test hole "A": 25% gas high, 15% gas sustained, Test hole "B": 15 % gas high, 10% gas sustained, Test hole "C": 85% gas high & sustained, Test hole "D": 0% gas, 0% LEL. Area in yard away from well vent: 30% gas high, 0% sustained (hole filled w/ water). Area near sewer cleanout closer to house: 0% gas, 0% LEL. Tested output of radon vent system: 0% gas, 0% LEL. Tested several locations in basement: 0% gas, 0% LEL.
2548719 Primary Facility 2016-11-09 Routine/Complete Inspection No Viols - Permanently Shut Down Visited site to take gas readings. Test Hole "A": 5% gas high, 0% sustained, Test Hole "B": 8% gas high, 2% sustained, Test Hole "C": 60 % sustained, water-filled and boiling, Test Hole "D": 0% gas & LEL. Area in yard away from well vent: 5%-2% LEL, area around sewer cleanout: 0% LEL. Ground saturated by overnight rains, revealed bubbling areas across driveway from vent and scattered areas in yard on vent side of driveway.
2548734 Primary Facility 2016-11-28 Routine/Complete Inspection No Viols - Permanently Shut Down Visited site w/ Echelon representative to evaluate site for remediation for stray gas isuues. Ran gas checks- Test Hole "A": 6% gas, Test Hole "B":22% gas, Tesr Hole"C": 99% gas. Test Hole"D": 0% gas/LEL, area in yard near vent:6% gas, area around sewer vent: 11% gas, water well cap: 0% gas/LEL Across driveway from vent: 37-20% gas. Half-way up & totally up driveway near house- several checks, all 0% LEL. Basement checks-all 0% LEL.
2608877 Primary Facility 2017-01-23 Routine/Partial Inspection No Viols - Permanently Shut Down Area around well vent and yard is totally water saturated from prior & current rains; unable to get any gas readings. The "blowhole" test hole is very actively venting gas.
2608885 Primary Facility 2017-02-21 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to get gas readings from test holes; "A": 10% gas max, 2% sustained, "B": 15% gas max, 5% sustained, "C"("blowhole"): 85% gas sustained, "D": 0% gas/LEL, Diagonal: 35% gas, 30% sustained, Sewer Cleanout: 1-2% gas, 20% LEL max. The day is 63 degrees, the ground is moist, but no standing water, several days since last precipitation.
2608890 Primary Facility 2017-03-29 Routine/Partial Inspection No Viols - Permanently Shut Down Talked to landowner to discuss upcoming remediation plans. We discussed several areas in the yard that have been actively venting lately, as well as Test Hole #3 (blowhole).
2608891 Primary Facility 2017-05-01 Routine/Partial Inspection No Viols - Permanently Shut Down Remediation work by Echelon was scheduled to begin today, but the forcast of rain has postponed the start. Excavator, piping & other materials are on site.
2608894 Primary Facility 2017-05-04 Routine/Partial Inspection No Viols - Permanently Shut Down Echelon completed the remediation trenches and vents, mulched & seeded site. Wellhead vent: 7% gas, 100% LEL, roadside vent: 0% gas, 0% LEL.
2608902 Primary Facility 2017-05-16 Routine/Partial Inspection No Viols - Permanently Shut Down Additional work was done to the site yesterday by Echelon, as there was still noticeable gas leaking in the yard. They removed/capped old piping placed by Hydrocarbon. They will need to do additional restoration to the site when it dries out more. Landowner is not happy with current restoration. Well vent: 17% gas 100% LEL, road vent: 0% gas, 1-2% LEL.
2608909 Primary Facility 2017-05-30 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to check status of remediation. Well vent: 42% gas, 100% LEL, road vent 0% Gas, 0% LEL. No noticeable leaks in the yard at time of inspection.
2621340 Primary Facility 2017-07-27 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to check gas flow in vent stacks. Well vent: 10% gas, 100 LEL, Road vent: 0% gas, 0% LEL. The soil is dry at site, w/ no noticeable stray gas leaks.
2654473 Primary Facility 2017-09-15 Routine/Partial Inspection No Viols - Permanently Shut Down Visit site to check for gas odors: occasional odors. Breezy, partly cloudy, upper 70s. Metered vent stacks. Well stack: 0% gas, 2-18% LEL. Road stack: 4-8% gas, 100% LEL. (This is the reverse of prior metering. The road stack has vented little or no gas in the past.)
2654485 Primary Facility 2017-09-20 Routine/Partial Inspection No Viols - Permanently Shut Down Visit site to meter vent stacks. Well stack: 5-6% gas. Road stack: 20% gas.
2654502 Primary Facility 2017-10-25 Routine/Partial Inspection No Viols - Permanently Shut Down Drove by site, checked air for gas odors. Noted a definite gas odor in area around vent. Overcast, 43, still to light breeze.
2664291 Primary Facility 2017-11-15 Routine/Partial Inspection No Viols - Permanently Shut Down Met with representative at site from NCM Odor and Dust Control to evaluate the site for methane odor control. Rep was optimistic and planned to submit a proposal in next few weeks.
2675883 Primary Facility 2017-12-28 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to photograph area near Antaki where the plugged Pierce #1 well was reported to be located. Forwarded photos to Harrisburg
2723874 Primary Facility 2018-04-12 Routine/Partial Inspection No Viols - Permanently Shut Down Met with former and current DEP OGIs for Allegheny County to discuss possible approximate location of the plugged Pierce#1 well. Results were inconclusive.
2723887 Primary Facility 2018-04-18 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site after heavy rains. One section of yard can be seen bubbling gas. No other areas can be seen bubbling, but the grass is dying again in the same area as before. Windy day, so gas odors were not detected from ventpipes.
2723900 Primary Facility 2018-04-19 Routine/Partial Inspection No Viols - Permanently Shut Down Met with operator who plugged the Pierce #1 well on site. He indicated a general area in the Antaki yard, 30-40 feet south of the Antaki well.
2735290 Primary Facility 2018-05-08 Routine/Partial Inspection No Viols - Permanently Shut Down Ran DEP camera into augers left in well. Got down to 20' before hitting obstruction. Gas appeared to be entering at auger joints and not from below.
2750739 Primary Facility 2018-06-21 Routine/Partial Inspection No Viols - Permanently Shut Down Met with property owner to discuss future work to be done on the well and drop off consent form to completed.
2750878 Primary Facility 2018-06-28 Routine/Partial Inspection No Viols - Permanently Shut Down Met with property owner to pick up consent form for upcoming planned work on well.
2759580 Primary Facility 2018-08-02 Routine/Partial Inspection No Viols - Permanently Shut Down Held pre bid meeting at site for planned state-funded plugging. Four plugging contractors attended, along with DEP representatives.
2765614 Primary Facility 2018-08-21 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site after heavy rains to look for stray gas in yard. Found bubbles in yard across driveway from well vent. Also found bubbles 12-15 feet from well vent toward house. Could not check vents for gas, sampling port plugs rusted in place. No odor of gas in ambient air.
2771891 Primary Facility 2018-09-06 Routine/Partial Inspection No Viols - Permanently Shut Down Spoke to owner about upcoming activities to re-open, clean out and plug well.

Checked vent stacks for gas with Bascom Turner meter. Well stack maxed out at 19% gas, road vent tested 0% gas and LEL. Soil is dry, day is partly cloudy and breezy.

2789449 Primary Facility 2018-10-16 Routine/Partial Inspection No Viols - Permanently Shut Down Checked vent stacks for gas with Altair 5 meter. Well stack maxed out at 40 % gas, road vent tested 0% gas and LEL. Soil is damp, day is 49 degrees, partly cloudy and breezy.
2801673 Primary Facility 2018-11-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost preparing site to mobilize rig. Placing mats and containment. Staging rig and some equipment at pull-off along Mcaleer Road near wellsite until site is ready.
2802155 Primary Facility 2018-11-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continues to prepare site to mobilize rig. Placing mats and containment. Staging rig and some equipment at pull-off along Mcaleer Road near wellsite until site is ready.
2802302 Primary Facility 2018-11-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continues placing mats and containment, nearly completed. Rig remains at pull-off along Mcaleer Road near wellsite until site is ready.
2803036 Primary Facility 2018-11-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost has all mats placed, with rig and most of equipment on site.
2803424 Primary Facility 2018-11-15 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost has rig and most of equipment on site. Pipe tub and tank remain to be mobilized.
2803822 Primary Facility 2018-11-05 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Check on site. One Call was called, but utilities have not been marked yet. Yost will be mobilizing in about one week. Site is soggy with gas bubbling through areas of standing water.
2803866 Primary Facility 2018-11-15 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost has rig and all equipment on site, rigged up and ready to begin work on well plugging tomorrow.
2804252 Primary Facility 2018-11-16 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost Drilling pulled four 5' and one 3' augers from the the well. The 4.25" auger head was packed with twisted up steel casing and wood. Yost is setting up well control equipment at the surface.
2804862 Primary Facility 2018-11-19 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost pulled all 5 sections of hollow stem augers (25') and bit last week. Worked on remaining site details today to prepare to begin drilling/cleaning out well tomorrow.
2806042 Primary Facility 2018-11-21 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost shut down for holiday, will begin well cleanout next week. Checked road vent for gas: 0% LEL.
2806254 Primary Facility 2018-11-26 Plugging(Includes Plugged/Mined Through) In Compliance with Policy No activity at site, Yost shut down for holiday/deer season. Well appears stable with no leaks noted.
2807036 Primary Facility 2018-11-27 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost drilling/cleaning hole at 27' with 6 1/4" tricone. Good fluid circulation. Making short wiper trips while drilling and circulating. Cuttings are predominantly wood with some cavings.
2807291 Primary Facility 2018-11-28 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost cleaned hole to 27' with 6 1/4" tricone. Good fluid circulation. Cuttings are predominantly wood with some cavings and PVC fragments. Working on shale shaker - replacing rubber shaker mounts.
2807753 Primary Facility 2018-11-28 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost drilling has reached 32' with returns that are mixed with a sandy material, wood, and plastic.
2808002 Primary Facility 2018-11-29 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost cleaned hole to 32' yesterday with 6 1/4" tricone. Good fluid circulation. Mixing mud this AM. Plan to swap out tricone button bit with tricone tooth bit.
2808339 Primary Facility 2018-11-29 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost cleaned hole to 56' with 6 1/4" tricone button bit. Good fluid circulation, bringing out PVC fragments, cement (?) and scattered wood fragments.
2808829 Primary Facility 2018-11-29 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost is drilling pieces of plastic, wood and what looks like cement. Yost is using a tri-cone button bit and has reached a depth of 45'.
2808898 Primary Facility 2018-11-30 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost has drilled to 60'. Circulation was lost around 59'. Yost increased the mud weight and circulation returned. They have switched to a tri-cone tooth bit.
2809312 Primary Facility 2018-12-03 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost cleaning hole with 6 1/2" tricone tooth bit. (Lost fluid circulation last week at 61', shut down and mixed mud.) Resumed drilling/cleaning hole today from 61' to 86'. Losing circulation intermittently. Shut down to mix additional mud.
2809416 Primary Facility 2018-12-03 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost pulled off bottom at 86' and has been mixing mud all afternoon.
2809457 Primary Facility 2018-12-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost has drilled to a depth of 86'. Drilling with a 6.25" roller bit they are getting returns of a mostly sandy material with a slight petroleum odor.
2825303 Primary Facility 2018-12-04 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost rig resumed drilling/cleaning hole out with heavy mud from 86' to 101'; losing fluid entire time. At 101' rig operator noticed muddy water flowing out of nearby Antaki water well. Shut down mud pump and rig. Due to water use in house, water contaminated with drilling mud (bentonite) got pumped from the water well into house water system. Water in well initially tested up to 4% methane gas, but lowered to 30-40% LEL using Altair 5. Tested water and ambient air in basement of house: 0% LEL for water and all ambient air test locations.

Dean's Water is scheduled to plumb-in water buffalo and deliver fresh water tomorrow AM.

2826048 Primary Facility 2018-12-05 Plugging(Includes Plugged/Mined Through) In Compliance with Policy DEP water quality representatives on site to collect samples from pressure tank in basement and rig's drilling pit.

Cement truck on location before 2:00 PM. Pumped ~1 1/2 yds portland slurry into well in attempt to stop communication of gas well with water well. Finished and rigged down by 2:30 PM.

2826056 Primary Facility 2018-12-06 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost mixing mud to begin drilling out yesterday's cement squeeze job. Tagged TOC squeeze at 10'.
2826058 Primary Facility 2018-12-07 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost mixing mud to resume drilling out cement squeeze job. Yesterday they drilled out cement from 10'-56'.
2826155 Primary Facility 2018-12-07 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continues drilling out cement squeeze job. Good circulation with no fluid loss, no communication with water well. Drilled out to ~85'.
2826165 Primary Facility 2018-12-10 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost mixing mud and warming up equipment after weekend shutdown. Pit frozen.
2826628 Primary Facility 2018-12-10 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost tried to circulate drilling mud downhole to begin cleanout. Unknown to them, wellhead was frozen solid from weekend shutdown. Drilling mud began to leak from head. Shut down, cleaned up, thawed wellhead and flowline by end of day. Winterized lines and rig and SD.
2826632 Primary Facility 2018-12-11 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up equipment, circulating pit (mixing), preparing to resume cleanout.
2826636 Primary Facility 2018-12-11 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost drilled/cleaned out hole to 116'. Circulated old chunks, 1/4" to 1/2" thick, of solid petroleum that appear to have been on side of casing.
2827463 Primary Facility 2018-12-12 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up equipment and mixing mud.
2827475 Primary Facility 2018-12-12 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost cleaning/drilling hole at 143', all shale cuttings on shaker. Bascom Turner reading on water well 79% LEL maximum. Water level remains steady with no gain or loss of water level.
2827491 Primary Facility 2018-12-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost plans to drill 30' more on freshwater to clear mud from hole, blow dry, then run downhole camera on Monday.

Water well was shut in ~18 hours. Opened and tested gas level at 5% gas. Will leave open to vent

2827507 Primary Facility 2018-12-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost vacuumed mud from drillpit then drilled one rod on aerated water to clean out mud from hole. Vacuum truck stayed on site during drilling. TD 176'. Black shale cuttings last 30'. Blew hole dry, TOOH, SD.
2829009 Primary Facility 2018-12-17 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH and blew hole to clear water, but water quickly returned to prior level. Rigged up Yost downhole camera. Worked fine until started down hole, then shorted out. Couldn't repair, so rigged down camera. Duncan camera scheduled for tomorrow AM. Plan to drill/clean hole on aerated water for remainder of day
2829025 Primary Facility 2018-12-17 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost attempted to drill/clean out deeper on aerated water, but began to communicate with water well and road vent around base, so SD. Flushed hole with ~1,000 gallons fresh water from Dean's with drillpipe 1' off bottom.
2829309 Primary Facility 2018-12-18 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Duncan onsite with downhole camera, would not work. Had to rehead and rewire connections, got camera to work, but had to tape 3 flashlights to camera head to supplement lighting. Unable to record data, as recorder would not work. Vigorous gas bubbling made visibility through water difficult. Here is a summary of what was observed: Abundant water entering well at ~8', below bottom of 16" conductor. Blurred glimpses through bubbling water revealed what looked like casing or tubing along the side of wellbore to 72'. The side of the casing/tubing was missing and tapered to a "V" at 72'. The wellbore deviated from the outside of the casing below 72' and penetrated fresh bedrock.
2829327 Primary Facility 2018-12-19 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Century Wireline ran gyro survey. Well deviates 3.8' northwest from surface to bottom of hole at 168.74'.
2829349 Primary Facility 2018-12-20 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost drilled with 12 1/2" button bit to 8', TOOH, removed button bit, put on 6 1/2" tooth bit and TIH to clean out for tomorrow's camera run.
2829369 Primary Facility 2018-12-20 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost completed cleanout of hole, TOOH, SD.
2829398 Primary Facility 2018-12-21 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost cleaned and blew hole to attempt to dry, but too much water entering near surface. Ran DEP camera in hole. Unable to record data. Found top of water at 23'. All visible hole above water and below conductor was cement, with some casing visible along side of borehole at 23'.

Yost TIH with 12 1/2" bit and started cleaning/drilling out cement. TOOH, found large, balled-up mass of wood fragments stuck in bit. Appears to be wooden conductor.

2830106 Primary Facility 2018-12-26 Plugging(Includes Plugged/Mined Through) In Compliance with Policy No plugging activity on site due to holiday shutdown. Well appears stable. All good at site.
2830320 Primary Facility 2019-01-02 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH with 16' of 11 3/4" washover pipe, worked down through shallow water zone.
2830365 Primary Facility 2019-01-02 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost got all 16' of 11 3/4" washover pipe worked down. Grouted annulus with heavy gel. SD. Water level appears to have lowered somewhat after setting pipe.
2830390 Primary Facility 2019-01-03 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH with 2 drilling rods, blew hole, TOOH. Water level at 23'. Can see top of twisted section of casing at ~20'. DEP downhole camera scheduled for tomorrow AM.
2830403 Primary Facility 2019-01-04 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Ran DEP camera, got clear view of partial casing/tubing from 12'-46'. Hole bridged below 46', so TIH with drillpipe, blew hole and removed bridge. TIH with camera, but water cloudy, so pulled out with camera. Will run more 11 3/4" pipe, then possibly run camera again.
2830470 Primary Facility 2019-01-07 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost turned and worked 11 3/4" casing down to 21 feet, taking all day to do so. Will continue tomorrow.
2830569 Primary Facility 2019-01-08 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continuing working 11 3/4" casing down.
2830576 Primary Facility 2019-01-08 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continued working 11 3/4" casing down to 34'. Will run remaining 2 feet of casing tomorrow. Fluid communication in 16"-11 3/4" annulus, so plan is to grout when all casing run.
2830586 Primary Facility 2019-01-09 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost finish working 11 3/4" casing down. Will grout 16"-11 3/4" annulus when done.
2830596 Primary Facility 2019-01-09 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost finished working 11 3/4" casing down to 36'. Grouted 16"-11 3/4" annulus with cement.
2830617 Primary Facility 2019-01-10 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost re-grouted 16"-11 3/4" annulus with cement. Yesterday's grout job was bubbling gas.
2830629 Primary Facility 2019-01-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up equipment, thawing pit and lines.
2830650 Primary Facility 2019-01-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost developed a leak at the bowl that was on 16" casing, so nippled up a diverter head onto the 11 3/4" casing.
2830654 Primary Facility 2019-01-16 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH with 10 3/4" washover pipe, worked down to 34' while at site.
2830660 Primary Facility 2019-01-16 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost working at 37' with 10 3/4" washover pipe. A lot of wood fragments in returns.
2830669 Primary Facility 2019-01-17 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost still using 10 3/4" washover head to drill down. Current depth is 40'. At 39', penetration rate slowed significantly, so TOOH. Washover head was plugged with twisted strips of metal casing.
2830691 Primary Facility 2019-01-18 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost worked washover pipe back to yesterday's depth of 40'. Continue to get wood fragments with assorted cuttings.

Check gas levels with Bascom Turner meter: Water well: 12% gas, Road vent stack: 0 PPM

2830698 Primary Facility 2019-01-18 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost worked 10 3/4" washover to 43', wouldn't go any deeper. TOOH, found all tungsten was worn off leading edge of washover head.
2830703 Primary Facility 2019-01-22 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continues working 10 3/4" washover at 44 1/2'. Getting a lot of wood fragments in returns.
2830731 Primary Facility 2019-01-23 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continued working washover at 44 1/2', unable to get deeper. TOOH with washover, retrieved a 6+ foot section of half-casing and casing "ball". Rigged up a box tap and started fishing. Retrieved large chunks if old cement and fragments of casing after repeated trips.
2831081 Primary Facility 2019-01-24 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH with 6 1/2" large tooth tricone bit to clean and clear hole. Will mix heavy mud later to clean hole. Current depth before leaving location: 64'.
2831327 Primary Facility 2019-01-24 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH with 6 1/2" large tooth tricone bit, cleaned and cleared hole to 68'. Mixed heavy mud and circulated, brought up a lot more cuttings. SD
2831917 Primary Facility 2019-01-28 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up and thawing equipment and tanks after cold weekend. (Cleaned out hole to 75' with 6 1/2" tricone last Friday before shutting down for weekend.)
2832308 Primary Facility 2019-01-28 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continues drilling out/cleaning hole with 6 1/2" tricone bit. Current depth is 80'. Returns include cavings/cuttings, along with numerous wood fragments and occasional cement and plastic (PVC).
2832611 Primary Facility 2019-01-29 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost continues drilling out/cleaning hole with 6 1/2" tricone bit. Current depth is 83'. Returns are mostly cavings/cuttings.
2833132 Primary Facility 2019-01-29 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TOOH with 6 1/2" tricone after drilling out/cleaning to 84'. TIH with 10 3/4" washover, worked down from 44 1/2' to 50'. Circulate and mix heavy mud in preparation for sub-zero temperatures forecast for coming days.
2838387 Primary Facility 2019-02-11 Plugging(Includes Plugged/Mined Through) No Violations Noted Run down hole camera in well to determine depth and to help identify obstruction.
2838817 Primary Facility 2019-02-04 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up equipment and thawing water tank and pit after five day shutdown due to subzero weather.
2838843 Primary Facility 2019-02-04 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost worked 10 3/4" washover down to ~61 feet, pulled up and circulated.
2838887 Primary Facility 2019-02-05 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost working 10 3/4" washover down at 62 feet.

Bascom Turner gas readings: Water well: 680 PPM Road vent: 0 PPM Drilling pit: 140 PPM

2839999 Primary Facility 2019-02-05 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TOOH to check washover head. Head was filled with "core" of shale formation, casing collar and chunks of casing. TIH and continue working down through 68 1/2'. Still getting wood, PVC fragments and cement in cuttings.
2840002 Primary Facility 2019-02-06 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost working 10 3/4" washover down, at 72'. TOOH earlier to check washover head, was filled with 2-3' core of shale with partial borehole down side.
2840010 Primary Facility 2019-02-06 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost working 10 3/4" washover down, retrieved another core of shale with partial borehole down side. Tilted derrick slightly toward road, tripped back in with washover, set down at 51'.
2840211 Primary Facility 2019-02-07 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost working 10 3/4" washover down, at 57' after tilting derrick toward road.
2840231 Primary Facility 2019-02-07 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost worked 10 3/4" washover down to 61', where it met no resistance down to 72'. Cored 72' to 75', retrieved 3' of concrete with pea gravel aggregate (photo). Core has two separate well bores down sides.
2840291 Primary Facility 2019-02-11 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming equipment, getting ready to run DEP camera. Left water in hole (over weekend) for 1st camera run. Camera could not get a clear view of well through cloudy, gas-cut water despite weekend. Sat down on bridge at 62'. TIH with drill string to clear bridge and blow water, TOOH. Run camera again. Hole was dry to 43', but quickly filled with water. Got glimpse of a sliver of casing imbedded in cement of 11" sidewall before flooded with water. Poor visibility in murky water, camera sat down again below 63'. Unable to record either camera run.
2841028 Primary Facility 2019-02-12 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost preparing to cement 6 1/2" hole that strays from true wellbore from 180' back to ~70'.
2841034 Primary Facility 2019-02-12 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost pumped cement, pulled up to 70', circulated with water, TOOH, WOC.
2841037 Primary Facility 2019-02-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost TIH with 10" flat-bottom mill after tagging TOC at 73'.
2841039 Primary Facility 2019-02-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost milling at 73', metal and wood in returns.
2841045 Primary Facility 2019-02-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up equipment, thawing pit to continue milling at 74'.
2841280 Primary Facility 2019-02-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost milling at 76', a lot of metal shavings and wood in returns.
2842034 Primary Facility 2019-02-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost milling, are down to 80'.
2842036 Primary Facility 2019-02-15 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost will begin milling at 81' when rig maintenance and mud mixing is done.
2842068 Primary Facility 2019-02-15 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost milled to 84' with 10" flat-bottom mill, TOOH. Center port of mill had 8" spiraled chunk of casing wedged in it. TIH with 10 3/4" washover.
2842072 Primary Facility 2019-02-19 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost working 10 3/4" washover down, at 88'.
2842092 Primary Facility 2019-02-19 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost worked 10 3/4" washover down from 88' to 91'. TOOH, no core in head. Nippled up 6 1/4" tricone button bit, TIH. Drill/clean out hole from 88' to 116' (rod down).
2842134 Primary Facility 2018-09-28 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to check gas levels at vents with Altair 5. Slightly breezy, sunny afternoon.

Well stack: 60% gas Road stack: 0% LEL

2842237 Primary Facility 2019-02-20 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost drilling/cleaning out hole with 6 1/4" tricone bit. Hit soft spot void-like area from 138'-146'. Got abundant PVC chunks in returns from 174'-176'. TOOH to check bit at 178'. Three chunks of casing were wedged between the cones.
2842693 Primary Facility 2019-02-21 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Century Wireline on site to run directional survey on recent cleanout activity since plug back. Log shows well deviating northwest in a similar direction to survey run 12/19/18. Bottom of hole is 4.8' off vertical now, prior survey indicated bottom of hole 3.8' off vertical. CCL log indicates borehole is beside casing or metal entire depth of 179'.

Yost will TIH with a 6" taper mill.

2842986 Primary Facility 2019-02-21 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost milling metal at 81 feet with 6" mill.
2850525 Primary Facility 2019-03-08 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost began the day drilling with a 7 7/8" tri-cone bit through 90' of 8 5/8". They started drilling at a depth of190'.
2850533 Primary Facility 2019-03-06 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost is drilling through 90' of 8 5/8" casing with a 6.5" tri-cone. They have reached a depth of 244'.
2850541 Primary Facility 2019-03-07 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost changed bits from a 6.5" tri-cone to a 7 7/8" tri-cone. They are drilling at 124' through 90' of 8 5/8" casing.
2850936 Primary Facility 2019-03-05 Plugging(Includes Plugged/Mined Through) No Violations Noted Run down hole camera in well to determine depth and to help identify obstruction.
2853253 Primary Facility 2019-03-05 Routine/Complete Inspection In Compliance with Policy At the time of this inspection, activities related to the plugging of this well are ongoing. Timber mats are installed on a portion of the well site.

Yost representative Pat Novak on-site. Yost representative John Mouser arrived later during this inspection.

SDSs are on-site. The Department observed several areas where a small amount of fluids was spilled on containment and/or the timber mats. Mr. Novak confirmed that the well site is on containment; prior to bringing equipment on-site, a 60'x120' piece of containment with berms was installed on-site. Mr. Novak showed a picture to the Department depicting this containment on-site prior to bringing equipment on-site.

Mr. Novak also stated that no grading of the site was performed as part of the site preparation for plugging activities. The Department recommends that E&S BMPs are installed as needed for any earth disturbance activities which may occur or have occurred and that an E&S plan is developed and implemented for any earth disturbance activities w

2855670 Primary Facility 2019-03-19 Routine/Complete Inspection No Violations Noted Assisted southwest region with downhole camera to plug the well.
2856767 Primary Facility 2019-03-19 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost pulled 91' of 8 5/8" casing out of the well. A down hole pump was lowered to 100' to lower the water level in the boring.

A camera run showed casing at 67' with possibly 2" tubing inside.

2856818 Primary Facility 2019-03-20 Plugging(Includes Plugged/Mined Through) No Violations Noted Yost ran their own camera and around 65' it looked like there may be another casing string along with the smaller pipe inside.

For data sources see[5]

References