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Well ID: 0646062312000 | Loading map...
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Location: 00/12-23-064-06W6/0 | |
Location Alias: 00/12-23-64-06 W6M | |
Location Alias 2: 00/12-23-064-06 W6/00 | |
Country: Canada | |
Province: Alberta | |
Township: 064 | |
Meridian: 6 | |
Range: 06 | |
Section: 23 | |
County/Municipality: Municipal District of Greenview No. 16 | |
Well Name: LONG RUN HZ KAKWA 12-23-64-6 | |
Operator Name: Long Run Exploration Ltd. | |
License Number: 0479192 | |
License Date: 2016-03-23 | |
License Status: Issued | |
Spud Date: 2016-10-09 | |
Final Drill Date: 2016-10-23 | |
Well Total Depth: 3300.00 m | |
Surface Hole Latitude: 54.550451 | |
Surface Hole Longitude: -118.777536 |
Date | Event |
---|---|
2016-03-23 | Obtained License |
2016-10-09 | Lost Circulation Occurred |
2016-10-13 | Surface Casing Operation Performed |
2016-10-15 | Direction Drilling Operation Performed - Deviate |
2016-10-16 | Direction Drilling Operation Performed - Horizontal |
2016-10-18 | Intermediate Casing Operation Performed |
2016-10-18 | Well Log Performed |
2016-10-23 | Finished Drilling |
2016-10-23 | Well Log Performed |
2016-10-23 | Well Mode changed to Drilled and Cased |
2016-10-24 | Liner Casing Operation Performed |
2016-10-24 | Perforation Treatment Performed - Open-Hole Completion |
2016-10-24 | Well Log Performed |
2016-10-25 | Rig Released |
2016-12-10 | Well Fluid changed to Gas |
2016-12-10 | Well Mode changed to Testing |
2016-12-12 | Perforation Treatment Performed - Multi-Stage Fracture |
2017-01-10 | Well Began Production |
2017-01-10 | Well Fluid changed to Gas |
2017-01-10 | Well Mode changed to Flowing |
For data sources see[3]
Start Date | Depth (m) | Reason |
---|---|---|
2016-10-15 | 1315.00 | Deviate (5 - 79 degrees) |
2016-10-16 | 1696.00 | Horizontal |
For data sources see[4]
Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
---|---|---|---|---|
2016-10-24 | Open Hole/Barefoot Completion | 3293.30 | 3300.00 | 0 |
2016-12-12 | Multi-Stage Fracture | 2692.50 | 2693.00 | 0 |
2016-12-12 | Multi-Stage Fracture | 2624.30 | 2624.80 | 0 |
2016-12-12 | Multi-Stage Fracture | 2557.30 | 2557.80 | 0 |
2016-12-12 | Multi-Stage Fracture | 2489.00 | 2489.50 | 0 |
2016-12-12 | Multi-Stage Fracture | 2421.10 | 2421.60 | 0 |
2016-12-12 | Multi-Stage Fracture | 2353.10 | 2353.60 | 0 |
2016-12-12 | Multi-Stage Fracture | 2285.20 | 2285.70 | 0 |
2016-12-12 | Multi-Stage Fracture | 2217.40 | 2217.90 | 0 |
2016-12-12 | Multi-Stage Fracture | 2149.70 | 2150.20 | 0 |
2016-12-12 | Multi-Stage Fracture | 2082.00 | 2082.50 | 0 |
2016-12-12 | Multi-Stage Fracture | 3235.40 | 3236.30 | 0 |
2016-12-12 | Multi-Stage Fracture | 2014.10 | 2014.60 | 0 |
2016-12-12 | Multi-Stage Fracture | 1946.80 | 1947.30 | 0 |
2016-12-12 | Multi-Stage Fracture | 1879.10 | 1879.60 | 0 |
2016-12-12 | Multi-Stage Fracture | 1798.80 | 1799.30 | 0 |
2016-12-12 | Multi-Stage Fracture | 3166.70 | 3167.20 | 0 |
2016-12-12 | Multi-Stage Fracture | 3098.70 | 3099.20 | 0 |
2016-12-12 | Multi-Stage Fracture | 3031.30 | 3031.80 | 0 |
2016-12-12 | Multi-Stage Fracture | 2963.40 | 2963.90 | 0 |
2016-12-12 | Multi-Stage Fracture | 2895.80 | 2896.30 | 0 |
2016-12-12 | Multi-Stage Fracture | 2828.10 | 2828.60 | 0 |
2016-12-12 | Multi-Stage Fracture | 2760.10 | 2760.60 | 0 |
For data sources see[5]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2016-12-12 | 2016-12-12 | 1,581 | 580 | N/A |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Water | Not Available | 100 | 38.987 | N/A | |||
FRAC SAND. 20/40 WHITE (OTTAWA TYPE) | Baker Hughes | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 29.5568 | N/A | ||
Alpha 544 | Baker Hughes | Bactericide/Biocide | 2.2-Dibromo-3-nitrilopropionamide | 10222-01-2 | 100 | 0.005 | N/A | |
Dibromoacetonitrile | 3252-43-5 | 100 | 0.005 | N/A | ||||
Polyethylene Glycol | 25322-68-3 | 100 | 0.005 | N/A | ||||
Sodium Bromide | 7647-15-6 | 100 | 0.005 | N/A | ||||
GBW-41LW | Baker Hughes | Breaker | Hydrogen Peroxide | 7722-84-1 | 100 | 0.1187 | N/A | |
Methanol | 67-56-1 | 100 | 0.1187 | N/A | ||||
Non-hazardous | Not Available | 100 | 0.1187 | N/A | ||||
FP-13L | Baker Hughes | Defoamer | Tributyl phosphate | 126-73-8 | 100 | 0.0039 | N/A | |
D-3 | Baker Hughes | Demulsifier | Ethoxylated alcohol. branched | 78330-19-5 | 100 | 0.0292 | N/A | |
Isopropanol | 67-63-0 | 100 | 0.0292 | N/A | ||||
Methanol | 67-56-1 | 100 | 0.0292 | N/A | ||||
Nitrogen | Baker Hughes | Energizing Fluid | Nitrogen | 7727-37-9 | 100 | 30.6729 | N/A | |
MaxPerm-20A | Baker Hughes | Friction Reducer | Non-hazardous | 9014 | 100 | 0.2627 | N/A | |
Oxyalkylated alcohol | 9014 | 100 | 0.2627 | N/A | ||||
Petroleum distillates | 64742-47-8 | 100 | 0.2627 | N/A | ||||
Polyacrylate | 9014 | 100 | 0.2627 | N/A | ||||
Nowferr 14P | Baker Hughes | Iron Control | Cupric sulphate. pentahydrate | 7758-99-8 | 100 | 0.003 | N/A | |
Flo-Back 30 | Baker Hughes | Surfactant | Cocamido propyl betaine | 61789-40-0 | 100 | 0.3604 | N/A | |
Glycerine | 56-81-5 | 100 | 0.3605 | N/A | ||||
Non-hazardous | Not Available | 100 | 0.3604 | N/A |
For data sources see[6]
Water Diversion Start Date | Water Diversion End Date | Water Source Type | Total Water Volume (m3) |
---|---|---|---|
2016-12-10 | 2016-12-12 | Surface Water - Runoff | 700 |
For data sources see[7]
Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
---|---|---|---|---|
2016 | 134 | 0.0 | 0.0 | 0.0 |
2017 | 8439 | 0.0 | 0.0 | 0.0 |
2018 | 8635 | 0.0 | 0.0 | 0.0 |
2019 | 8674 | 0.0 | 0.0 | 0.0 |
2020 | 2183 | 0.0 | 0.0 | 0.0 |
For data sources see[8]
Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
---|---|---|---|
2016-10-09 | Lost Circulation | 25.00 | 133.00 |
2016-12-22 | No Incident Encountered | 0.00 | 0.00 |
For data sources see[9]