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Well ID: 0646061312000 | Loading map...
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Location: 00/12-13-064-06W6/0 | |
Location Alias: 00/12-13-64-06 W6M | |
Location Alias 2: 00/12-13-064-06 W6/00 | |
Country: Canada | |
Province: Alberta | |
Township: 064 | |
Meridian: 6 | |
Range: 06 | |
Section: 13 | |
County/Municipality: Municipal District of Greenview No. 16 | |
Well Name: LONG RUN HZ KAKWA 12-13-64-6 | |
Operator Name: Long Run Exploration Ltd. | |
License Number: 0479605 | |
License Date: 2016-06-03 | |
License Status: Issued | |
Spud Date: 2016-12-28 | |
Final Drill Date: 2017-01-10 | |
Well Total Depth: 2973.00 m | |
Surface Hole Latitude: 54.541196 | |
Surface Hole Longitude: -118.756006 |
Date | Event |
---|---|
2016-06-03 | Obtained License |
2016-12-29 | Surface Casing Operation Performed |
2016-12-31 | Direction Drilling Operation Performed - Deviate |
2016-12-31 | Direction Drilling Operation Performed - Horizontal |
2017-01-02 | Intermediate Casing Operation Performed |
2017-01-10 | Finished Drilling |
2017-01-10 | Liner Casing Operation Performed |
2017-01-10 | Perforation Treatment Performed - Open-Hole Completion |
2017-01-10 | Well Log Performed |
2017-01-10 | Well Mode changed to Drilled and Cased |
2017-01-11 | Rig Released |
2017-01-24 | Perforation Treatment Performed - Multi-Stage Fracture |
2017-02-07 | Well Fluid changed to Gas |
2017-02-07 | Well Mode changed to Testing |
2017-03-01 | Well Began Production |
2017-03-01 | Well Fluid changed to Gas |
2017-03-01 | Well Mode changed to Flowing |
For data sources see[3]
Spud Date | Contractor | Rig Number | New Projected Depth (m) | Activity Type |
---|---|---|---|---|
2016-12-28 | Bonanza Drilling Inc. | 9 | N/A | Drill To LD |
For data sources see[4]
Start Date | Depth (m) | Reason |
---|---|---|
2016-12-31 | 1419.80 | Deviate (5 - 79 degrees) |
2016-12-31 | 1743.30 | Horizontal |
For data sources see[5]
Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
---|---|---|---|---|
2017-01-10 | Open Hole/Barefoot Completion | 2965.70 | 2973.00 | 0 |
2017-01-24 | Multi-Stage Fracture | 2500.50 | 2501.00 | 0 |
2017-01-24 | Multi-Stage Fracture | 2455.10 | 2455.60 | 0 |
2017-01-24 | Multi-Stage Fracture | 2409.80 | 2410.30 | 0 |
2017-01-24 | Multi-Stage Fracture | 2350.90 | 2351.40 | 0 |
2017-01-24 | Multi-Stage Fracture | 2305.50 | 2306.00 | 0 |
2017-01-24 | Multi-Stage Fracture | 2246.60 | 2247.10 | 0 |
2017-01-24 | Multi-Stage Fracture | 2201.30 | 2201.80 | 0 |
2017-01-24 | Multi-Stage Fracture | 2142.40 | 2142.90 | 0 |
2017-01-24 | Multi-Stage Fracture | 2097.10 | 2097.60 | 0 |
2017-01-24 | Multi-Stage Fracture | 2038.20 | 2038.70 | 0 |
2017-01-24 | Multi-Stage Fracture | 2931.50 | 2932.40 | 0 |
2017-01-24 | Multi-Stage Fracture | 1992.90 | 1993.40 | 0 |
2017-01-24 | Multi-Stage Fracture | 1934.00 | 1934.50 | 0 |
2017-01-24 | Multi-Stage Fracture | 1888.70 | 1889.20 | 0 |
2017-01-24 | Multi-Stage Fracture | 2872.00 | 2872.50 | 0 |
2017-01-24 | Multi-Stage Fracture | 2813.20 | 2813.70 | 0 |
2017-01-24 | Multi-Stage Fracture | 2767.90 | 2768.40 | 0 |
2017-01-24 | Multi-Stage Fracture | 2709.00 | 2709.50 | 0 |
2017-01-24 | Multi-Stage Fracture | 2663.70 | 2664.20 | 0 |
2017-01-24 | Multi-Stage Fracture | 2604.80 | 2605.30 | 0 |
2017-01-24 | Multi-Stage Fracture | 2559.40 | 2559.90 | 0 |
For data sources see[6]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2017-01-24 | 2017-01-24 | 1,647 | 545 | N/A |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Water | 7732-18-5 | 100 | 45.615 | N/A | |||
FRAC SAND. 20/40 WHITE (OTTAWA TYPE) | Baker Hughes | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 30.3631 | N/A | ||
Alpha 544 | Baker Hughes | Bactericide/Biocide | 2.2-Dibromo-3-nitrilopropionamide | 10222-01-2 | 100 | 0.0041 | N/A | |
Dibromoacetonitrile | 3252-43-5 | 100 | 0.0041 | N/A | ||||
Polyethylene Glycol | 25322-68-3 | 100 | 0.0041 | N/A | ||||
Sodium Bromide | 7647-15-6 | 100 | 0.0041 | N/A | ||||
Water | 7732-18-5 | 100 | 0.0041 | N/A | ||||
GBW-41LW | Baker Hughes | Breaker | Hydrogen Peroxide | 7722-84-1 | 100 | 0.1372 | N/A | |
Methanol | 67-56-1 | 100 | 0.1372 | N/A | ||||
Non-hazardous | Not Available | 100 | 0.1372 | N/A | ||||
ClayMix | Baker Hughes | Clay Control | Choline chloride | 67-48-1 | 100 | 0.1001 | N/A | |
Complex polyamine salt | 138879-94-4 | 100 | 0.1001 | N/A | ||||
Non-hazardous | Not Available | 100 | 0.1001 | N/A | ||||
Water | 7732-18-5 | 100 | 0.1001 | N/A | ||||
D-3 | Baker Hughes | Demulsifier | Ethoxylated alcohol. branched | 78330-19-5 | 100 | 0.0356 | N/A | |
Isopropanol | 67-63-0 | 100 | 0.0356 | N/A | ||||
Methanol | 67-56-1 | 100 | 0.0356 | N/A | ||||
Nitrogen | Baker Hughes | Energizing Fluid | Nitrogen | 7727-37-9 | 100 | 25.5706 | N/A | |
FAW-30 | Baker Hughes | Friction Reducer | Amine derivative | 9842 | 100 | 0.4482 | N/A | |
Glycerine | 56-81-5 | 100 | 0.4482 | N/A | ||||
MaxPerm-20A | Baker Hughes | Friction Reducer | Non-hazardous | 9014 | 100 | 0.2976 | N/A | |
Oxyalkylated alcohol | 9014 | 100 | 0.2976 | N/A | ||||
Petroleum distillates | 64742-47-8 | 100 | 0.2976 | N/A | ||||
Polyacrylate | 9014 | 100 | 0.2976 | N/A |
For data sources see[7]
Water Diversion Start Date | Water Diversion End Date | Water Source Type | Total Water Volume (m3) |
---|---|---|---|
2017-01-16 | 2017-01-25 | Surface Water - Runoff | 690 |
For data sources see[8]
Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
---|---|---|---|---|
2017 | 5938 | 0.0 | 0.0 | 0.0 |
2018 | 8545 | 0.0 | 0.0 | 0.0 |
2019 | 7960 | 0.0 | 0.0 | 0.0 |
2020 | 2183 | 0.0 | 0.0 | 0.0 |
For data sources see[9]
Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
---|---|---|---|
2017-01-11 | No Incident Encountered | 0.00 | 0.00 |
2017-01-29 | No Incident Encountered | 0.00 | 0.00 |
For data sources see[10]