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Well ID: 0646061216020 | Loading map...
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Location: 02/16-12-064-06W6/0 | |
Location Alias: 02/16-12-64-06 W6M | |
Location Alias 2: 02/16-12-064-06 W6/00 | |
Country: Canada | |
Province: Alberta | |
Township: 064 | |
Meridian: 6 | |
Range: 06 | |
Section: 12 | |
County/Municipality: Municipal District of Greenview No. 16 | |
Well Name: LONG RUN HZ 102 KAKWA 16-12-64-6 | |
Operator Name: Long Run Exploration Ltd. | |
License Number: 0469030 | |
License Date: 2014-08-12 | |
License Status: Amended | |
Spud Date: 2014-11-02 | |
Final Drill Date: 2014-11-22 | |
Well Total Depth: 2951.00 m | |
Surface Hole Latitude: 54.530402 | |
Surface Hole Longitude: -118.781037 |
Date | Event |
---|---|
2014-08-12 | Obtained License |
2014-11-02 | Lost Circulation Occurred |
2014-11-05 | Surface Casing Operation Performed |
2014-11-07 | Direction Drilling Operation Performed - Deviate |
2014-11-09 | Direction Drilling Operation Performed - Horizontal |
2014-11-13 | Intermediate Casing Operation Performed |
2014-11-22 | Finished Drilling |
2014-11-22 | Well Log Performed |
2014-11-22 | Well Mode changed to Drilled and Cased |
2014-11-23 | Liner Casing Operation Performed |
2014-11-23 | Perforation Treatment Performed - Open-Hole Completion |
2014-11-24 | Rig Released |
2014-12-16 | Perforation Treatment Performed - Multi-Stage Fracture |
2014-12-29 | Well Began Production |
2014-12-29 | Well Fluid changed to Gas |
2014-12-29 | Well Mode changed to Flowing |
For data sources see[3]
Spud Date | Contractor | Rig Number | New Projected Depth (m) | Activity Type |
---|---|---|---|---|
2014-11-02 | Trinidad Drilling Ltd. | 21 | N/A | Drill To LD |
For data sources see[4]
Start Date | Depth (m) | Reason |
---|---|---|
2014-11-07 | 1276.30 | Deviate (5 - 79 degrees) |
2014-11-09 | 1714.50 | Horizontal |
For data sources see[5]
Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
---|---|---|---|---|
2014-11-23 | Open Hole/Barefoot Completion | 2943.00 | 2951.00 | 0 |
2014-12-16 | Multi-Stage Fracture | 2486.50 | 2487.00 | 0 |
2014-12-16 | Multi-Stage Fracture | 2426.60 | 2427.10 | 0 |
2014-12-16 | Multi-Stage Fracture | 2394.00 | 2394.50 | 0 |
2014-12-16 | Multi-Stage Fracture | 2177.60 | 2178.10 | 0 |
2014-12-16 | Multi-Stage Fracture | 2131.30 | 2131.80 | 0 |
2014-12-16 | Multi-Stage Fracture | 2087.60 | 2088.10 | 0 |
2014-12-16 | Multi-Stage Fracture | 2041.10 | 2041.60 | 0 |
2014-12-16 | Multi-Stage Fracture | 1981.00 | 1981.50 | 0 |
2014-12-16 | Multi-Stage Fracture | 1934.30 | 1934.80 | 0 |
2014-12-16 | Multi-Stage Fracture | 1888.40 | 1888.90 | 0 |
2014-12-16 | Multi-Stage Fracture | 2923.70 | 2924.60 | 0 |
2014-12-16 | Multi-Stage Fracture | 1841.50 | 1842.00 | 0 |
2014-12-16 | Multi-Stage Fracture | 1781.10 | 1781.60 | 0 |
2014-12-16 | Multi-Stage Fracture | 2862.90 | 2863.40 | 0 |
2014-12-16 | Multi-Stage Fracture | 2802.60 | 2803.10 | 0 |
2014-12-16 | Multi-Stage Fracture | 2756.10 | 2756.60 | 0 |
2014-12-16 | Multi-Stage Fracture | 2695.40 | 2695.90 | 0 |
2014-12-16 | Multi-Stage Fracture | 2649.10 | 2649.60 | 0 |
2014-12-16 | Multi-Stage Fracture | 2602.40 | 2602.90 | 0 |
2014-12-16 | Multi-Stage Fracture | 2543.80 | 2544.30 | 0 |
For data sources see[6]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2014-12-16 | 2014-12-16 | 1,548 | 477 | N/A |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Water | Not Available | 100 | 37.7469 | N/A | |||
FRAC SAND. 20/40 WHITE (OTTAWA TYPE) | Baker Hughes | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 31.6517 | N/A | ||
2K7 Solution W-M | Baker Hughes | Bactericide/Biocide | 2-Bromo-2-nitropropane-1.3-diol | 52-51-7 | 100 | 0.0191 | N/A | |
Methanol | 67-56-1 | 100 | 0.0191 | N/A | ||||
Water | 7732-18-5 | 100 | 0.0191 | N/A | ||||
GBW-41LW | Baker Hughes | Breaker | Hydrogen Peroxide | 7722-84-1 | 100 | 0.0165 | N/A | |
Methanol | 67-56-1 | 100 | 0.0165 | N/A | ||||
Non-hazardous | Not Available | 100 | 0.0165 | N/A | ||||
Nitrogen | Baker Hughes | Energizing Fluid | Nitrogen | 7727-37-9 | 100 | 30.2215 | N/A | |
MaxPerm-20A | Baker Hughes | Friction Reducer | Non-hazardous | 9014 | 100 | 0.2412 | N/A | |
Oxyalkylated alcohol | 9014 | 100 | 0.2412 | N/A | ||||
Petroleum distillates | 64742-47-8 | 100 | 0.2412 | N/A | ||||
Polyacrylate | 9014 | 100 | 0.2412 | N/A | ||||
Nowferr 14P | Baker Hughes | Iron Control | Cupric sulphate. pentahydrate | 7758-99-8 | 100 | 0.0019 | N/A | |
FAW-26 | Baker Hughes | Surfactant | 1-Butoxy-2-propanol | 5131-66-8 | 100 | 0.1008 | N/A | |
Diethanolamine | 111-42-2 | 100 | 0.1008 | N/A | ||||
Ethanol | 64-17-5 | 100 | 0.1008 | N/A | ||||
Methanol | 67-56-1 | 100 | 0.1007 | N/A | ||||
Polyoxyalkylene sulfate | 68891-29-2 | 100 | 0.1007 | N/A |
For data sources see[7]
Water Diversion Start Date | Water Diversion End Date | Water Source Type | Total Water Volume (m3) |
---|---|---|---|
2014-12-14 | 2014-12-15 | Surface Water - Runoff | 720 |
For data sources see[8]
Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
---|---|---|---|---|
2014 | 216 | 0.0 | 0.0 | 0.0 |
2015 | 8172 | 0.0 | 0.0 | 0.0 |
2016 | 8338 | 0.0 | 0.0 | 0.0 |
2017 | 8371 | 0.0 | 0.0 | 0.0 |
2018 | 8679 | 0.0 | 0.0 | 0.0 |
2019 | 8579 | 0.0 | 0.0 | 0.0 |
2020 | 2183 | 0.0 | 0.0 | 0.0 |
For data sources see[9]
Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
---|---|---|---|
2014-11-02 | Lost Circulation | 75.00 | 440.00 |
2014-12-22 | No Incident Encountered | 0.00 | 0.00 |
For data sources see[10]