X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

0444010810000

Well Details

Well ID: 0444010810000
Loading map...
Location: 00/10-08-044-01W4/0
Location Alias: 00/10-08-44-01 W4M
Location Alias 2: 00/10-08-044-01 W4/00
Country: Canada
Province: Alberta
Township: 044
Meridian: 4
Range: 01
Section: 08
County/Municipality: Municipal District of Wainwright No. 61
Well Name: TIKA RADIAL ET AL CHAUVIN 10-8-44-1
Operator Name: Surge Energy Inc.
License Number: 0065474
License Date: 1977-08-29
License Status: Abandoned
Spud Date: 1977-08-29
Final Drill Date: 1977-09-01
Well Total Depth: 746.80 m
Surface Hole Latitude: 52.777721
Surface Hole Longitude: -110.107608

For data sources see[1][2]

Well History

Date Event
1909-09-09 Well Log Performed
1977-08-29 Obtained License
1977-09-01 Drill Stem Test Performed
1977-09-01 Finished Drilling
1977-09-02 Drill Stem Test Performed
1977-09-02 Production Casing Operation Performed
1977-10-08 Well Mode changed to Drilled and Cased
1982-06-08 Perforation Treatment Performed - Cement Squeeze
1982-06-08 Perforation Treatment Performed - Selective Jet Perforations
1982-06-09 Perforation Treatment Performed - Acid Squeeze - Press Used
1982-06-09 Perforation Treatment Performed - Jet Perforation
1982-06-10 Perforation Treatment Performed - Jet Perforation
1982-06-11 Perforation Treatment Performed - Acid Squeeze - Press Used
2007-11-22 Perforation Treatment Performed - Bridge Plug Capped W/Cement
2007-11-22 Perforation Treatment Performed - Jet Perforation
2007-11-22 Plug Back Performed
2007-11-22 Well Log Performed
2007-11-22 Well Mode changed to Abandoned Zone
2007-11-23 Perforation Treatment Performed - Remedial Casing
2007-11-26 Perforation Treatment Performed - Cement Plug
2007-11-26 Plug Back Performed
2015-01-12 Well Log Performed
2015-01-13 Perforation Treatment Performed - Jet Perforation
2015-01-13 Perforation Treatment Performed - Remedial Casing
2015-01-13 Well Log Performed
2015-01-14 Perforation Treatment Performed - Cement Plug
2015-01-14 Plug Back Performed
2015-01-30 Perforation Treatment Performed - Jet Perforation
2015-01-30 Perforation Treatment Performed - Remedial Casing
2015-01-30 Well Log Performed
2015-02-02 Perforation Treatment Performed - Cement Plug
2015-02-02 Plug Back Performed
2015-02-06 Well Abandoned
2015-02-06 Well Mode changed to Abandoned

For data sources see[3]


Perforation Treatments

Perforation Date Perforation Type Interval Top (m) Interval Base (m) Number of Shots
1982-06-08 Selective Jet Perforations 580.00 580.00 0
2007-11-23 Remedial Casing Cementing 342.00 343.00 0
2007-11-23 Remedial Casing Cementing 228.00 229.00 0
2007-11-26 Cement Plug 132.60 358.00 0
2015-01-13 Perforation 234.00 235.00 17
2015-01-13 Remedial Casing Cementing 234.00 235.00 0
2015-01-13 Perforation 224.00 225.00 20
2015-01-13 Remedial Casing Cementing 224.00 225.00 0
2015-01-14 Cement Plug 150.80 246.00 0
2015-01-30 Perforation 194.00 195.00 18
2015-01-30 Remedial Casing Cementing 194.00 195.00 0
1982-06-08 Cement Squeeze 580.00 580.00 0
2015-02-02 Cement Plug 147.30 210.30 0
1982-06-09 Perforation 569.00 570.00 7
1982-06-09 Acid Treatment 569.00 570.00 0
1982-06-10 Perforation 571.20 572.40 7
1982-06-11 Acid Treatment 569.00 572.40 0
2007-11-22 Packing Device Capped w/Cement 556.00 564.00 0
2007-11-22 Perforation 342.00 343.00 13
2007-11-22 Perforation 228.00 229.00 13

For data sources see[4]


Occurences

Occurence Date Occurence Type Occurence Depth (m) Occurence Control Depth (m)
2015-02-04 No Incident Encountered 0.00 0.00

For data sources see[5]

References