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Well ID: 0224070207002 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Location: 00/07-02-022-07W4/2 | |
Location Alias: 00/07-02-22-07 W4M | |
Location Alias 2: 00/07-02-022-07 W4/02 | |
Country: Canada | |
Province: Alberta | |
Township: 022 | |
Meridian: 4 | |
Range: 07 | |
Section: 02 | |
County/Municipality: Special Areas No. 2 | |
Well Name: SLE ATL-BUFF 7-2-22-7 | |
Operator Name: SanLing Energy Ltd. | |
License Number: 0043769 | |
License Date: 1972-10-06 | |
License Status: Abandoned | |
Spud Date: 1972-10-12 | |
Final Drill Date: 1972-10-17 | |
Well Total Depth: 947.90 m | |
Surface Hole Latitude: 50.839075 | |
Surface Hole Longitude: -110.865943 |
Date | Event |
---|---|
1909-09-09 | Well Log Performed |
1972-10-06 | Obtained License |
1972-10-17 | Finished Drilling |
1972-10-17 | Lost Circulation Occurred |
1972-10-17 | Well Mode changed to Drilled and Cased |
1972-10-18 | Drill Stem Test Performed |
1972-10-19 | Production Casing Operation Performed |
1973-10-29 | Perforation Treatment Performed - Jet Perforation |
1996-08-16 | Well Log Performed |
1996-08-19 | Perforation Treatment Performed - Cement Squeeze |
1996-08-19 | Plug Back Performed |
1996-08-20 | Well Log Performed |
1996-08-21 | Perforation Treatment Performed - Jet Perforation |
1996-08-21 | Well Log Performed |
1996-08-22 | Well Log Performed |
1996-10-15 | Well Began Injection |
1996-10-15 | Well Fluid changed to Water |
1996-10-15 | Well Type changed to Disposal |
1999-01-24 | Perforation Treatment Performed - Bridge Plug Capped W/Cement |
1999-01-24 | Plug Back Performed |
1999-01-25 | Perforation Treatment Performed - Jet Perforation |
1999-01-25 | Well Fluid changed to Water |
1999-01-25 | Well Type changed to Disposal |
1999-09-01 | Well Fluid changed to Water |
1999-09-01 | Well Mode changed to Suspended |
1999-09-01 | Well Type changed to Disposal |
2018-01-13 | Perforation Treatment Performed - Bridge Plug Capped W/Cement |
2018-01-13 | Plug Back Performed |
2018-01-13 | Well Fluid changed to Water |
2018-01-13 | Well Mode changed to Abandoned Zone |
2018-01-13 | Well Type changed to Disposal |
2018-02-26 | Well Abandoned |
For data sources see[3]
Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
---|---|---|---|---|
1973-10-29 | Perforation | 913.80 | 916.80 | 13 |
1973-10-29 | Perforation | 918.70 | 925.40 | 13 |
1996-08-19 | Cement Squeeze | 913.80 | 925.40 | 0 |
1996-08-21 | Perforation | 938.80 | 941.50 | 13 |
1999-01-24 | Packing Device Capped w/Cement | 922.00 | 930.00 | 0 |
1999-01-25 | Perforation | 195.00 | 200.00 | 20 |
2018-01-13 | Packing Device Capped w/Cement | 175.50 | 183.50 | 0 |
For data sources see[4]
Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
---|---|---|---|---|
1997 | 0 | 0.0 | 0.0 | 0.0 |
1998 | 0 | 0.0 | 0.0 | 0.0 |
For data sources see[5]
Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
---|---|---|---|
1972-10-17 | Lost Circulation | 729.10 | 729.10 |
2018-01-13 | No Incident Encountered | 0.00 | 0.00 |
For data sources see[6]