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34-119-28035

Well Details

Well ID: 34-119-28035
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Country: United States
State: Ohio
County: Muskingum
Municipality: Highland Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: KING T P - KING CLYDE
License Status: Producing
License Date: 1996-06-06
Spud Date: 1996-07-28
Spud Drilling Contractor: G & H DRLG
Final Drill Date: 1996-08-07
Well Total Depth: 7105 ft
Configuration: Vertical
Latitude: 40.065970686
Longitude: -81.72561352

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1996-06-06 4431 VALLEY ENTERPRISES GeoDate 6/6/96
Oil and Gas 1996-06-06 Issued Date 6/6/96 Expired Date Acres 0040000 Tool Type RTAF Proposed Formation COPPER RIDGE Proposed Depth Proposed Drill Depth
Original Spud 1996-07-28 ?=LOG TYPE ( VDL ) IP. AT 30-35MCFG
Completed 1996-08-07 ?=LOG TYPE ( VDL ) IP. AT 30-35MCFG
Reached Total Depth 1996-08-07 ?=LOG TYPE ( VDL ) IP. AT 30-35MCFG
Completion Report Received 1997-01-30 ?=LOG TYPE ( VDL ) IP. AT 30-35MCFG
Construction Permit Expires 1997-06-06 ?=LOG TYPE ( VDL ) IP. AT 30-35MCFG
Change of Owner 2007-12-13 Operator changed from 4431, VALLEY ENTERPRISES to 1333, BIG SKY ENERGY INC
Record Last Modified 2017-02-15 ?=LOG TYPE ( VDL ) IP. AT 30-35MCFG

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 6995 7001 13
1997-06-29 6945 0
2006-09-11 7080 7090 21
2006-09-11 7022 7032 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 TREATED W/3000 GAL ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1996 VALLEY ENTERPRISES 1326 0 28
2001 VALLEY ENTERPRISES 3878 60 320
2008 BIG SKY ENERGY INC 0 0 0
2009 BIG SKY ENERGY INC 660 0 365
2011 BIG SKY ENERGY INC 26 0 365
2012 BIG SKY ENERGY INC 52 0 366
2013 BIG SKY ENERGY INC 200 0 250
2014 BIG SKY ENERGY INC 0 0 250
2016 BIG SKY ENERGY INC 0 0 0
2017 BIG SKY ENERGY INC 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1996 VALLEY ENTERPRISES Brine 0 28
2001 VALLEY ENTERPRISES Brine 0 320
2008 BIG SKY ENERGY INC Brine 0 0
2009 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 250
2014 BIG SKY ENERGY INC Brine 0 250
2016 BIG SKY ENERGY INC Brine 0 0
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0321797318 2004-02-20 Preliminary Restoration No Violations
0504821287 2009-06-15 Production Wells No Violations Well is on line. Appears to be selling gas.
0635902781 2008-03-19 Production Wells No Violations On line, meter on production unit has been removed. Shut-in at the sales point.
0868017055 2014-04-28 Production Wells Violations Noted Well is a producing well and in line with the well API# 5038. The production for the last two years does not meet the Minimum Criteria for production of 100 MCF per year. The well is shut in at the Dominion Master meter as a result of the Suspension Order. There is no identification at the well. Place an identification at the well . Plug well with in 180 days of the Compliance Action [CA date] date. Place identification with in 15 days of the CA date. Failure to comply will result in a Chiefs Order.
0991325699 2014-10-29 Administrative Inspection No Violations I called Greg Henderson with Big Sky. He stated that as soon as Dominion fixes line that they will be in line with well. He will call.
1064416044 2003-09-24 Production Wells No Violations Tubing pulled out of well and laying on ground. Location needs work to stop erosion.
1197681803 2017-11-28 Production Wells No Violations The purpose of my inspection is due to a follow-up to Chiefs order number 2015-[1]210 barrel steel tank that is enclosed within an earthen impoundment.
1405630446 2016-04-16 Production Wells Violations Noted The follow-up inspection is due to a Temporary Restraining Order issued in the Trumbull County Court of Common Pleas and the Chiefs Order #2015-535, Chiefs Order #2016-105.

The well is an idle well with no place for the gas to go. The meters down on Stoney point road have been shut in since 11-13--

1416321127 2014-11-18 Production Wells No Violations I met with Greg Henderson of Big Sky on well and he had hooked well up from annulus of 4.5casing and the inside of the 4.5casing. The well is now selling into the Dominion line at the bottom of the hill. This is resolving the compliance notice #868017055.
1940471622 2014-10-29 Production Wells No Violations I checked well and identification is in place. The well has been shut in due to Dominion. This is partially resolving the compliance notice #868017055.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0868017055 US-OH-129874 2014-12-31 Failure to legibly identify well
0868017055 US-OH-129875 2014-12-31 Well shall be plugged
1405630446 US-OH-111952 2016-06-17 Failure to have required locks, bull plugs
1405630446 US-OH-111953 2016-07-26 NONE Well shall be plugged

For data sources see[9]

References