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Well ID: 37-063-36003 | Loading map...
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Operator Name: ALLIANCE PETROLEUM CORP | |
First Permit Date: 2008-07-28 | |
Last Permit Date: 2008-07-28 | |
Spud Date: 2008-11-04 | |
Unconventional: No | |
Horizontal: No | |
Violations: None | |
Latitude: 40.461037 | |
Longitude: -79.036442 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2011-0 | 19973.35 | 365.0 | 0.0 | 0.0 | 0.01 | 365.0 |
2010-0 | 4095.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2009-0 | 8424.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2011-0 | PRODUCED FLUID | 75.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY | JOSEPHINE | PA |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1873427 | 2010-03-26 | No Violations Noted | According to records, permit was granted 7/28/09 and no record of WRAC submitted and approved at the DEP. Well completed with 8¿ pipe reduced to 4¿ pipe reduced 2¿ production pipe with shut off valves. Total gas volume meter showed a reading of 593 x 100 cubic ft. Data logger showed 125/ 0 psi. Production equipment contained 100 bbl unit with 50 bbl fluid and separator (100 psi). Based on site conditions, no indication of IW or E&S issues at the site. Well tag present. No gas leaks around well head and production equipment |