X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-157-22985

Well Details

Well ID: 34-157-22985
Loading map...
Country: United States
State: Ohio
County: Tuscarawas
Municipality: Washington Township
Operator Name: JADCO ENERGY INC
Well Pad ID:
Farm/Lease Name: LEASE HURSEY
License Status: Producing
License Date: 1977-10-05
Spud Date: 1977-10-11
Spud Drilling Contractor:
Final Drill Date: 1977-10-20
Well Total Depth: 5128.00 ft
Configuration: Vertical
Latitude: 40.240000
Longitude: -81.480000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1977-10-11
Completed 1977-10-20
Reached Total Depth 1977-10-20
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4938 5009 13
4938 5009 13
4938 5009 13

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2200 Bbl 70000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 HI SNYDER/SNYDER OIL & GAS INC 3465.00 0.00 0
1987 HI SNYDER/SNYDER OIL & GAS INC 3036.00 0.00 0
1988 HI SNYDER/SNYDER OIL & GAS INC 2705.00 0.00 0
1989 HI SNYDER/SNYDER OIL & GAS INC 1864.00 0.00 0
1990 HI SNYDER/SNYDER OIL & GAS INC 2216.00 0.00 365
1991 HI SNYDER/SNYDER OIL & GAS INC 1580.00 0.00 365
1992 HI SNYDER/SNYDER OIL & GAS INC 1608.00 0.00 365
1993 HI SNYDER/SNYDER OIL & GAS INC 1129.00 25.00 0
1994 HI SNYDER/SNYDER OIL & GAS INC 812.00 0.00 0
1995 HI SNYDER/SNYDER OIL & GAS INC 222.00 0.00 0
1996 HI SNYDER/SNYDER OIL & GAS INC 308.00 0.00 0
1997 HI SNYDER/SNYDER OIL & GAS INC 342.00 11.00 0
1998 HI SNYDER/SNYDER OIL & GAS INC 133.00 0.00 365
1999 HI SNYDER/SNYDER OIL & GAS INC 87.00 0.00 365
2000 HI SNYDER/SNYDER OIL & GAS INC 72.00 0.00 365
2001 HI SNYDER/SNYDER OIL & GAS INC 82.00 0.00 213
2002 HI SNYDER/SNYDER OIL & GAS INC 53.00 86.00 234
2004 HI SNYDER/SNYDER OIL & GAS INC 90.00 0.00 180
2005 HI SNYDER/SNYDER OIL & GAS INC 0.00 0.00 0
2006 HI SNYDER/SNYDER OIL & GAS INC 261.00 0.00 216
2008 HI SNYDER/SNYDER OIL & GAS INC 30.00 0.00 159
2009 HI SNYDER/SNYDER OIL & GAS INC 67.00 78.00 244
2010 HI SNYDER/SNYDER OIL & GAS INC 44.00 0.00 287
2011 HI SNYDER/SNYDER OIL & GAS INC 246.00 0.00 81
2012 HI SNYDER/SNYDER OIL & GAS INC 33.00 0.00 152
2013 HI SNYDER/SNYDER OIL & GAS INC 104.00 0.00 62
2014 HI SNYDER/SNYDER OIL & GAS INC 283.00 0.00 137
2015 HI SNYDER/SNYDER OIL & GAS INC 148.00 0.00 67
2016 HI SNYDER/SNYDER OIL & GAS INC 154.00 0.00 228
2017 HI SNYDER/SNYDER OIL & GAS INC 12.00 0.00 163
2018 HI SNYDER/SNYDER OIL & GAS INC 27.00 0.00 147

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1987 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1988 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1989 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1990 HI SNYDER/SNYDER OIL & GAS INC Brine 0 365
1991 HI SNYDER/SNYDER OIL & GAS INC Brine 0 365
1992 HI SNYDER/SNYDER OIL & GAS INC Brine 0 365
1993 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1994 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1995 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1996 HI SNYDER/SNYDER OIL & GAS INC Brine 0 0
1997 HI SNYDER/SNYDER OIL & GAS INC Brine 0
1998 HI SNYDER/SNYDER OIL & GAS INC Brine 0 365
1999 HI SNYDER/SNYDER OIL & GAS INC Brine 0 365
2000 HI SNYDER/SNYDER OIL & GAS INC Brine 0 365
2001 HI SNYDER/SNYDER OIL & GAS INC Brine 0 213
2002 HI SNYDER/SNYDER OIL & GAS INC Brine 0 234
2004 HI SNYDER/SNYDER OIL & GAS INC Brine 0 180
2005 HI SNYDER/SNYDER OIL & GAS INC Brine 0
2006 HI SNYDER/SNYDER OIL & GAS INC Brine 0 216
2008 HI SNYDER/SNYDER OIL & GAS INC Brine 0 159
2009 HI SNYDER/SNYDER OIL & GAS INC Brine 0 244
2010 HI SNYDER/SNYDER OIL & GAS INC Brine 0 287
2011 HI SNYDER/SNYDER OIL & GAS INC Brine 0 81
2012 HI SNYDER/SNYDER OIL & GAS INC Brine 0 152
2013 HI SNYDER/SNYDER OIL & GAS INC Brine 0 62
2014 HI SNYDER/SNYDER OIL & GAS INC Brine 0 137
2015 HI SNYDER/SNYDER OIL & GAS INC Brine 0 67
2016 HI SNYDER/SNYDER OIL & GAS INC Brine 0 228
2017 HI SNYDER/SNYDER OIL & GAS INC Brine 0 163
2018 HI SNYDER/SNYDER OIL & GAS INC Brine 0 147

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1400269969 2015-12-16 0:00 AM No Violations
-1641300771 2020-4-8 0:00:0 PW No Violations 0.30
0919270074 2014-05-02 Production Wells No Violations On the day of my inspection following up on NOV-1331052107 and complaint id #3631, I witnessed that the well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system and a domestic gas hookup. Production equipment included a 210bbl tank, a concrete brine vault, a vertical separator and a 2 inch meter run with a .5 inch orifice and a chart recorder. Identification was not present and production records are current. Made phone call to Jeremy Caldwell of PAC Drilling, operator of well and I stated that identification needs to be updated to clear the current violation on the well. Jeremy stated it would be up by the end of next week.
0936631306 2014-04-09 Production Wells No Violations On the day of my inspection following up on NOV-1331052107, I witnessed that the well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system and a domestic gas hookup. Production equipment included a 210bbl tank, a concrete brine vault, a vertical separator and a 2 inch meter run with a .5 inch orifice and a chart recorder. Contamination has been cleaned up and with production records current and meet the minimum for 2013. No identification was present.
0998489007 2015-04-22 Production Wells No Violations On the date of inspection I am following up on NOV-1331052107 and complaint #3631. The well is equipped with a gas plunger lift system, 1.5 inch tubing, 4.5 inch casing, and 8.625 inch casing. The tubing valve and one casing valve are in open position. Casing valve is connected to a domestic line. Production equipment includes a 210bbl tank, a concrete brine vault, and a vertical separator. Identification is present on the tank and the well head. Production records are current through 2014 and have met the minimum requirements for 2013 and 2014. The well is now in compliance.
1151756767 2017-08-10 Production Wells No Violations On the day of my inspection I found the well equipped with 8 5/8 inch diameter casing 4 1/2 inch diameter casing, and 1 1/2 inch diameter tubing, operated by a plunger lift system. The production equipment is made up of one 210 bbl. steel tank, one horizontal separator. The production reporting is up to date, and the tank is properly identified. This well provides domestic gas.
1331052107 2012-03-01 Production Wells Violations Noted arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit.
1400269969 2015-12-16 Administrative Inspection No Violations The issues have been resolved and the case is closed
919270074 2014-5-2 0:00:0 PW No Violations 1.50
936631306 2014-4-9 0:00:0 PW No Violations 1.50
998489007 2015-4-22 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1331052107 US-OH-109487 2012-03-06 Well operation causing pollution and contamination
1331052107 US-OH-109488 2012-03-06 Failure to legibly identify well
1331052107 US-OH-109489 2012-03-06 Defective casing, leaking well

For data sources see[9]

References