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Difference between revisions of "34-155-20975"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-155-20975
 
| Well ID: 34-155-20975
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.31511447, -80.82665602 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.31, -80.82 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Trumbull County, Ohio|Trumbull]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[ENERVEST OPERATING L]]
+
| County: [[Trumbull_County,_Ohio|Trumbull]]
 +
|-
 +
| Municipality: [[Champion_Township,_Trumbull_County,_Ohio|Champion Township]]
 +
|-
 +
| Operator Name: [[ENERVEST OPERATING LLC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: THOMAS LEWIS & PATRICIA
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2019-01-08
 
|-
 
|-
 
| Spud Date: 1978-07-17
 
| Spud Date: 1978-07-17
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1978-07-23
 +
|-
 +
| Well Total Depth: 4453.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 41.310000
 +
|-
 +
| Longitude: -80.820000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Original Spud
 +
| 1978-07-17
 +
|  UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
 +
|-
 +
| Completed
 +
| 1978-07-23
 +
|  UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
 +
|-
 +
| Reached Total Depth
 +
| 1978-07-23
 +
|  UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
 +
|-
 +
| CO
 +
| 1981-06-30
 +
| 271  TGX CORP  GeoDate  6/30/81
 +
|-
 +
| CO
 +
| 1994-03-29
 +
| 182  BELDEN & BLAKE CO  GeoDate  6/30/81
 +
|-
 +
| Change of Owner
 +
| 2007-04-27
 +
| Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
 +
|-
 +
| APP
 +
| 2013-03-06
 +
| Proposed Formations:CLINTON, Issued Date:3/6/2013, Expired Date:3/6/2015 12:00:00 PM, Drilling unit acres:74, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Violations: 0
+
| APP
 +
| 2015-08-17
 +
| Proposed Formations:CLINTON, Issued Date:8/17/2015, Expired Date:8/16/2017 12:00:00 PM, Drilling unit acres:74, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Latitude: 41.31511447
+
| APP
 +
| 2019-01-08
 +
| Proposed Formations:CLINTON SAND, Issued Date:1/8/2019, Expired Date:1/7/2021 12:00:00 PM, Drilling unit acres:74, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Longitude: -80.82665602
+
| Record Last Modified
 +
| 2019-04-01
 +
|  UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
 +
|-
 +
| Construction Permit Expires
 +
| 2021-01-07
 +
|  UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | CONDENSATE PRODUCTION DAYS
+
|-
!scope="col" | OIL QUANTITY
+
| 2006-09-11
!scope="col" | OIL PRODUCTION DAYS
+
| style="text-align: right;" | 4245
 +
| style="text-align: right;" | 4343
 +
| style="text-align: right;" | 14
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 13549.0
 
 
|  
 
|  
 +
| style="text-align: right;" | 4245
 +
| style="text-align: right;" | 4343
 +
| style="text-align: right;" | 14
 +
|-
 
|  
 
|  
|  
+
| style="text-align: right;" | 4245
| style="text-align:right;" | 63.0
+
| style="text-align: right;" | 4343
|  
+
| style="text-align: right;" | 14
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 13549.00
 +
| style="text-align: right;" | 63.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 10642.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 187
 +
|-
 +
| 1986
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 8510.00
 +
| style="text-align: right;" | 44.00
 +
| style="text-align: right;" | 210
 +
|-
 +
| 1987
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 14188.00
 +
| style="text-align: right;" | 76.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1988
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 11231.00
 +
| style="text-align: right;" | 60.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1989
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 11681.00
 +
| style="text-align: right;" | 56.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1990
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 10163.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 7877.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[TGX CORP]]
 +
| style="text-align: right;" | 5987.00
 +
| style="text-align: right;" | 57.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[ATLAS ENERGY GROUP INC]]
 +
| style="text-align: right;" | 9481.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 7263.00
 +
| style="text-align: right;" | 34.00
 +
| style="text-align: right;" | 331
 
|-
 
|-
 +
| 1995
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 5419.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 332
 
|-
 
|-
| 1985-0
+
| 1996
| style="text-align:right;" | 10642.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| style="text-align: right;" | 6422.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 279
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 1997
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 8000.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1986-0
+
| 1998
| style="text-align:right;" | 8510.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 1934.00
|
+
| style="text-align: right;" | 41.00
|  
+
| style="text-align: right;" | 144
| style="text-align:right;" | 44.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 3317.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 149
 
|-
 
|-
| 1987-0
+
| 2000
| style="text-align:right;" | 14188.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 4633.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 357
| style="text-align:right;" | 76.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 888.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 17
 
|-
 
|-
| 1988-0
+
| 2002
| style="text-align:right;" | 11231.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 3151.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 60.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 4899.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1989-0
+
| 2004
| style="text-align:right;" | 11681.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 4025.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 267
| style="text-align:right;" | 56.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 3107.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1990-0
+
| 2006
| style="text-align:right;" | 10163.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| style="text-align: right;" | 2430.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2007
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 91
 
|-
 
|-
| 1991-0
+
| 2008
| style="text-align:right;" | 7877.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 91
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2009
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1992-0
+
| 2010
| style="text-align:right;" | 5987.0
+
| [[ENERVEST OPERATING LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 57.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1993-0
+
| 2012
| style="text-align:right;" | 9481.0
+
| [[ENERVEST OPERATING LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1994-0
+
| 2014
| style="text-align:right;" | 7263.0
+
| [[ENERVEST OPERATING LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 34.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 2
 
|-
 
|-
| 1995-0
+
| 2016
| style="text-align:right;" | 5419.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 2
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 +
| 2017
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1996-0
+
| 2018
| style="text-align:right;" | 6422.0
+
| [[ENERVEST OPERATING LLC]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1997-0
+
| 1984
| style="text-align:right;" | 8000.0
+
| [[TGX CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 80
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1985
 +
| [[TGX CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 187
 
|-
 
|-
| 1998-0
+
| 1986
| style="text-align:right;" | 1934.0
+
| [[TGX CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 210
| style="text-align:right;" | 41.0
 
|
 
 
|-
 
|-
 +
| 1987
 +
| [[TGX CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 1988
| style="text-align:right;" | 3317.0
+
| [[TGX CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1989
 +
| [[TGX CORP]]
 +
| Brine
 +
| style="text-align: right;" | 35
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 1990
| style="text-align:right;" | 4633.0
+
| [[TGX CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[TGX CORP]]
 +
| Brine
 +
| style="text-align: right;" | 35
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1992
| style="text-align:right;" | 888.0
+
| [[TGX CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[ATLAS ENERGY GROUP INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 1994
| style="text-align:right;" | 3151.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 17
|
+
| style="text-align: right;" | 331
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 12
 +
| style="text-align: right;" | 332
 
|-
 
|-
| 2003-0
+
| 1996
| style="text-align:right;" | 4899.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 279
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 1998
| style="text-align:right;" | 4025.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 7
|
+
| style="text-align: right;" | 144
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 149
 
|-
 
|-
| 2005-0
+
| 2000
| style="text-align:right;" | 3107.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 357
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 17
 
|-
 
|-
| 2006-0
+
| 2002
| style="text-align:right;" | 2430.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2007-0
+
| 2004
| style="text-align:right;" | 0.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 267
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 32
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2006
| style="text-align:right;" | 0.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 91
 
|-
 
|-
| 2009-0
+
| 2008
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 91
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2010-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 
|-
 
|-
| 2011-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2012-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 2
 
|-
 
|-
| 2013-0
+
| 2016
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 2
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2014-0
+
| 2018
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
| style="text-align:right;" | 0.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
 
| 1367931740
 
| 1367931740
 
| 2013-05-06
 
| 2013-05-06
 +
| UrbanProduction Wells
 +
| Violations Noted
 +
| I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid.  I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower.  He immediately dispatched a well tender to assess the situation and make repairs.  Larry found the 1.5 tubing on the plunger lift unit had a small hole from a gun shot.  Also, a coupling on the flow line had a mark from a gun shot.  The well tender placed a clamp on the tubing to stop the leaking.  On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again.  I called Larry Lower and he dispatched the well tender.  The well tender replaced the clamp with a new full circle clamp until further repairs could be made.  My inspection on 5/6/2013 found the clamp holding.  I noticed a 10 grassy area around the well that had been impacted from the leak.  Enervest had peat sorb and absorbent pads in place.  A Bobcat was dispatched to the location to remove all of the grass and soil impacted.  Approximately 3 to 4 barrels of brine was released.  I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation.  The tank battery contained one, 100 barrel production tank.  The dike was weathered and did not meet containment requirements.  The heat, treated separator was surrounded by debris from the resident.  There was an identification sign posted on the production tank.  The was no lease road to the tank battery.  Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well.  Enervest was issued a plugging permit on 3/6/2013.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1367931740
 +
| US-OH-110847
 +
| 2013-05-07
 
|  
 
|  
| I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid.  I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower.  He immediately dispatched a well tender to assess the situation and make repairs.  Larry found the 1.5 tubing on the plunger lift unit had a small hole from a gun shot.  Also, a coupling on the flow line had a mark from a gun shot.  The well tender placed a clamp on the tubing to stop the leaking.  On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again.  I called Larry Lower and he dispatched the well tender.  The well tender replaced the clamp with a new full circle clamp until further repairs could be made.  My inspection on 5/6/2013 found the clamp holding.  I noticed a 10' grassy area around the well that had been impacted from the leak.  Enervest had peat sorb and absorbent pads in place.  A Bobcat was dispatched to the location to remove all of the grass and soil impacted.  Approximately 3 to 4 barrels of brine was released.  I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation.  The tank battery contained one, 100 barrel production tank.  The dike was weathered and did not meet containment requirements.  The heat, treated separator was surrounded by debris from the resident.  There was an identification sign posted on the production tank.  The was no lease road to the tank battery.  Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well.  Enervest was issued a plugging permit on 3/6/2013.
+
| ACCESS ROAD E(1-5)
|  
+
|-
 +
| 1367931740
 +
| US-OH-110848
 +
| 2013-05-07
 
|  
 
|  
 +
| No SPCC dike/or failure to keep dike free of water or oil
 +
|-
 +
| 1367931740
 +
| US-OH-110849
 +
| 2013-05-07
 
|  
 
|  
 +
| Nonproduction; well shall be plugged or placed in temporary inactive status
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 09:43, 12 January 2021

Well Details

Well ID: 34-155-20975
Loading map...
Country: United States
State: Ohio
County: Trumbull
Municipality: Champion Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: THOMAS LEWIS & PATRICIA
License Status: Producing
License Date: 2019-01-08
Spud Date: 1978-07-17
Spud Drilling Contractor:
Final Drill Date: 1978-07-23
Well Total Depth: 4453.00 ft
Configuration: Vertical
Latitude: 41.310000
Longitude: -80.820000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1978-07-17 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
Completed 1978-07-23 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
Reached Total Depth 1978-07-23 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
CO 1981-06-30 271 TGX CORP GeoDate 6/30/81
CO 1994-03-29 182 BELDEN & BLAKE CO GeoDate 6/30/81
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
APP 2013-03-06 Proposed Formations:CLINTON, Issued Date:3/6/2013, Expired Date:3/6/2015 12:00:00 PM, Drilling unit acres:74, Proposed Well Type:OG, Proposed Well Class:
APP 2015-08-17 Proposed Formations:CLINTON, Issued Date:8/17/2015, Expired Date:8/16/2017 12:00:00 PM, Drilling unit acres:74, Proposed Well Type:OG, Proposed Well Class:
APP 2019-01-08 Proposed Formations:CLINTON SAND, Issued Date:1/8/2019, Expired Date:1/7/2021 12:00:00 PM, Drilling unit acres:74, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2019-04-01 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.
Construction Permit Expires 2021-01-07 UPDATE LOCATION PER DOGRM SURVEYOR 4/1/19 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4245 4343 14
4245 4343 14
4245 4343 14

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TGX CORP 13549.00 63.00 0
1985 TGX CORP 10642.00 0.00 187
1986 TGX CORP 8510.00 44.00 210
1987 TGX CORP 14188.00 76.00 365
1988 TGX CORP 11231.00 60.00 365
1989 TGX CORP 11681.00 56.00 365
1990 TGX CORP 10163.00 0.00 365
1991 TGX CORP 7877.00 0.00 365
1992 TGX CORP 5987.00 57.00 365
1993 ATLAS ENERGY GROUP INC 9481.00 0.00 365
1994 BELDEN & BLAKE CORPORATION 7263.00 34.00 331
1995 BELDEN & BLAKE CORPORATION 5419.00 0.00 332
1996 BELDEN & BLAKE CORPORATION 6422.00 0.00 279
1997 BELDEN & BLAKE CORPORATION 8000.00 0.00 365
1998 BELDEN & BLAKE CORPORATION 1934.00 41.00 144
1999 BELDEN & BLAKE CORPORATION 3317.00 0.00 149
2000 BELDEN & BLAKE CORPORATION 4633.00 0.00 357
2001 BELDEN & BLAKE CORPORATION 888.00 0.00 17
2002 BELDEN & BLAKE CORPORATION 3151.00 0.00 0
2003 BELDEN & BLAKE CORPORATION 4899.00 0.00 0
2004 BELDEN & BLAKE CORPORATION 4025.00 0.00 267
2005 BELDEN & BLAKE CORPORATION 3107.00 0.00 365
2006 BELDEN & BLAKE CORPORATION 2430.00 0.00 365
2007 ENERVEST OPERATING LLC 0.00 0.00 91
2008 ENERVEST OPERATING LLC 0.00 0.00 91
2009 ENERVEST OPERATING LLC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 2
2016 ENERVEST OPERATING LLC 0.00 0.00 2
2017 ENERVEST OPERATING LLC 0.00 0.00 0
2018 ENERVEST OPERATING LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TGX CORP Brine 80 0
1985 TGX CORP Brine 0 187
1986 TGX CORP Brine 0 210
1987 TGX CORP Brine 0 365
1988 TGX CORP Brine 0 365
1989 TGX CORP Brine 35 365
1990 TGX CORP Brine 0 365
1991 TGX CORP Brine 35 365
1992 TGX CORP Brine 0 365
1993 ATLAS ENERGY GROUP INC Brine 0 365
1994 BELDEN & BLAKE CORPORATION Brine 17 331
1995 BELDEN & BLAKE CORPORATION Brine 12 332
1996 BELDEN & BLAKE CORPORATION Brine 0 279
1997 BELDEN & BLAKE CORPORATION Brine 0 365
1998 BELDEN & BLAKE CORPORATION Brine 7 144
1999 BELDEN & BLAKE CORPORATION Brine 0 149
2000 BELDEN & BLAKE CORPORATION Brine 0 357
2001 BELDEN & BLAKE CORPORATION Brine 0 17
2002 BELDEN & BLAKE CORPORATION Brine 0 0
2003 BELDEN & BLAKE CORPORATION Brine 0 0
2004 BELDEN & BLAKE CORPORATION Brine 0 267
2005 BELDEN & BLAKE CORPORATION Brine 32 365
2006 BELDEN & BLAKE CORPORATION Brine 0 365
2007 ENERVEST OPERATING LLC Brine 0 91
2008 ENERVEST OPERATING LLC Brine 0 91
2009 ENERVEST OPERATING LLC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 2
2016 ENERVEST OPERATING LLC Brine 0 2
2017 ENERVEST OPERATING LLC Brine 0 0
2018 ENERVEST OPERATING LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1367931740 2013-05-06 UrbanProduction Wells Violations Noted I received a call on 5/4/2013 at 9:15 pm from ODNR communications (614-799-9538) about a well in Champion that had been shot and was leaking fluid. I found the well belonged to Enervest and called their field supervisor at 216-570-8708, Larry Lower. He immediately dispatched a well tender to assess the situation and make repairs. Larry found the 1.5 tubing on the plunger lift unit had a small hole from a gun shot. Also, a coupling on the flow line had a mark from a gun shot. The well tender placed a clamp on the tubing to stop the leaking. On 5/5/2013, I received a call from Trumbull County 911 that the tubing was leaking again. I called Larry Lower and he dispatched the well tender. The well tender replaced the clamp with a new full circle clamp until further repairs could be made. My inspection on 5/6/2013 found the clamp holding. I noticed a 10 grassy area around the well that had been impacted from the leak. Enervest had peat sorb and absorbent pads in place. A Bobcat was dispatched to the location to remove all of the grass and soil impacted. Approximately 3 to 4 barrels of brine was released. I researched our database and found the well had not produced since 2006 under Belden and Blake Corporation. The tank battery contained one, 100 barrel production tank. The dike was weathered and did not meet containment requirements. The heat, treated separator was surrounded by debris from the resident. There was an identification sign posted on the production tank. The was no lease road to the tank battery. Larry Lower informed me that Enervest was working on contacting the landowner to get access to the tank battery and well. Enervest was issued a plugging permit on 3/6/2013.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1367931740 US-OH-110847 2013-05-07 ACCESS ROAD E(1-5)
1367931740 US-OH-110848 2013-05-07 No SPCC dike/or failure to keep dike free of water or oil
1367931740 US-OH-110849 2013-05-07 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[8]

References