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34-121-23695

Well Details

Well ID: 34-121-23695
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Country: United States
State: Ohio
County: Noble
Municipality: Brookfield Township
Operator Name: GREEN GAS CO
Well Pad ID:
Farm/Lease Name: HEDGE JOHN
License Status: Producing
License Date: 1990-11-26
Spud Date: 1991-10-02
Spud Drilling Contractor: MATTMARK DRILLING
Final Drill Date: 1991-10-05
Well Total Depth: 5470.00 ft
Configuration: Vertical
Latitude: 39.770000
Longitude: -81.650000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1989-09-14 201 GREEN GAS CO GeoDate 9/14/89
Oil and Gas 1989-09-14 Issued Date 9/14/89 Expired Date 9/14/90 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1990-11-26 201 GREEN GAS CO GeoDate 11/26/90
Oil and Gas 1990-11-26 Issued Date 11/26/90 Expired Date 11/26/91 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05470 Proposed Drill Depth 05470
Original Spud 1991-10-01 RI 12-1-90
Completed 1991-10-05 RI 12-1-90
Reached Total Depth 1991-10-05 RI 12-1-90
Construction Permit Expires 1991-11-26 RI 12-1-90
Completion Report Received 1991-12-04 RI 12-1-90
Record Last Modified 2017-02-15 RI 12-1-90

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5209 5286 0
5209 5286 0
2006-09-11 5240 5256 2
5240 5256 2
5209 5286 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 98140 Gal 28000 FRAC W/98,140 GAL WATER AND 28M #

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1992 GREEN GAS CO 32701.00 138.00 365
1993 GREEN GAS CO 45486.00 56.00 365
1994 GREEN GAS CO 21051.00 0.00 365
1995 GREEN GAS CO 19671.00 98.00 365
1996 GREEN GAS CO 12743.00 62.00 365
1997 GREEN GAS CO 9860.00 66.00 365
1998 GREEN GAS CO 7545.00 0.00 365
1999 GREEN GAS CO 8368.00 0.00 365
2000 GREEN GAS CO 7628.00 54.00 365
2001 GREEN GAS CO 7809.00 0.00 365
2002 GREEN GAS CO 6345.00 0.00 365
2003 GREEN GAS CO 1166.00 0.00 365
2004 GREEN GAS CO 5739.00 0.00 365
2005 GREEN GAS CO 5270.00 0.00 365
2006 GREEN GAS CO 4814.00 50.00 365
2007 GREEN GAS CO 3751.00 0.00 365
2008 GREEN GAS CO 1451.00 0.00 365
2009 GREEN GAS CO 4007.00 0.00 365
2010 GREEN GAS CO 2958.00 0.00 365
2011 GREEN GAS CO 2633.00 0.00 0
2012 GREEN GAS CO 0.00 0.00 0
2013 GREEN GAS CO 0.00 0.00 0
2014 GREEN GAS CO 0.00 0.00 0
2016 GREEN GAS CO 0.00 0.00 0
2017 GREEN GAS CO 0.00 0.00 0
2018 GREEN GAS CO 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1992 GREEN GAS CO Brine 540 365
1993 GREEN GAS CO Brine 1295 365
1994 GREEN GAS CO Brine 100 365
1995 GREEN GAS CO Brine 20 365
1996 GREEN GAS CO Brine 30 365
1997 GREEN GAS CO Brine 28 365
1998 GREEN GAS CO Brine 20 365
1999 GREEN GAS CO Brine 0 365
2000 GREEN GAS CO Brine 35 365
2001 GREEN GAS CO Brine 0 365
2002 GREEN GAS CO Brine 24 365
2003 GREEN GAS CO Brine 0 365
2004 GREEN GAS CO Brine 15 365
2005 GREEN GAS CO Brine 0 365
2006 GREEN GAS CO Brine 0 365
2007 GREEN GAS CO Brine 0 365
2008 GREEN GAS CO Brine 0 365
2009 GREEN GAS CO Brine 0 365
2010 GREEN GAS CO Brine 0 365
2011 GREEN GAS CO Brine 0
2012 GREEN GAS CO Brine 0 0
2013 GREEN GAS CO Brine 0 0
2014 GREEN GAS CO Brine 0 0
2016 GREEN GAS CO Brine 0 0
2017 GREEN GAS CO Brine 0 0
2018 GREEN GAS CO Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1036081509 2019-2-28 0:00: PL No Violations 1.00
-258852510 2013-10-29 0:00 PW No Violations 2.00
-347515618 2016-6-15 0:00: PW No Violations 1.00
-434027202 2019-10-7 0:00: PW No Violations 1.00
-833660317 2017-5-9 0:00:0 PW No Violations 1.00
-87810079 2020-8-6 0:00:0 PW No Violations 0.80
-954364698 2017-2-13 0:00: PW No Violations 1.00
0000004865 Preliminary Restoration No Violations PASSED Y WITNESSED 10/20/95 INSPECTOR TED DOBBIN DATE 10/2019/95 DATA FROM OLD VAX INFO
0000004866 Preliminary Restoration No Violations PASSED Y WITNESSED 6/17/93 INSPECTOR TED DOBBIN DATE 06/1719/93 DATA FROM OLD VAX INFO
0149704886 2014-03-13 Production Wells No Violations My inspection today finds the well is equipped with 4.5 casing and 1.5 tubing. There are no production lines attached to the well. All production valves are shut. The tank has been removed. The violation has not been corrected
0258852510 2013-10-29 Production Wells Violations Noted My inspection today finds the well is equipped with 4.5 casing and 1.5 tubing. There are no production lines attached to the well. All production valves are shut. The well reported zero production in 2012. A 210 bbl tank sets approximately 200 from the well, it has no identification or dike. MAKE THE WELL CAPABLE OF PRODUCTION WITHIN 30 DAYS; OR PLUG THE WELL WITHIN 90 DAYS. FAILURE TO COMPLY MAY RESULT IN FORFIETURE OF BOND. SENT BY EMAIL 10/29/2013
0301696323 2018-09-26 Production Wells No Violations Following up on compliance notice -258852510. During my inspection the well was equipped with 13-inch diameter conductor, 8.625-inch diameter surface casing with casing head, 4.5-inch diameter production casing with a tubing head, and 1.5-inch diameter tubing with a tubing valve. All valves were in the closed position, no production lines attached, and there was not any production equipment. Green Gas has submitted reports pf zero production for the years 2012, 2013, 2014, 2016, and 2017. The well was not legibly identified in a conspicuous place on or near the wellhead.
0347515618 2016-06-15 Production Wells No Violations My inspection today finds the well is shut in. The well is disconnected from any pipelines. Additionally, there is no production equipment. Photos were taken.
0710139275 2005-09-28 Production Wells No Violations No violations noted on the day of my inspection,well is equipped with 1-210 bbl tank will need dike work preformed when SPCC rules goes into effect.
0827415849 2015-09-29 Administrative Inspection No Violations At 2:29 pm I received a call from Scott Davis in response to a voice mail I left. Mr. Davis and I discussed the companys plans for the well. Mr. Davis stated that he was going plug the well.
0833660317 2017-05-09 Production Wells No Violations The purpose of my inspection was a status check on compliance notice -258852510. The compliance notice issued to Green Gas Company in 2011 stated that the well was in violation of 1509.062 (A) Nonproduction, 1501:9-9-05 (A) (10) Failure to legibly identify well, and 1501:9-9-05 (A) (9) No SPCC dike/or failure to keep dike free of water or oil. During my inspection the well was equipped with 13 inch diameter conductor, 8.625 inch diameter surface casing with casing head, 4.5 inch diameter production casing with a tubing head, and 1.5 inch diameter tubing with a tubing valve. All valves were in the closed position, no production lines attached, and there is not any production equipment. Since the year 2012 to the year 2014 Green Gas has reported all zeros for production. The well was not legibly identified in a conspicuous place on or near the wellhead. No action has been taken to gain compliance and all of the original violations from the compliance notice -258852510 still exist. Pictures were taken to assist this inspection.
0954364698 2017-02-13 Production Wells No Violations The purpose of my inspection today is a status check on a compliance notice numbered -258852510 that was sent to Green Gas Company. The compliance notice stated that the well is in violation of 1501:9-9-05(10), 1501:9-9-05(9), and 1509.62(A). During my inspection the well was equipped with 8.625 inch diameter surface casing, 4.5 inch diameter production casing, 1.5 inch diameter tubing, and a plunger lift system. The tubing valve is closed and the production valve is closed. There are no production lines attached to the well. The well is idle. There has been no action taken to gain compliance. Pictures were taken to assist this inspection.
1036081509 2019-02-28 Preliminary Restoration No Violations The purpose of my inspection was to follow up on a previously issued compliance notice. On the day of my inspection I witnessed 13-inch diameter conductor, 8.625-inch diameter surface casing, 4.5-inch diameter production casing, with 1.5-inch diameter tubing equipped with a plunger lift system as means of production. At the time of my inspection there all valves were in the closed position, and there was no production equipment on location or attached to the well head. Green gas has reported production as 0 since 2012. There was no identification present and the well appeared to be idle at the time of my inspection. Photographs were taken to assist with the inspection.
1337866399 2012-05-24 Production Wells Violations Noted Inspection of the well head found 8.625 surface casing -4.5 production casing -1.5 tubing with the production valves closed and the production flow lines not hooked up .Inspection of the tank battery found a 210 barrel tank and separator ,Identification present but not legible .Inspector will note found dike with approximately 5 to 7 barrel of oil released into it in which the spill is contained to dike area ,inspected visible valves for possible vandalism by opening of valve and no open valves found and no leakage from burner tube present, tank appears to have rusted out. Measurement of dike 50x 25 Depth of oil in dike 2. At 10:05 am Inspector notified ODNR supervisor and Green Gas company field representative Rusty Walters who indicated they would be responding immediately to begin clean up.
1339214440 2018-01-30 Production Wells No Violations The purpose of my inspection was a status check on compliance notice -258852510. During my inspection the well was equipped with 13 inch diameter conductor, 8.625 inch diameter surface casing with casing head, 4.5 inch diameter production casing with a tubing head, and 1.5 inch diameter tubing with a tubing valve. All valves were in the closed position, no production lines attached, and there was not any production equipment. Green Gas has reported all zeros for production for the years 2012, 2013, 2014, and 2016. The well was not legibly identified in a conspicuous place on or near the wellhead. No action has been taken to gain compliance.
149704886 2014-3-13 0:00: PW No Violations 1.00
1546202658 2015-10-27 Production Wells No Violations My inspection today finds the well is shut in and disconnected from any gas lines. No other production equipment is on site. There is no identification on the wellhead.
1576594534 2019-12-17 0:00 PW No Violations 0.80
1644258443 2014-10-15 Production Wells No Violations My inspection today finds the well is shut in and disconnected from any gas lines. No other production equipment is on site. There is no identification on the wellhead.
1863276743 2020-1-27 0:00: PW No Violations 1.00
2017728973 2019-7-22 0:00: PW No Violations 0.80
2058059030 2019-6-5 0:00:0 PW No Violations 0.80
2096199715 2012-05-29 Production Wells No Violations Inspection of tank battery spill site found spill cleaned up with the equipment removed and the tank battery closed resolving NOV.
301696323 2018-9-26 0:00: PW No Violations 0.50
4865 PL No Violations
4866 PL No Violations
710139275 2005-9-28 0:00: PW No Violations
827415849 2015-9-29 0:00: AM No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0258852510 US-OH-122665 2013-10-29 Failure to legibly identify well
0258852510 US-OH-122666 2013-10-29 No SPCC dike/or failure to keep dike free of water or oil
0258852510 US-OH-122667 2013-10-29 Nonproduction; well shall be plugged or placed in temporary inactive status
1337866399 US-OH-109735 2012-05-24 Well operation causing pollution and contamination

For data sources see[9]

References