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34-067-20991

Well Details

Well ID: 34-067-20991
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Country: United States
State: Ohio
County: Harrison
Municipality: Green Township
Operator Name: COAL GAS TRANSPORTATION LLC
Well Pad ID:
Farm/Lease Name: CAM OHIO
License Status: Producing
License Date: 2005-11-25
Spud Date: 2006-01-23
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC
Final Drill Date: 2006-01-25
Well Total Depth: 495.00 ft
Configuration: Vertical
Latitude: 40.280000
Longitude: -80.950000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-11-25 Proposed Formations:LOWER FREEPORT, Issued Date:11/25/2005, Expired Date:11/25/2006 6:00:00 AM, Drilling unit acres:1, Proposed Well Type:CM, Proposed Well Class:POOL
Original Spud 2006-01-23 RBDMS Rec
Completed 2006-01-25 RBDMS Rec
Reached Total Depth 2006-01-25 RBDMS Rec
Construction Permit Expires 2006-11-25 RBDMS Rec
Completion Report Received 2006-12-22 RBDMS Rec
Change of Owner 2008-12-29 Operator changed from 5319, LAHD ENERGY INC to 8454, COAL GAS TRANSPORTATION LLC
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2006 LAHD ENERGY INC 2750.00 0.00 275
2007 LAHD ENERGY INC 7300.00 0.00 365
2008 LAHD ENERGY INC 4149.00 0.00 334
2009 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2010 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2011 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2012 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2013 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2014 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2015 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2016 COAL GAS TRANSPORTATION LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2006 LAHD ENERGY INC Brine 0 275
2007 LAHD ENERGY INC Brine 0 365
2008 LAHD ENERGY INC Brine 0 334
2009 COAL GAS TRANSPORTATION LLC Brine 0 0
2010 COAL GAS TRANSPORTATION LLC Brine 0 0
2011 COAL GAS TRANSPORTATION LLC Brine 0 0
2012 COAL GAS TRANSPORTATION LLC Brine 0 0
2013 COAL GAS TRANSPORTATION LLC Brine 0 0
2014 COAL GAS TRANSPORTATION LLC Brine 0 0
2015 COAL GAS TRANSPORTATION LLC Brine 0 0
2016 COAL GAS TRANSPORTATION LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1004780231 2006-1-26 0:00: DD No Violations 0.50
-114623322 2020-10-6 0:00: PW No Violations 1.00
-1339267499 2018-3-13 0:00: PL No Violations 1.00
-1797713325 2019-7-15 0:00: PW No Violations 1.00
-2113878256 2020-5-13 0:00: PW No Violations 1.00
-863542039 2020-1-15 0:00: PW No Violations 1.00
-866654491 2006-3-22 0:00: PW No Violations 0.50
0866654491 2006-03-22 Production Wells No Violations Inspection revealed that the drilling pit has been closed ; no violations at this time . No tank lat/long because there is no tank battery associated with this well .
1004780231 2006-01-26 Drill / Deepen / Reopen No Violations Inspection revealed that Monroe Drilling has finished the well and moved off location . Inspection of the drilling pit revealed that the liner is intact and the fluid level is acceptable . No violations at this time .
1126867263 2017-04-26 Production Wells No Violations On the day of my inspection I witnessed the well is equipped with a 7 inch diameter casing. No production equipment on site. Well has proper identification and last shown production was in 2008.
1213914641 2007-10-22 Preliminary Restoration No Violations Inspection revealed that the preliminary restoration can be approved at this time. No violations at this time.
1339267499 2018-03-13 Preliminary Restoration No Violations On the day of my inspection I am performing a follow up to Chiefs Order 2017-414 issued on 10-31-17 for liability insurance. This well is labeled and has not shown production since 2008. Well is shut in.
1621502342 2019-7-15 0:00: PW No Violations 0.40

For data sources see[8]

References