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Well ID: 34-059-20965 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Valley Township | |
Operator Name: BUCKSHOT DISPOSAL LLC | |
Well Pad ID: | |
Farm/Lease Name: SILFKO (SWIW #10) | |
License Status: Active Injection | |
License Date: 2019-10-17 | |
Spud Date: 1969-06-02 | |
Spud Drilling Contractor: PEP DRLG | |
Final Drill Date: 1969-06-13 | |
Well Total Depth: 5315.00 ft | |
Configuration: Vertical | |
Latitude: 39.910000 | |
Longitude: -81.550000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1969-06-02 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
Reached Total Depth | 1969-06-13 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
CO | 1985-10-22 | 70 WALDRON DAVID A & ASS INC GeoDate 10/22/85 |
Unknown | 1985-10-22 | Issued Date 10/22/85 Expired Date 10/22/86 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
CO | 1991-10-01 | 70 WALDRON DAVID A & ASS INC GeoDate 5/29/69 |
Conversion to Injector | 1991-10-02 | |
CO | 1991-10-03 | 2111 BUFFALO OILFIELD SER INC GeoDate 10/3/91 |
Salt Water Injection Well | 1991-10-03 | Issued Date 10/2/91 Expired Date 10/1/92 Acres 0070000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05315 Proposed Drill Depth 05315 |
Storage Well | 1991-10-03 | Issued Date 10/2/91 Expired Date 10/1/92 Acres 0070000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05315 Proposed Drill Depth 05315 |
First Injection | 1991-10-10 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
Completed | 1991-10-15 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
Construction Permit Expires | 1992-10-01 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
Completion Report Received | 1993-04-30 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
CO | 1994-09-30 | 4930 CANTON OIL & GAS COMPANY GeoDate 10/3/91 |
Annulus Pressure Monitoring Approved | 2000-01-03 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
Change of Owner | 2004-07-14 | Operator changed from 4930, CANTON OIL & GAS COMPANY to 7666, ARVILLA OILFIELD SERVICES LLC |
Change of Owner | 2011-03-18 | Operator changed from 7666, ARVILLA OILFIELD SERVICES LLC to 8690, SES ASSETS LLC |
Last Compliance Report | 2013-09-18 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
Change of Owner | 2018-10-19 | Operator changed from 8690, SELECT ENERGY SERVICES LLC to 10176, BUCKSHOT DISPOSAL LLC |
Record Last Modified | 2019-06-11 | CONVERTED FROM OIL & GAS TO SWIW IN 1991 CONVERT 10-5-91 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-04-28 | 5184 | 5254 | 20 |
5184 | 5254 | 20 | |
5184 | 5254 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 3000 Bbl | 85000 | |||
N2 | 0 | 194 Mscf | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1034578143 | 2014-4-1 0:00:0 | SW | No Violations | |
-1040699815 | 2015-10-21 0:00 | SW | No Violations | |
-105893522 | 2012-10-29 0:00 | SW | No Violations | |
-1064332599 | 2010-12-9 0:00: | SW | No Violations | |
-1076473028 | 2013-8-27 0:00: | SW | No Violations | 2.00 |
-1078337851 | 2018-9-14 0:00: | SW | No Violations | |
-1121563572 | 2015-6-10 0:00: | SW | No Violations | |
-1139774210 | 2015-9-17 0:00: | SW | No Violations | |
-1158847936 | 2017-6-28 0:00: | SW | No Violations | |
-1167643332 | 2008-9-3 0:00:0 | SW | No Violations | |
-1193987468 | 2003-10-15 0:00 | SW | No Violations | |
-1216180478 | 2018-1-19 0:00: | SW | No Violations | |
-1255643112 | 2006-1-31 0:00: | SW | No Violations | |
-1305861626 | 2007-6-14 0:00: | SW | No Violations | |
-130594566 | 2003-10-16 0:00 | SW | No Violations | |
-1313919800 | 2015-12-21 0:00 | SW | No Violations | |
-1334237034 | 2013-8-20 0:00: | SW | No Violations | 2.00 |
-1395672544 | 2017-2-10 0:00: | SW | No Violations | |
-1457924880 | 2019-7-12 0:00: | SW | No Violations | |
-1502939168 | 2009-9-25 0:00: | SW | No Violations | |
-1510150487 | 2010-9-9 0:00:0 | SW | No Violations | |
-1510492736 | 2014-4-28 0:00: | SW | No Violations | |
-1540918015 | 2006-7-6 0:00:0 | SW | No Violations | |
-1554039381 | 2013-7-11 0:00: | SW | No Violations | |
-1586554894 | 2011-3-22 0:00: | SW | No Violations | |
-1594202848 | 2009-10-6 0:00: | SW | No Violations | |
-1627679492 | 2014-7-24 0:00: | SW | No Violations | |
-1654037502 | 2013-1-10 0:00: | SW | No Violations | |
-1662937172 | 2013-9-9 0:00:0 | SW | No Violations | |
-1701748376 | 2017-12-26 0:00 | SW | No Violations | |
-1715825287 | 2013-9-3 0:00:0 | SW | No Violations | |
-1807687750 | 2010-7-15 0:00: | SW | No Violations | |
-1809936100 | 2011-4-6 0:00:0 | SW | No Violations | |
-181617605 | 2017-1-11 0:00: | SW | No Violations | |
-1845885987 | 2013-11-25 0:00 | SW | No Violations | |
-1862437650 | 2013-12-11 0:00 | SW | No Violations | |
-1867919123 | 2009-12-28 0:00 | SW | No Violations | |
-2037911599 | 2016-8-19 0:00: | SW | No Violations | |
-2095403358 | 2015-6-24 0:00: | SW | No Violations | |
-21254740 | 2010-5-3 0:00:0 | SW | No Violations | 1.00 |
-22342967 | 2014-6-4 0:00:0 | SW | No Violations | |
-261246990 | 2017-6-13 0:00: | SW | No Violations | |
-288223402 | 2019-9-24 0:00: | SW | No Violations | |
-316360535 | 2013-12-26 0:00 | SW | No Violations | |
-321179266 | 2013-9-19 0:00: | SW | No Violations | |
-402323020 | 2013-10-15 0:00 | SW | No Violations | |
-472772540 | 2017-11-8 0:00: | SW | No Violations | |
-502885024 | 2019-12-16 0:00 | SW | No Violations | |
-549323034 | 2008-12-31 0:00 | SW | No Violations | |
-652271872 | 2017-9-19 0:00: | SW | No Violations | |
-712513414 | 2012-12-5 0:00: | SW | No Violations | |
-833008003 | 2010-1-20 0:00: | SW | No Violations | |
-892591359 | 2008-2-13 0:00: | SW | No Violations | |
-897747644 | 2010-12-29 0:00 | SW | No Violations | |
-944441526 | 2008-7-25 0:00: | SW | No Violations | |
000UIC1813 | 1999-11-24 | Salt Water Injection Well | No Violations | 1501:9-3-07 (H) SUSPEND INJECTION |
001289i495 | 2002-07-05 | Salt Water Injection Well | No Violations | no violations noted this inspection. |
0020480534 | 2002-11-05 | Salt Water Injection Well | No Violations | S.W.I.W. |
0021254740 | 2010-05-03 | Salt Water Injection Well | No Violations | Inspection revealed that well is in operation and not used much.
Note: As suggested on last inspection stone is still needed in tank area. |
0022342967 | 2014-06-04 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that owner has constructed a new building over the current injection pump. |
0066326927 | 2008-06-09 | Salt Water Injection Well | No Violations | SALT WATER INJECTION WELL. NOT BEING OPERATED THIS INSPECTION |
0105893522 | 2012-10-29 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that owner has placed stone over exposed portions of pit liner as requested from previous inspections and new sump pump has been installed in unloading pad vault. |
0130594566 | 2003-10-16 | Salt Water Injection Well | No Violations | SWIW WORKOVER. PIT M.TD. 2 DITCHES TO CHECK DIKE AREA FOR LEAKS CLOSED. AREA MULCHED. NEEDS MORE WORK AS GROUND DRIES 0UT. WELL IS NOT BEING USED AT THIS TIME. NEW TRI-PLEX PUMP BASE IS BEING BUILT, DESIGNED TO CONTAIN ANY WATER LEAKING FROM IT. AREA OF WELL HEAD WILL BE COMPLETELY RESTORED AS WEATHER PERMITS. |
0150991049 | 2013-08-26 | Salt Water Injection Well | No Violations | Service rig still trying to get hole stabilized so they can get well perforated and then run rebuilt Baker Packer in hole. |
0158836312 | 2004-06-07 | Salt Water Injection Well | No Violations | INSPECTED WELL FOUND FLOW LINE LEAK HAD BEEN REPAIRED 2 WEEKS AGO. AREA OF FLOWLINE NEEDS VEGETATION RE-ESTABLISHED ALONG THE LENGTH OF FLOW LINE. SCALD AREA NEEDS LIMED HEAVILY SEEDED, FERTILIZED,MULCHED. PHONE CALL TO JIMMY HAWKINS, INFORMING HIM |
0181617605 | 2017-01-11 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation and it was noted that unloading pad is in need of a good cleaning. |
0208367403 | 2010-03-04 | Salt Water Injection Well | No Violations | Inspection revealed that pump was in operation during my inspection, noted that annulus of tubing has no pressure ,called and discussed with well tender that they would need to get pressure applied to backside of tubing ASAP. |
0223643473 | 2016-09-20 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
0227390659 | 2015-07-09 | Brine Hauler | No Violations | PERFORMED FIELD AUDIT OF BRINE TRUCKS: SELECT ENERGY SERVICES UIC #25-359 ON SITE. LABELED PROPERLY AND APPROVED TO HAUL TO THE SLIFKO #1. NO TRUCK VIOLATIONS FOUND. |
0261246990 | 2017-06-13 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation at the time of my inspection. |
0316360535 | 2013-12-26 | Salt Water Injection Well | No Violations | Inspection revealed that company rep arrived on site during my inspection and started injection and it was noted that one company owned vacuum truck arrived at facility during my inspection. |
0321179266 | 2013-09-19 | Salt Water Injection Well | No Violations | On site along with county inspector Mike Hartshorn to instruct him on proper way to check tubing and annulus pressures on injection well facility. |
0384131479 | 2016-03-16 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was not in operation and it appears that well is not used much at this time. |
0402323020 | 2013-10-15 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection and it was noted that vegetation needs to be established in area of wellhead area was cleared off when well was recently worked over. |
0407567559 | 2017-08-30 | Salt Water Injection Well | No Violations | Well is down due too fact of lack of customers. |
0442530543 | 2016-02-04 | Salt Water Injection Well | No Violations | Well is not in operation at this time. |
0445681157 | 2004-06-28 | Salt Water Injection Well | No Violations | FLOW LINE BEING REPLACED TODAY. FROM INSIDE DIKE TO WELLHEAD. SCALD AREA ON OUTSIDE DIKE, APPROXIMATELY 15 NEEDS RE-VEGETATED TO RE-ESTABLISH VEGETATION. TRIPLEX PUMP ALSO WORKED ON TO CHECK LEAK. |
0453491033 | 2009-04-29 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time,owner is in process of having tanks cleaned out and all of tank plumbing replaced,talked to well tender requesting that they remove all old plumbing from site and perform housekeeping on unloading pad he stated that work will be preformed in the near future also noted that electric motor from injection pump has been removed for repair. |
0472772540 | 2017-11-08 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time. |
0479190046 | 2013-08-12 | Salt Water Injection Well | No Violations | Well not in operation during my inspection, in conversation with company rep stating they are planning on checking total depth with wire line truck this week they suspect perforations are possibly covered up and not allowing fluid to properly enter formation. |
0549323034 | 2008-12-31 | Salt Water Injection Well | No Violations | WELL NOT IN OPERATION. FACILITY GATE LOCKED. FACILITY IS BEING UPKEPT. |
0549926787 | 2016-01-22 | Salt Water Injection Well | No Violations | Inspection revealed that well was not in operation during my inspection. |
0572990617 | 2013-08-19 | Salt Water Injection Well | No Violations | Kilbarger Services moving service rig in on site to work over well. |
0573618851 | 2008-04-14 | Salt Water Injection Well | No Violations | WELL NOT BEING USED AT THIS TIME. GATE LOCKED. PUMP NOT RUNNING |
0630192608 | 2014-01-24 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today due too extreme weather conditions. |
0639984510 | 2010-06-08 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation during my inspection.
Note: Weed eating needs to be preformed at site ASAP,and stone is still needed in tank area |
0652271872 | 2017-09-19 | Salt Water Injection Well | No Violations | Inspection revealed that well is shut in at this time due to lack of customers. |
0663087469 | 2015-07-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was being shut down when I arrived on site due to fact they were nearing maximum pressure allowed and also we measured dike area to determine if they had enough storage area to contain volume of water that is in the tanks and they were short on volume and I requested that they submit plan to bring dike into compliance. |
0712513414 | 2012-12-05 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that owner has been placing stone on exposed portions of liner as requested from previous inspections. |
0739083447 | 2014-05-08 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump has been replaced and owner has constructed a building over the pump and new electrical service has been installed at site. |
0833008003 | 2010-01-20 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today, noted that pit liner in tank area is in need of repair and Stone is needed in tank area and unloading area respectively. |
0884361131 | 2016-10-27 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation and it was noted that area around facility has been recently weedeated. |
0888660432 | 2011-04-08 | Salt Water Injection Well | No Violations | On site to witness injection testing preformed by Producers Services they pumped water and KCL solution into well at 3/10ths bbl per min and we monitored pressures testing began@12.20 P.M and ended@1.54 P.M. company rep John Gaydos will discuss findings with corporate office and decision will be made on what they plan on doing with well. |
0892591359 | 2008-02-13 | Salt Water Injection Well | No Violations | SWIW INSPECTED. MINI TEST PERFORMED 2/12/08. |
0897747644 | 2010-12-29 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today, it appears that well is not used much in cold weather climate.
Note: As weather permits stone is still needed in tank area and unloading pad is in need of a good cleaning. |
0900502503 | 2016-12-21 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was not in operation. |
0944441526 | 2008-07-25 | Salt Water Injection Well | No Violations | SALT WATER INJECTION WELL. WALKWAYS AND STEPS STILL NEED WORKED ON. UNLOADING PAD AND DIKE AREA IN GOOD REPAIR. WELL NOT IN OPERATION AT THIS TIME. |
1004724685 | 2008-05-07 | Salt Water Injection Well | No Violations | WELL IS NOT BEING USED AT THIS TIME. UNLOADING PAD HAS STAINS BUT NO RECENT WATER ON IT. |
1034578143 | 2014-04-01 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that one Select Energy vacuum truck was unloading at facility during my inspection. |
1040699815 | 2015-10-21 | Salt Water Injection Well | No Violations | Inspection revealed that owner still needs to remove two storage tanks at site to become into compliance with SPCC rules there tank capacity exceeds there dike capacity at this time, owner stated that they are making plans on removing tanks in the near future.
Note: One G-R Contracting vacuum truck was unloading at the facility during my inspection(25-271) brine hauler number. |
1051719453 | 2003-04-30 | Salt Water Injection Well | No Violations | SWIW # 10 n.o violations noted this inspection |
1057020655 | 2003-06-30 | Salt Water Injection Well | No Violations | TRIPLEX PUMP LEAKING BADLY. NOTIFIED JIM HAWKINS, SUPERVISOR, ARROW, SENT WATER TRUCK IN TO START SUCKING OUT DIKE AREA,PUTTING WATER BACK IN TANKS INSIDE DIKE.TO MEET HAWKINS ON LOCATION 7/1/03, IN A.M. TO INSTRUCT ON CLEAN UP OF DIKE AREA.WEDS ALSO NEED |
1057152740 | 2003-07-01 | Salt Water Injection Well | No Violations | MET JIM HAWKINS,GIB WEXTLER AT WELL.WATER BEING HAULED OUT TO GO TO RIG IN PA.STARTED TO CHANGE OUT SEATS INTRIPLEX PUMP.DISCUSSED CLEAN UP WITH MR. HAWKINS.TO TAKE GRAVEL OUT OF PAD AND TRUCK FRESH IN.ALSO NOTED NO P/C GOT OUT OF DIKE OR DIKE AREA. |
1057154604 | 2003-07-02 | Salt Water Injection Well | No Violations | CLEAN-UP STILL IN PROGRESS. WATER TRUCK UNLOADING LOAD WATER.INSTRUCTED DRIVER TO MAKE SURE OTHER DRIVERS KEEP UNLOADING PAD AREA RESONABLY CLEAN FROM NOW ON IN. |
1057598810 | 2003-07-07 | Salt Water Injection Well | No Violations | INSIDE OF TANK PAD CLEANED UP. FRESH SCREENINGS PUT DOWN. |
1064332599 | 2010-12-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1065452712 | 2003-10-06 | Salt Water Injection Well | No Violations | ARROW OILFIELD,GIB WEXTLER. PRESSURE TESTED WELL.980# ANNULUS,700# ON TUBING. COULD NOT BRING UP TO TEST PRESSURE 1080#. SHUT IN AT 980#, BLED BACK TO 900# WITHIN 5 MINUTES.SUSPECTED PACJER BECAME UNSEATED.TO SCHEDULE RIG TO MOVE ON AND PULL PACKER.NO DEC |
1065730416 | 2003-10-09 | Salt Water Injection Well | No Violations | ARROW RIG ON HOLE, PULLING PACKER, SET AT 5145. PULLED TUBING TODAY. NOTICED ONE SMALL PINHOLE IN TUBING. DISCUSSED OVER TELEPHONE WITH DENNIS CHASE, ARROW, ABOUT REBUILDING DIKE AREA. TO DISCUSS FURTHER TOMORROW. TO PRESSURE TEST TUBING TOMORROW, RUN PACKER BACK IN HOLE AFTER PRESSURE TESTIG TUBING. |
1065798240 | 2003-10-10 | Salt Water Injection Well | No Violations | PRESSURE TEST TUBING, 1100# PUT ON TUBING.15 JOINTS TESTED 8 FAILED ( HOLES ). RECOMMENDED TO COMPANY, JIMMY HAWKINS , NEW 23/8 TUBING BE BROUGHT IN AND RUN WITH PACKER 10/14/03. MONDAY IS HOLDAY, I COULD NOT BE PRESENT TO WITNESS PACKER BEING SET. |
1066135758 | 2003-10-02 | Salt Water Injection Well | No Violations | NOTIFIED CANTON OIL & GAS THAT WELL HAD LOST MIT AND INJECTION PUMP WAS LEAKING AND NEEDED REPAIR. WELL NEEDED TO BE SHUT DOWN IMMEDIATELY. |
1066237727 | 2003-10-14 | Salt Water Injection Well | No Violations | ARROW OILFIELD RIG. RUN 5145,23/8 PACKER. BAKER-HUGHES LOCKSET. HANG IN HOLE UNTIL 10/15/03. |
1066695794 | 2003-10-20 | Salt Water Injection Well | No Violations | DIRT WORK COMPLETED AT WELL SITE PIT CLOSED, COMPLETE WELL SITE SMOOTHED OUT.TRI-PLEX PUMP RE-BUILT AND IN OPERATION. WELL IS TAKING WATER AT THIS TIME. NOLEAKS NOTED ON PUMP. |
1071078573 | 2013-02-22 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: Told operator that old stained stone in tank area needs to be replaced when time allows and possibly storage tanks need a fresh coat of paint. |
1074019405 | 2004-01-13 | Salt Water Injection Well | No Violations | INSPECTED SWIW,TRIPLEX PUMP STARTING TO LEAK AGAIN,CATCH BOX BENEATH PUMP NOT YET RE-BUILT.ERIC ANDERSON,DRIVER,ARROW OILFIELD UNLOADING ON PAD.CALLED JIM HAWKINS,REORTED LEAK ON PUMP,AND CATCH BOX NOT YET INSTALLED. |
1076473028 | 2013-08-27 | Salt Water Injection Well | No Violations | Kilbarger still trying to stabilize well so they can perforate Clinton section of well, decision was made to cement inside of casing from 5300 back up to 4900 and then drill out cement and then perforate casing again if hole is stabilized. |
1078337851 | 2018-09-14 | Salt Water Injection Well | No Violations | Well is currently shut in waiting on tranfer of well to new owner to be completed. |
1088451404 | 2018-03-14 | Salt Water Injection Well | No Violations | Well is currently not in operation. |
1088597000 | 2005-10-04 | Salt Water Injection Well | No Violations | INSPECTED SWIW. NO VIOLATIONS NOTED THIS INSPECTION. |
1097770196 | 2011-09-19 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today.
Note: Weed eating needed around well head and tank area and unloading pad vault needs to be emptied. |
1104983910 | 2020-3-5 0:00:0 | SW | No Violations | |
1107355903 | 2005-02-02 | Salt Water Injection Well | No Violations | SALT WATER INJECTION WELL. UNLOADING PAD COULD USE HOUSEKEEPING DONE. DIKE AREA APPEARS TO BE IN GOOD SHAPE. |
1112035812 | 2005-03-28 | Salt Water Injection Well | No Violations | INSPECTION REVEALED A SMALL LEAK IN AN OIL STORAGE TANK INSIDE THE DIKE AREA OF THIS FACILITY. PHONE CALL MADE TO JIMMY HAWKINS,SUPERVISOR FOR ARVILLA CORP., NOTIFYING HIM OF LEAK. HE STATED ARVILLA HAS PLANS TO CHANGE OUT TANK WITHIN THE NEXT 2 WEEKS WHICH WILL RECTIFY THE SITUATION. |
1121563572 | 2015-06-10 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and in conversation with operator stating that well is not used much at this time due too near maximum allowable pressure. |
1128447277 | 2005-10-04 | Salt Water Injection Well | No Violations | INSPECTED WELL AND LOAD OUT FACILITY. NO VIOLATIONS NOTED. |
1131871555 | 2012-08-21 | Salt Water Injection Well | No Violations | On site with UIC Director and group from Central Office to inspect well site and surface facility.
Note: Exposed portion of pit liner needs to be covered with stone to help prevent exposure to sunlight liner is showing signs of fatigue and once liner displays loss integrity we may require it to be removed and replaced and leaks on injection pump needs to be addressed. |
1139774210 | 2015-09-17 | Salt Water Injection Well | No Violations | Pump not in operation today and owner is preparing storage area for upgrades being made to dike area. |
1152124091 | 2006-07-05 | Salt Water Injection Well | No Violations | NOTED EXCESSIVE AMOUNT OF FRESH WATER IN UNLOADING PAD AND ALSO INSIDE DIKE AREA. PHONE CALL TO DENNIS CHASE INFORMED HIM OF FINDINGS. HE SAID HE WOULD GET SITUATION TAKEN CARE OF ON 7/6/2006. |
1157375141 | 2018-05-09 | Salt Water Injection Well | No Violations | Inspection revealed that well is currently not being used and it has been recently sold waiting on well transfer to be completed.
Ken Parsons is the new owner of the Select Energy Wells. |
1158847936 | 2017-06-28 | Salt Water Injection Well | No Violations | Injection pump was not in operation during my inspection. |
1167643332 | 2008-09-03 | Salt Water Injection Well | No Violations | WELL NOT BEING USED THIS INSPECTION |
1170389515 | 2014-09-17 | Surface Facility Construction | No Violations | Company rep applied positive pressure to annulus of tubing as requested on my last inspection. |
1184538490 | 2007-07-13 | Salt Water Injection Well | No Violations | WELL BEING INJECTED INTO. CLAYTON DENBOW, DRIVER UNLOADING WATER AT THIS TIME. WEDDS NEED CUT ON DIKE AREA AND AROUND WELLHEAD. FACILITY HAS BEEN PRETTY MUCH IGNORED RECENTLY. HOUSEKEEPING COULD BE A LITTLE BETTER. NO VIOLATIONS, HOWEVER. |
1186493759 | 2007-08-07 | Salt Water Injection Well | No Violations | WEEDS WERE PARTIALLY CUT ON DIKE AREA. WELL IS UP AND RUNNING. NEEDS MORE HOUSEKEEPNG AROUND TANK SITE. |
1193987468 | 2003-10-15 | Salt Water Injection Well | No Violations | ARROW OILFIELD RIG SET PACKER AT 5129. PRESSURE TESTED AT 1100# FOR 15 MINUTES. 1000 GAL. ACID 28% I.C. 5GAL. RUST INHIBITOR. PSC.DID THE PRESSURE TEST AND ACIDIZING. |
1209463802 | 2004-06-29 | Salt Water Injection Well | No Violations | CHECK INJ. PRESSURE, 1050#, ANNULUS 90# |
1216180478 | 2018-01-19 | Salt Water Injection Well | No Violations | Well is not in operation at this time current owner is trying to sell well. |
1216814641 | 2006-04-06 | Salt Water Injection Well | No Violations | INSIDE AREA OF DIKE NEEDS CLEANED UP BADLY, WATER LYING INSIDE AREA OF DIKE NEEDS PUMPED OUT AND CLEANED OUT. UNLOADING PAD NEEDS HOUSEKEEPING PERFORMED ALSO. CALLED DENNIS CHASE AND INFORMED HIM AS TO INSPECTION FINDINGS. WELL NOT IN OPERATION AT THIS TI |
1248723707 | 2011-05-19 | Salt Water Injection Well | No Violations | On site with Tom Tomastik to inspect well site.
Note: Unloading pad needs to be cleaned and vault drained it was standing full of fresh water on the day we inspected well. |
1250633914 | 2009-08-17 | Salt Water Injection Well | No Violations | Inspection revealed that well was not in operation during my inspection, called well tender and discussed placing belt guard back onto pump, told him that it was a safety hazard and guard needed to be in place, well does not appear to be used much noted that owner has had plumbing replaced on tanks and weed eating has been preformed around wellhead. |
1255643112 | 2006-01-31 | Salt Water Injection Well | No Violations | WELL NOT IN OPERATION. PUMP NOT RUNNING |
1270676679 | 2010-04-07 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today.
Note: Stone is needed in tank area and unloading area to help minimize tracking mud out onto township road. |
1281128240 | 2010-08-05 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection, noted that unloading pad vault was in need of a good cleaning and also stone is still needed in tank area. |
1289i21257 | 2002-03-27 | Annular Disposal | No Violations | A.D. WELL |
1289i21257267 | 2002-3-27 0:00: | AD | No Violations | |
1289i22053 | 2001-05-16 | Salt Water Injection Well | No Violations | |
1289i22053805 | 2001-5-16 0:00: | SW | No Violations | |
1289i495 | 2002-7-5 0:00:0 | SW | No Violations | |
1305861626 | 2007-06-14 | Salt Water Injection Well | No Violations | WELL SHUT DOWN. INLECTION PRESSURE ELEVATED TRYING TO DROP PRESSUR INJECTION ZONE. |
1312966793 | 2011-08-09 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today, unloading pad is in need of a good cleaning and weed eating around dike area needs to be preformed. |
1313919800 | 2015-12-21 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1330985877 | 2012-03-05 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today as weather permits clean up in tank area needed and also stone needs to be applied to exposed liner to protect it from decay. |
1334237034 | 2013-08-20 | Salt Water Injection Well | No Violations | Kilbarger Services on site to pull packer and work over well, they released packer and were in process of pulling tubing and packer I told company rep to make sure and secure well head before they go home for the night. |
1340748592 | 2012-06-25 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that weed eating has been performed around site since my last inspection.
Note: Plungers on pump is in need of repair and catch pan needs to be constructed under injection pump too avoid contamination to soil. |
1349817042 | 2012-10-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: Stone has been delivered to site to cover exposed portions of liner and place remaining stone in tank area. Also brush along lease road to well head needs to be trimmed back so inspector can drive to wellhead!!!!. |
1364933295 | 2013-04-01 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was also noted that owner has placed stone in dike area as requested from previous inspections. |
1376671521 | 2013-08-15 | Salt Water Injection Well | No Violations | On site to witness Schlumberger Wireline truck run tools into well to check for fillup within casing they sat down@5191 which indicates they have 7 of injection zone open they have service rig coming 8/19/13 to release packer and then clean out casing to cement shoe@5309. |
1377122842 | 2013-08-21 | Salt Water Injection Well | No Violations | Kilbarger Services cleaning out inside of casing they made 30 today they will resume operations again tomorrow. |
1377261233 | 2013-08-23 | Salt Water Injection Well | No Violations | On site to witness APPLACHIAN Well Services attempt to perforate Clinton sand they ran into obstruction@5217 so decision was made to run tubing and bit back into well and make a clean out run we will attempt to perforate tomorrow and then run packer and tubing into well. |
1377539801 | 2014-11-04 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1377727972 | 2013-08-28 | Salt Water Injection Well | No Violations | On site to witness squeeze job of suspected rotted casing Formation Cementing pumped 25 sacks of Class A cement and rig crew pulled tubing above 5000 and then they pressured up on casing forcing cement into suspected faulty casing zone.
Note: Rig crew will confirm cement top tomorrow. |
1378408619 | 2013-09-05 | Salt Water Injection Well | No Violations | On site to witness running of Baker Set Lok A-3 packer and 2.375 tubing into well and flush annulus and pump inhibitor and if all goes well they will pump 1000 gallon of 15% acid into formation and let soak overnite then resume injection operation tomorrow . |
1378494563 | 2013-09-06 | Salt Water Injection Well | No Violations | On site to retest pressure on annulus of tubing after moving packer up hole one joint setting depth of packer is 5107 and top perforation in casing is5180 and calculated cement top on backside of 4.5 is 4326 they pressured up to 1220 and we monitored pressure for 15 minutes with a 15# decline in pressure once test was completed we bleed pressure down to 500# and they began to plumb well back up to go into operation. |
1379610160 | 2013-09-19 | Salt Water Injection Well | No Violations | On the day of my inspection, I checked the injection pressure it was 1180 and the annulas was 120 psi, the injuction pump was running. |
1385152143 | 2018-06-25 | Salt Water Injection Well | No Violations | Well not in operation at this time waiting on well to transfer to new owner. |
1395672544 | 2017-02-10 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation at the time of my inspection and it was noted that unloading pad area is in the need of a good cleaning and unloading pad vault is in need of a good cleaning also it has several inches of build up in it. |
1407165465 | 2014-07-31 | Salt Water Injection Well | No Violations | Injection pump not in operation today and it was noted that one company owned vacuum truck was unloading at facility during my inspection. |
1410562460 | 2014-09-10 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that unloading pad has been cleaned since my last inspection. |
1431206069 | 2015-05-08 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that one company owned vacuum truck was unloading at the facility during my inspection. |
1432378480 | 2015-05-18 | Salt Water Injection Well | No Violations | On site to witness acid treatment job performed by Producers Services they pumped 1500 gallon of 28% acid and then proceeded to pressure test annulus of tubing they pressured up too 1300 psi and we monitored pressure for 15 min with no decline in pressure after test was complete they bled pressure down to 770 psi and we left site. |
1443391681 | 2015-09-23 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection, inquired with operator when they plan on making upgrades to existing dike area he stated that they plan on starting on it within the next couple of weeks. |
1452281324 | 2016-01-06 | Annular Disposal | No Violations | Injection pump was not in operation during my inspection and in conversation with well attendant stating that they have not taken in any water within the last couple of days. |
1478717368 | 2016-11-08 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was in operation.
Note: Plastic storage tank within dike area is showing signs of fatigue it will need to be replaced in the near future. |
1480444995 | 2016-11-29 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pump was not in operation and well tender was working on sump pump in area of the unloading pad. |
1498439554 | 2017-02-07 | Salt Water Injection Well | No Violations | Injection pump not in operation during my inspection and it was noted that vault storage tank is in need of replacement. |
1502939168 | 2009-09-25 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time,belt guard on injection pump still needs to be put back in place before operating pump for safety reasons. |
1504734404 | 2017-09-06 | Salt Water Injection Well | No Violations | Well is not in operation at this time due to lack of customers. |
150991049 | 2013-8-26 0:00: | SW | No Violations | 2.00 |
1510150487 | 2010-09-09 | Salt Water Injection Well | No Violations | Inspection revealed that pump was in operation today, noted that unloading pad is in the need of a good cleaning and weed eating is needed in dike area and stone is also needed in tank area. |
1510492736 | 2014-04-28 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump has been replaced and owner is waiting on electrical work to be performed and once that is completed they will place well back into operation. |
1517546904 | 2013-07-17 | Salt Water Injection Well | No Violations | On site along with company rep Jonathan Mika to perform pressure testing of annulus of tubing he hooked up pressure washer and placed 1200 psi on backside of tubing and we monitored pressure for 15 minutes with no decline in pressure.
Note: Test passed. |
1518804995 | 2018-02-16 | Salt Water Injection Well | No Violations | Inspection today revealed that contractor Ken Parsons was on site installing new sump pump in unloading pad area and pumping water within tank area back into storage tanks in preparation to be pumped down hole the next time they run injection pump. |
1523036512 | 2018-04-06 | Salt Water Injection Well | No Violations | Inspection revealed that well is currently not in operation at this time. |
1524244870 | 2018-04-20 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation and it appears that well is not being used at this time. |
1525459717 | 2018-05-02 | Salt Water Injection Well | No Violations | Inspected site along with potential buyer of Select Energy wells Ken Parsons he plans on closing on purchase next Monday. |
1526111305 | 2020-7-31 0:00: | SW | No Violations | |
1529142405 | 2018-06-12 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time.
New owner is waiting on well transfer to be completed. |
1540918015 | 2006-07-06 | Salt Water Injection Well | No Violations | FOLLOW UP ON PHONE CALL. DIKE DRAINED AND UNLOADING PAD. WEEDS BEING CUT ON DIKE AREA. |
1550002851 | 2019-02-12 | Salt Water Injection Well | No Violations | Well is currently not in operation, waiting on owner to apply for plugging permit. |
1554039381 | 2013-07-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation today and it was noted that injection pressure was at maximum level and I called company rep to discuss possible acid job being preformed on said well in the near future. |
1555698998 | 2019-04-16 | Salt Water Injection Well | No Violations | Waiting on owner to get plugging permit applied for, currently well is not in operation.
Had meeting with owner to talk over plugging operation when they get permit and service rig under contract to plug said well. |
1584797834 | 2020-3-19 0:00: | SW | No Violations | |
1586554894 | 2011-03-22 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was operating during my inspection.
Note 1/4 needle valve on tubing side of wellhead needs to be replaced and I.D. at facility needs to be changed to Select Energy not Arvilla. |
158836312 | 2004-6-7 0:00:0 | SW | No Violations | |
1594202848 | 2009-10-06 | Salt Water Injection Well | No Violations | Inspection revealed that well is not in operation at this time,talked to well tender and he stated as soon as they get belt guard back onto pump they would start disposing of brine. |
1598955313 | 2018-12-05 | Salt Water Injection Well | No Violations | Meeting with well owner Ken Parsons to discuss requirements for plugging of said well.
|
1606763350 | 2014-12-12 | Salt Water Injection Well | No Violations | Injection pump was not in operation during my inspection and it was noted that annulus pressure has fallen to zero and I called company rep and requested that they have positive pressure applied to annulus of tubing and they stated that it would be done on 12/15/2014. |
1627679492 | 2014-07-24 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and in conversation with Johnathon Mika well attendant stating that pump shut off at 0600 and they have four loads of brine coming to wellsite today. |
1639088421 | 2013-01-18 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
1648228796 | 2016-06-07 | Salt Water Injection Well | No Violations | Injection pump not in operation during my inspection. |
1654037502 | 2013-01-10 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it was noted that stone has been placed over exposed portions of liner to help prevent rotting due to exposure to sunlight. |
1662937172 | 2013-09-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today. |
1663718580 | 2008-07-08 | Salt Water Injection Well | No Violations | GATE LOCKED. NO RECENT ACTIVITY. STEPS AND WALKWAY COULD USE SOME REPAIR(WELDING). WEEDS RECENTLY TRIMMED. FACILITY APPEARS TO BE IN GOOD REPAIR. NOTE: WALKWAY AND STEPS LEADING UP TO WALKWAY ARE DEFINITELY A SAFTEY CONCERNE TO EVERY ONE USING THEM AND NEED TO BE REPAIRED IMMEDIATELY. |
1673430752 | 2017-06-22 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation upon my arrival on site informed operator Jonathan Mika to cease operations due to Chiefs order issued for no insurance on wells he turned off injection pump and called his supervisor Jordan Monroe and informed him of my request after contacting Central office it was discovered that insurnce policy has ben received and I called them later in the day and told them they could resume operations at the site. |
1701748376 | 2017-12-26 | Salt Water Injection Well | No Violations | Inspection today indicated that well is currently down and shut in due to lack of water and owner is trying to sell the two wells they have here in Ohio. |
1709839148 | 2003-10-08 | Salt Water Injection Well | No Violations | MOVE RIG ON, RIG UP. DIG PIT. DUG (2) two ditches ACROSS AREA ABOVE SCALD AREA. DOWN TO 6 FEET.COULD NOT FIND WHERE WATER WAS GETTING OUT OF INSIDE OF DIKE. |
1715825287 | 2013-09-03 | Salt Water Injection Well | No Violations | Service rig on site drilling out cement from within casing they drilled to 5300 and circulated hole clean and pulled string above 5100 and shut down for the evening they will attempt to go back to bottom in the morning to check and see if recent squeeze job did any good or not. |
1749206028 | 2020-8-14 0:00: | SW | No Violations | |
1807687750 | 2010-07-15 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today,area around wellhead has been recently weedeated but tank area still needs to be done and stone is also needed in tank area. |
1807805594 | 2020-7-9 0:00:0 | SW | No Violations | |
1809936100 | 2011-04-06 | Salt Water Injection Well | No Violations | Met with company reps to discuss upcoming flow testing of well ,they propose to pump fresh water into formation and check flow rate and not to exceed maximum injection pressure. |
1845885987 | 2013-11-25 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today. |
1851334015 | 2010-10-12 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection.
Note: Stone is still needed in tank area and when well tranfer to Select becomes final new I.D. will need to be posted. |
1862437650 | 2013-12-11 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today and it was noted that four company owned vacuum trucks were waiting to unload at facility. |
1866577085 | 2013-05-09 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection but it was noted that a Myers truck was getting ready to enter facility when my inspection was completed. |
1867919123 | 2009-12-28 | Salt Water Injection Well | No Violations | Inspection revealed that well was not in operation during my inspection.
Note: Stone is needed on driveway to unloading pad it will help cut down on tracking mud onto township road. |
1895219471 | 2012-04-13 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today facility appears to be in satisfactory condition.
Note: Liner on north side of dike needs to be covered with stone to prevent liner from deterioration. |
1982441621 | 2009-11-04 | Salt Water Injection Well | No Violations | Inspection revealed that pump was not in operation today,noted that belt guard on pump has been placed back on since my last inspection.
Housekeeping needed in tank area. |
2037911599 | 2016-08-19 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection. |
20480534 | 2002-11-5 0:00: | SW | No Violations | |
208367403 | 2010-3-4 0:00:0 | SW | No Violations | 1.00 |
2087953572 | 2011-06-20 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation today, unloading pad vault still needs to be emptied and exposed liner in dike area still needs to be covered with stone/dirt, it was noted that 1/2 tank is still on site awaiting on service rig to perform testing on said well. |
2095403358 | 2015-06-24 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was not in operation during my inspection and it appears that well is not being used much at this time. |
2131657373 | 2003-10-14 | Salt Water Injection Well | No Violations | Watch proceedings of recompleting SWIW to pass pressure test. Today ran in new 2 3/8 casing with Baker A-3 Lockset packer to @5100 with pup joint totaling 61 of length. Perfs at 5184-5254 and want to set packer in 100 feet of zone above packer. Will set pipe tomorrow |
2135186397 | 2017-04-12 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pump was not in operation and it was noted that housekeeping is needed in unloading pad area. |
223643473 | 2016-9-20 0:00: | SW | No Violations | |
227390659 | 2015-7-9 0:00:0 | BH | No Violations | |
384131479 | 2016-3-16 0:00: | SW | No Violations | |
407567559 | 2017-8-30 0:00: | SW | No Violations | |
442530543 | 2016-2-4 0:00:0 | SW | No Violations | |
445681157 | 2004-6-28 0:00: | SW | No Violations | |
453491033 | 2009-4-29 0:00: | SW | No Violations | |
479190046 | 2013-8-12 0:00: | SW | No Violations | |
549926787 | 2016-1-22 0:00: | SW | No Violations | |
572990617 | 2013-8-19 0:00: | SW | No Violations | 1.00 |
573618851 | 2008-4-14 0:00: | SW | No Violations | |
630192608 | 2014-1-24 0:00: | SW | No Violations | |
639984510 | 2010-6-8 0:00:0 | SW | No Violations | |
663087469 | 2015-7-14 0:00: | SW | No Violations | |
66326927 | 2008-6-9 0:00:0 | SW | No Violations | |
739083447 | 2014-5-8 0:00:0 | SW | No Violations | |
794572908 | 2020-8-21 0:00: | PB | No Violations | |
884361131 | 2016-10-27 0:00 | SW | No Violations | |
888660432 | 2011-4-8 0:00:0 | SW | No Violations | |
900502503 | 2016-12-21 0:00 | SW | No Violations | |
UIC1813 | 1999-11-24 0:00 | SW | No Violations |
For data sources see[5]