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Well ID: 34-011-20104 | Loading map...
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Country: United States | |
State: Ohio | |
County: Auglaize | |
Municipality: Goshen Township | |
Operator Name: MYERS TOM F | |
Well Pad ID: | |
Farm/Lease Name: MYERS TOM | |
License Status: Producing | |
License Date: 2016-08-17 | |
Spud Date: 2016-08-30 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 2017-03-29 | |
Well Total Depth: 1430.00 ft | |
Configuration: Vertical | |
Latitude: 40.540000 | |
Longitude: -83.900000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2016-08-17 | Proposed Formations:TRENTON, Issued Date:8/17/2016, Expired Date:8/17/2018 12:00:00 PM, Drilling unit acres:36, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2017-03-29 | UPDATED STATUS TO PR-PRODUCTION DATE OMITTED FROM FORM 8, UPDATED INFORMATION PER JOHN WILLIAMS. ALE |
Completion Report Received | 2017-05-25 | UPDATED STATUS TO PR-PRODUCTION DATE OMITTED FROM FORM 8, UPDATED INFORMATION PER JOHN WILLIAMS. ALE |
Record Last Modified | 2018-04-06 | UPDATED STATUS TO PR-PRODUCTION DATE OMITTED FROM FORM 8, UPDATED INFORMATION PER JOHN WILLIAMS. ALE |
Construction Permit Expires | 2018-08-17 | UPDATED STATUS TO PR-PRODUCTION DATE OMITTED FROM FORM 8, UPDATED INFORMATION PER JOHN WILLIAMS. ALE |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | MYERS TOM F | 11.00 | 4.00 | 365 |
2018 | MYERS TOM F | 7.00 | 4.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | MYERS TOM F | Brine | 3 | 365 |
2018 | MYERS TOM F | Brine | 3 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1347548228 | 2017-2-4 0:00:0 | DD | No Violations | |
-1706167485 | 2018-1-2 0:00:0 | PW | No Violations | |
-1840262768 | 2017-6-28 0:00: | PB | No Violations | |
-2094860275 | 2017-2-6 0:00:0 | DD | No Violations | |
-333114772 | 2017-1-13 0:00: | DD | No Violations | |
0183898615 | 2017-01-11 | Drill / Deepen / Reopen | No Violations | Inspected well after cementing the surface casing. Wiper plug was spotted at a depth of 120 feet inside the surface casing. Cement on the annulus of the surface casing did not make it to the surface. Operator will try to install cement to surface on annulus of surface casing. |
0333114772 | 2017-01-13 | Drill / Deepen / Reopen | No Violations | Checked status of cementing process on surface casing. Drilling operator has installed an additional 50 sacks of cement to annulus of surface casing and cement has not made it to the surface. |
0999450366 | 2016-09-09 | Drill / Deepen / Reopen | No Violations | Tom Myers is currently on site drilling with a cable tool rig. A pit has been installed and currently has a liner with a limited amount of water in pit. Drilling activity is currently involving the installation of the 10.75 inch drive pipe.. |
1347548228 | 2017-02-04 | Drill / Deepen / Reopen | No Violations | Jet Waterline on site to complete a cement bond log on this well. Observed the process of the bond log. Cement bond log was completed and the results allowed the operator to continue the operation of drilling this well. |
1489366625 | 2017-03-03 | Drill / Deepen / Reopen | No Violations | Inspected site after well has been completed to a depth of 1430 feet. |
1489675417 | 2017-03-16 | Preliminary Restoration | No Violations | Well has been completed at a depth of 1430 feet deep. Surface casing currently has a seven inch reducer to two inch installed with 2 closed manual valves. Operator will determine at a later date what kind of stimulation is required if any. Pit is still open and will be emptied and closed at a later date. |
1508645262 | 2017-01-10 | Casing String Witnessed | No Violations | Witnessed the installation of cement for the surface casing program. Cement did not circulate to surface and did not appear to install enough water for displacement purposes. |
1527152841 | 2016-12-29 | Drill / Deepen / Reopen | No Violations | Inspected area and also pits and drilling equipment. Drilling permit is on site and drilling operator has obtained a depth of approximately 300 deep. |
1601355482 | 2017-05-16 | Preliminary Restoration | No Violations | Preliminary restoration has been completed. Pits have been filled and drilling equipment has been removed from site. Operator is currently testing well with pump jack and temporary storage tank. |
1706167485 | 2018-01-02 | Production Wells | No Violations | Pump jack is installed at well but no storage tanks are attached to wellhead. Well is currently producing natural gas only. |
183898615 | 2017-1-11 0:00: | DD | No Violations | |
1840262768 | 2017-06-28 | Plug / Plug Back | No Violations | Drilling equipment has been removed from site. Drilling pits have been filled and planted to corn. Pump jack has been installed on well and 5 horsepower gasoline engine is installed to power pump jack Temporary storage equipment has been installed on site to test well. Preliminary restoration has been approved. |
1997371349 | 2017-02-17 | Drill / Deepen / Reopen | No Violations | Checked drilling site for compliance issues and no violations observed at the present time. Depth of well is currently at 1145 feet. |
2094860275 | 2017-02-06 | Drill / Deepen / Reopen | No Violations | Picked up the completed cement bond log and driller is at a depth of approximately 545 deep. |
999450366 | 2016-9-9 0:00:0 | DD | No Violations |
For data sources see[7]