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34-005-20218

Well Details

Well ID: 34-005-20218
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Country: United States
State: Ohio
County: Ashland
Municipality: Mohican Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: METCALF H
License Status: Producing
License Date:
Spud Date: 1943-09-21
Spud Drilling Contractor:
Final Drill Date: 1943-10-28
Well Total Depth: 3010.00 ft
Configuration: Vertical
Latitude: 40.760000
Longitude: -82.180000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1943-09-21 QUAD=WEST SALEM, GL=P-1161.6
Completed 1943-10-28 QUAD=WEST SALEM, GL=P-1161.6
Reached Total Depth 1943-10-28 QUAD=WEST SALEM, GL=P-1161.6
CO 1991-02-22 2936 COLUMBIA NATURAL RES INC
Change of Owner 2005-02-04 Operator changed from 2936, COLUMBIA NATURAL RES INC to 7774, AMERICAN OIL & GAS LLC
Change of Owner 2007-01-25 Operator changed from 7774, AMERICAN OIL & GAS LLC to 8154, AB RESOURCES OH LLC
Change of Owner 2010-09-21 Operator changed from 8154, AB RESOURCES OH LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2019-06-04 QUAD=WEST SALEM, GL=P-1161.6

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 COLUMBIA GAS TRANSMISSION LLC 1601.00 0.00 0
1985 COLUMBIA GAS TRANSMISSION LLC 2114.00 0.00 361
1986 COLUMBIA GAS TRANSMISSION LLC 2012.00 0.00 361
1987 COLUMBIA GAS TRANSMISSION LLC 1981.00 0.00 363
1988 COLUMBIA GAS TRANSMISSION LLC 2265.00 0.00 363
1989 CHESAPEAKE APPALACHIA LLC 1983.00 0.00 365
1990 CHESAPEAKE APPALACHIA LLC 1956.00 0.00 365
1991 CHESAPEAKE APPALACHIA LLC 1664.00 0.00 365
1992 CHESAPEAKE APPALACHIA LLC 1477.00 0.00 365
1993 CHESAPEAKE APPALACHIA LLC 1481.00 0.00 365
1994 CHESAPEAKE APPALACHIA LLC 1290.00 0.00 363
1995 CHESAPEAKE APPALACHIA LLC 1146.00 0.00 365
1996 CHESAPEAKE APPALACHIA LLC 809.00 0.00 366
1997 CHESAPEAKE APPALACHIA LLC 573.00 0.00 601
1998 CHESAPEAKE APPALACHIA LLC 417.00 0.00 341
1999 CHESAPEAKE APPALACHIA LLC 388.00 0.00 365
2000 CHESAPEAKE APPALACHIA LLC 458.00 0.00 364
2001 CHESAPEAKE APPALACHIA LLC 481.00 0.00 364
2002 CHESAPEAKE APPALACHIA LLC 512.00 0.00 368
2003 CHESAPEAKE APPALACHIA LLC 543.00 0.00 364
2004 CHESAPEAKE APPALACHIA LLC 578.00 0.00 366
2005 AMERICAN OIL & GAS LLC 457.00 0.00 334
2006 AMERICAN OIL & GAS LLC 436.00 0.00 365
2007 AB RESOURCES OH LLC 0.00 0.00 0
2008 AB RESOURCES OH LLC 162.00 0.00 365
2009 AB RESOURCES OH LLC 356.00 0.00 365
2010 AB RESOURCES OH LLC 272.00 0.00 365
2011 M & R INVESTMENTS OHIO LLC 1258.00 0.00 365
2012 M & R INVESTMENTS OHIO LLC 988.00 0.00 366
2013 M & R INVESTMENTS OHIO LLC 925.00 0.00 365
2014 M & R INVESTMENTS OHIO LLC 489.00 0.00 365
2015 M & R INVESTMENTS OHIO LLC 774.00 0.00 365
2016 M & R INVESTMENTS OHIO LLC 744.00 0.00 365
2017 M & R INVESTMENTS OHIO LLC 588.00 0.00 365
2018 M & R INVESTMENTS OHIO LLC 460.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
1985 COLUMBIA GAS TRANSMISSION LLC Brine 0 361
1986 COLUMBIA GAS TRANSMISSION LLC Brine 0 361
1987 COLUMBIA GAS TRANSMISSION LLC Brine 0 363
1988 COLUMBIA GAS TRANSMISSION LLC Brine 0 363
1989 CHESAPEAKE APPALACHIA LLC Brine 0 365
1990 CHESAPEAKE APPALACHIA LLC Brine 0 365
1991 CHESAPEAKE APPALACHIA LLC Brine 0 365
1992 CHESAPEAKE APPALACHIA LLC Brine 0 365
1993 CHESAPEAKE APPALACHIA LLC Brine 0 365
1994 CHESAPEAKE APPALACHIA LLC Brine 0 363
1995 CHESAPEAKE APPALACHIA LLC Brine 0 365
1996 CHESAPEAKE APPALACHIA LLC Brine 1 366
1997 CHESAPEAKE APPALACHIA LLC Brine 0 601
1998 CHESAPEAKE APPALACHIA LLC Brine 1 341
1999 CHESAPEAKE APPALACHIA LLC Brine 0 365
2000 CHESAPEAKE APPALACHIA LLC Brine 0 364
2001 CHESAPEAKE APPALACHIA LLC Brine 0 364
2002 CHESAPEAKE APPALACHIA LLC Brine 2 368
2003 CHESAPEAKE APPALACHIA LLC Brine 0 364
2004 CHESAPEAKE APPALACHIA LLC Brine 0 366
2005 CHESAPEAKE APPALACHIA LLC Brine 0 59
2006 AMERICAN OIL & GAS LLC Brine 0 365
2007 AB RESOURCES OH LLC Brine 0 0
2008 AB RESOURCES OH LLC Brine 0 365
2009 AB RESOURCES OH LLC Brine 0 365
2010 AB RESOURCES OH LLC Brine 0 365
2011 M & R INVESTMENTS OHIO LLC Brine 0 365
2012 M & R INVESTMENTS OHIO LLC Brine 0 366
2013 M & R INVESTMENTS OHIO LLC Brine 0 365
2014 M & R INVESTMENTS OHIO LLC Brine 0 365
2015 M & R INVESTMENTS OHIO LLC Brine 0 365
2016 M & R INVESTMENTS OHIO LLC Brine 0 365
2017 M & R INVESTMENTS OHIO LLC Brine 0 365
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-127965043 2018-2-20 0:00: PW No Violations
-698216806 2013-5-30 0:00: PW No Violations
0127965043 2018-02-20 Production Wells No Violations The well is equipped with 3.5 inch production casing and a gate valve. The well is in production. There is a house gas tap at the well. ID is posted.
0698216806 2013-05-30 Production Wells Violations Noted The well head was found to be leaking gas. The well is a former storage well. The 3.5 inch has rusted out at the swage. It was patched previously with a piece of rubber and hose clamps. The well needs to be repaired to contain gas pressure by July 31, 2013. ID needs to be posted at the well.
1498403312 2013-07-25 Production Wells No Violations The leak from the 3.5 inch has been repaired with a patch and a resin based sealant. The well is no longer leaking.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0698216806 US-OH-127902 2013-07-25 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[8]

References