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Well ID: 34-059-23203 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Oxford Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: BULLIONS W | |
License Status: Final Restoration | |
License Date: 2014-11-25 | |
Spud Date: 1981-12-18 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-12-23 | |
Well Total Depth: 6176 ft | |
Configuration: Vertical | |
Latitude: 40.039120804 | |
Longitude: -81.33331590 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-11-13 | 2143 CARLESS RESOURCES INC GeoDate 11/13/81 |
Original Spud | 1981-12-18 | |
Completed | 1981-12-23 | |
Reached Total Depth | 1981-12-23 | |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Correction to Well | 2000-04-07 | ADDED THE FOLLOWING TO DATABASE: FOOTAGE LOCATION: 510'NL & 1836'EL OF SEC. 36; X= 2,326,675; Y= 744,800 AND ELEVATION 1020' |
Change of Owner | 2010-05-06 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2014-11-25 | Proposed Formations:CLINTON, Issued Date:11/25/2014, Expired Date:11/24/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-09-16 | |
Construction Permit Expires | 2016-11-24 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5994 | 6012 | 11 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 50000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0095958068 | 2015-09-16 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Chipco LLC after pulling tubing on 9/15/15 and setting up to rip 4.5 inch casing found that the casing was parted at 1506 feet. Chipco tripped 1.5 inch tubing in to 1723 feet gained circulation and pumped a 60 sack 200 foot Class A bottom of the surface cement plug from 1723 feet to 1523 feet. Cement was displaced with 3.8bbls of fresh water. Chipco tripped tubing to 200 feet gained circulation and pumped a sack 200 foot Class A surface cement plug from 200 feet to surface. Cement stayed at the surface. |
0335150967 | 2006-05-30 | Production Wells | No Violations | PRODUCING WELL. |
0386693145 | 2005-11-18 | Production Wells | No Violations | STATUS CHECK |
0822108854 | 2015-10-22 | Final Restoration | No Violations | I received call from Operator stating debris has been removed. Upon inspection remaining debris has been removed and the site passed final restoration according to ORC 1509.072B. |
1070847220 | 2005-09-16 | Production Wells | No Violations | STATUS CHECK |
1105517254 | 2004-08-18 | Production Wells | No Violations | STATUS CHECK, 210 BBL. |
1106227508 | 2005-01-19 | Production Wells | No Violations | CHECK TANK SITE FOR LEAKS. |
1352713635 | 2015-10-21 | Plug / Plug Back | No Violations | On the day of my inspection I restoration of location was completed and production equipment has been removed. Five pieces of 4.5 inch casing 9 foot in length were still on site where 210bbl tank was sitting. I placed call to operator and requested that the casing be removed and area seeded. |
1442231966 | 2015-09-14 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Chipco LLC tripped 1.5 inch tubing to 3700 feet and Appalachian Well Service perforated the Big Lime with 10 Shots from 4300 feet to 4290 feet with 10 shots. Chipco ran 1.5 inch tubing to 6026 feet and pumped a 30 sack 400 foot Class A Clinton plug from 6026 feet to 5626 feet. Cement was displaced with 14bbls of fresh water. Chipco tripped tubing to 4295 and pumped a 60 sack 200 foot Class A Big Lime plug from 4295 to 4095 feet. Cement was displaced with 10.3bbls of fresh water. Chipco tripped tubing out and will rip 4.5 inch casing tomorrow. |
1510270107 | 2006-05-05 | Production Wells | No Violations | PRODUCING WELL |
1990988802 | 2007-11-21 | Production Wells | No Violations | STATUS CHECK. PRODUCING WELL |
2039455782 | 2008-01-16 | Production Wells | No Violations | TANK REPLACED. CHANGED TO 100 BBL. |
For data sources see[9]