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34-013-21016

Well Details

Well ID: 34-013-21016
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Country: United States
State: Ohio
County: Belmont
Municipality: York Township
Operator Name: GULFPORT ENERGY CORPORATION
Well Pad ID: US-OH-001342
Farm/Lease Name: CHARLIE 210472
License Status: Cancelled
License Date: 2015-11-17
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Horizontal
Latitude: 39.878282475
Longitude: -80.84251478

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2015-11-17 Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:11/17/2015, Expired Date:11/16/2017 12:00:00 PM, Drilling unit acres:552.218, Proposed Well Type:OG, Proposed Well Class:POOL
Record Last Modified 2017-02-10
Construction Permit Expires 2017-11-16

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0359240881 2017-10-12 Production Wells No Violations This well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing with no artificial lift technology present. The well is piped to a gas processing unit and then to a production area that contains four 400-barrel production fluid holding tanks. Production records for this well are current to 2017 within RBDMS.
0910310859 2016-01-19 Surface Facility Construction No Violations On this day I was accompanied by Inspector Jim Nicholson. Jim and I were reviewing the slip area that is to be remediated. There was a track hoe working large rocks into the slip area for stabilization. Operations on this pad are on hold until the slip area is approved by the engineering section.
1075567030 2016-01-21 Surface Facility Construction No Violations On this day I was accompanied by Emergency Responder Josh S. Josh and I were reviewing the slip area that is to be remediated. There was a track hoe working large rocks into the slip area for stabilization. Operations on this pad are on hold until the slip area is approved by the engineering section.
1467137732 2018-08-20 Production Wells No Violations On the day of my inspection I witnessed that the well was equipped with a three-string casing design with 5.5-inch diameter production casing that appeared to be open flowing with no artificial lift technology. Annular pressure monitoring was in place for the 9.625-inch diameter intermediate casing gauge read 0 pounds per square inch, and the 13.375-inch diameter casing gauge read 120 pounds per square inch. Production equipment included a Sand Separator, Gas Processing unit and four 400-barrel production fluid tanks, and a 50-barrel produced water tank shared with the other producing wells on the well pad. There were multiple Emergency Shutoff Devices on location, Identification tags were present, and production was up to date.
1698847506 2016-03-05 Casing String Witnessed No Violations On this day Rocky Mountain had reached a total depth of 110 with the 32 auger bit. The 26 casing was ran and cemented by Stingray Cementing using 290 sack of Class A cement. Cement returns to surface were successful.

For data sources see[3]

References