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37-005-01538

Well Details

Well ID: 37-005-01538
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Sugarcreek Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: KEYSTONE MINING CO. 5463
License Status: Plugged OG Well
Spud Date: 1/1/1800
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.956426
Longitude: -79.592134

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1992 NATL FUEL GAS SUPPLY CORP 3,896.00 366 0.00 0.00
1996 SENECA RESOURCES CORP 2,939.00 365 0.00 0.00
1997 SENECA RESOURCES CORP 3,606.00 359 0.00 0.00
1998 SENECA RESOURCES CORP 3,372.00 359 0.00 0.00
1999 SENECA RESOURCES CORP 3,294.00 365 0.00 0.00
2000 SENECA RESOURCES CORP 3,008.00 365 0.00 0.00
2001 SENECA RESOURCES CORP 3,483.00 365 0.00 0.00
2002 SENECA RESOURCES CORP 3,552.00 365 0.00 0.00
2003 SENECA RESOURCES CORP 3,806.00 364 0.00 0.00
2004 SENECA RESOURCES CORP 3,758.00 365 0.00 0.00
2006 SENECA RESOURCES CORP 2,506.00 365 0.00 0.00
2007 SENECA RESOURCES CORP 2,272.00 365 0.00 0.00
2008 SENECA RESOURCES CORP 2,483.00 365 0.00 0.00
2009 SENECA RESOURCES CORP 2,476.00 365 0.00 0.00
2010 SENECA RESOURCES CO LLC 2,145.00 365 0.00 0.00
2011 0.00 0.00 0.00
2012 0.00 0.00 0.00
2013 SENECA RESOURCES CO LLC 686.00 365 0.00 0.00
2014 0.00 0.00 0.00
2015 0.00 0.00 0.00
2016 0.00 0.00 0.00
2017 0.00 0.00 0.00
2018 0.00 0.00 0.00

For data sources see[4]

Waste Data

Period Waste Type Quantity Disposal Method Waste Facility ID
2018-0 Produced Fluid (in Barrels) RWC 802 50.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2760965 Primary Facility 2018-08-07 Plugging(Includes Plugged/Mined Through) No Violations Noted The plugging rig has reached a TD of 1420' and was rigging up tools to prepare to drill out and clean the hole out a bit deeper in order to expose and cement through the Venango gas bearing sands if possible. All equipment on site looked ok.

For data sources see[6]

References