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Well ID: 37-005-01538 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Sugarcreek Township | |
Operator Name: SENECA RESOURCES CO LLC | |
Well Pad ID: | |
Farm/Lease Name: KEYSTONE MINING CO. | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.956426 | |
Longitude: -79.592134 |
Date | Event |
---|---|
1901-01-01 | Drilling Completion |
1986-01-01 | OLD WELL |
2018-08-06 | Begin Plugging |
2018-08-23 | Finished Plugging |
2019-06-28 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | NATL FUEL GAS SUPPLY CORP | 3408.00 | 352 | 0.00 | 0 | 0.00 | 0 |
1992 | NATL FUEL GAS SUPPLY CORP | 3,896.00 | 366 | 0.00 | 0 | 0.00 | 0 |
1996 | SENECA RESOURCES CO LLC | 2939 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | SENECA RESOURCES CO LLC | 3606 | 359 | 0.00 | 0 | 0.00 | 0 |
1998 | SENECA RESOURCES CO LLC | 3372 | 359 | 0.00 | 0 | 0.00 | 0 |
1999 | SENECA RESOURCES CO LLC | 3294 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | SENECA RESOURCES CO LLC | 3,008.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | SENECA RESOURCES CO LLC | 3483 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | SENECA RESOURCES CO LLC | 3552 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | SENECA RESOURCES CO LLC | 3806 | 364 | 0.00 | 0 | 0.00 | 0 |
2004 | SENECA RESOURCES CO LLC | 3758 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | SENECA RESOURCES CO LLC | 2506.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | SENECA RESOURCES CO LLC | 2272.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 2483.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 2476.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 2,145.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 686.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2018 | SENECA RESOURCES CO LLC | Produced Fluid | 50.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2760965 | Primary Facility | 2018-08-07 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | The plugging rig has reached a TD of 1420' and was rigging up tools to prepare to drill out and clean the hole out a bit deeper in order to expose and cement through the Venango gas bearing sands if possible. All equipment on site looked ok. |
For data sources see[7]