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Well ID: 34-007-20773 | Loading map...
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County: Ashtabula | |
Municipality: | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 41.69159013 | |
Longitude: -80.72473748 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1993-0 | 64.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1376655411 | 2013-08-16 | When I arrived on location on 8/16/2013 Nick's Well Plugging was rigged up and ripped the 4.5 casing at 2285'. Nick's then broke circulation on the well and proceeded to run 86 sacks of Class A cement to cover the Big Lime plug. Nick's pulled 61 joints of 4.5 casing. Nick's then broke circulation and proceeded to run 115 sacks of Class A cement. Cement was circulated to surface. The remaining 12 joints of 4.5 casing was removed from the well and the hole was topped off with cement. | ||||
1386863152 | 2013-09-24 | The final restoration has been completed . There is a landowner waiver to leave three telephone poles from road to well site area . No violations . The final restoration is approved . | ||||
230924419 | 2013-08-29 | The well has been plugged resolving the compliance notice issued on 7-17-2012 . Complaintant [ Norm Stokes ] . NO VIOLATIONS RESOLVED . | ||||
-465337490 | 2012-07-17 | My inspection of this well was in response to a request from Norm Stokes [ landowner ]. My inspection found there is no tank battery for this well. Further inspection of wellhead found 4.5 casing with swedge reduced to 2 with a valve which is shut-in. The well is disconnected from the flow line. Our database records showed no production reported since 1993. This well is idle. I spoke with Ralph Tallmadge (Northwood Energy) of this idle well violation and the deadline [ 9-21-2012 ] for remediation of this violation. | ||||
-789032456 | 2013-08-15 | I arrived on location on 08/15/2013 and Nick's Well Plugging was on location to perform the plug job. Nick's rigged up and bullheaded the bottom plug with 30 sacks of Class A cement and 50lbs of cottonseed hulls. The plug landed and the well was pressured up to 1500psi. The well was shut in until the following morning. |
For data sources see[2]