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Well ID: 34-007-20773 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashtabula | |
Municipality: Lenox Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: SCHMITT | |
License Status: Final Restoration | |
License Date: 2012-09-21 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: 3620.00 ft | |
Configuration: Vertical | |
Latitude: 41.690000 | |
Longitude: -80.720000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-07-07 | 298 NATIONAL PETROLEUM CORP GeoDate 7/7/82 |
Unknown | 1982-07-07 | Issued Date 7/7/82 Expired Date 1/1/83 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
CO | 1983-01-25 | 2669 WOOD DONALD E GeoDate 1/25/83 |
Unknown | 1983-01-25 | Issued Date 1/25/83 Expired Date 7/24/83 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Change of Owner | 2002-10-16 | Operator changed from 2669, WOOD DONALD E to 1634, NORTHWOOD ENERGY CORP |
APP | 2012-09-21 | Proposed Formations:CLINTON, Issued Date:9/21/2012, Expired Date:9/21/2014 12:00:00 PM, Drilling unit acres:45, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-08-16 | |
Record Last Modified | 2014-07-10 | |
Construction Permit Expires | 2014-09-21 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3462 | 3530 | 22 |
3462 | 3530 | 22 | |
3462 | 3530 | 22 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1950 Bbl | 50000 | |||
ACID | 0 | 500 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | WOOD DONALD E | 64.00 | 0.00 | 365 |
2006 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2008 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2009 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2011 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2013 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 228 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | WOOD DONALD E | Brine | 0 | 365 |
2006 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2008 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2009 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2010 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2011 | NORTHWOOD ENERGY CORP | Brine | 0 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2013 | NORTHWOOD ENERGY CORP | Brine | 0 | 228 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-465337490 | 2012-7-17 0:00: | PW | No Violations | |
-789032456 | 2013-8-15 0:00: | PB | No Violations | |
0230924419 | 2013-08-29 | Plug / Plug Back | No Violations | The well has been plugged resolving the compliance notice issued on 7-17-2012 . Complaintant [ Norm Stokes ] . NO VIOLATIONS RESOLVED . |
0465337490 | 2012-07-17 | Production Wells | No Violations | My inspection of this well was in response to a request from Norm Stokes [ landowner ]. My inspection found there is no tank battery for this well. Further inspection of wellhead found 4.5 casing with swedge reduced to 2 with a valve which is shut-in. The well is disconnected from the flow line. Our database records showed no production reported since 1993. This well is idle. I spoke with Ralph Tallmadge (Northwood Energy) of this idle well violation and the deadline [ 9-21-2012 ] for remediation of this violation. |
0789032456 | 2013-08-15 | Plug / Plug Back | No Violations | I arrived on location on 08/15/2013 and Nicks Well Plugging was on location to perform the plug job. Nicks rigged up and bullheaded the bottom plug with 30 sacks of Class A cement and 50lbs of cottonseed hulls. The plug landed and the well was pressured up to 1500psi. The well was shut in until the following morning. |
1376655411 | 2013-08-16 | Plug / Plug Back | No Violations | When I arrived on location on 8/16/2013 Nicks Well Plugging was rigged up and ripped the 4.5 casing at 2285. Nicks then broke circulation on the well and proceeded to run 86 sacks of Class A cement to cover the Big Lime plug. Nicks pulled 61 joints of 4.5 casing. Nicks then broke circulation and proceeded to run 115 sacks of Class A cement. Cement was circulated to surface. The remaining 12 joints of 4.5 casing was removed from the well and the hole was topped off with cement. |
1386863152 | 2013-09-24 | Final Restoration | No Violations | The final restoration has been completed . There is a landowner waiver to leave three telephone poles from road to well site area . No violations . The final restoration is approved . |
230924419 | 2013-8-29 0:00: | PB | No Violations |
For data sources see[9]