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34-085-21265

Well Details

Well ID: 34-085-21265
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2008-12-11
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 41.6525995868
Longitude: -81.2139800466

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1357326315 2013-10-09 The producing unit consists of a wellhead and aboveground storage tank (AST) battery in separate board-on-board enclosures. The wellhead is a mechanical plunger lift unit and is producing. The battery is comprised of 1 210-barrel and 1 140-barrel steel tank and separator. Secondary containment, spacing, and signage is good. Process safety equipment (spark arrestor, carbon filter, and low-pressure relief valve) are present. Gates are locked. A drainage culvert appears to have been added along the lease road. No current problems with surface water drainage are noted.
-929051858 2012-11-07 The unit is comprised of a 2-tank battery (1 210-barrel production tank and 1 100-barrel brine tank) and mechanical separator in an 8-foot wooden enclosure. The wellhead includes a mechanical plunger lift located in a 6-foot wooden enclosure. The well is currently in production. The tank and well spacing is in accordance with 1509:9-9-05 . Unit identification is present and legible at the tank battery. I did not observe any leaks, spills, or other signs of contamination. No violations noted.
1327345506 2012-01-10 Meet land owner during inspection. Land owner is concerned about drainage accumulating on the north side of the lease road and causing trees to fall. Water accumulates in a low area on the land owners property. Low area could be connected to a drainage ditch that is west of the low area. The land owner is also concerned about a seep that has formed in the area between the wellhead and the tank battery. Sent Tim Reilly an e-mail notifying him of the landowner concerns. Land owner is happy with the condition of the site accept for the drainage. HB-278 equipment needs installed on the tank battery. Called Jim from John D informed him that the well needs HB-278 equipment installed on the battery, charcoal filter, spark arrestor, sealing hatches and low-pressure relief valves. 9-05E4
1331666417 2012-03-13 HB-278 equipment has been installed on the production tanks. Preliminary Restoration has been completed. The man doors still need locks and an identification sign needs posted on the outside of the board on board tank battery fence. The operator will be contacted in regards to needed items.
1720270613 2009-10-20 There were no violations at the time of inspection.
242638581 2008-12-11 cementing surface