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34-121-23136

Well Details

Well ID: 34-121-23136
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-05-29
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.6035231919
Longitude: -81.4940405001

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-126321449 2004-03-23 Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phot's indicate

H2S gas odor present.

1362360061 2014-05-02 My inspection today finds the service rig crew pulled the collar off of the 4.5" casing while trying to rip the pipe. The cement crew was sent back.
1399049324 2014-05-01 My inspection today finds Davis Well Service moved a rig onto the location. The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042'.
1399309060 2014-05-05 My inspection today finds the casing was ripped at 3660'. Cemenco circulated a 38 sk class A 2% gel plug. The casing was pulled up to 1950'. Cemenco circulated a 52 sk 2% gel plug into place. A 200' 54 sk plug was placed from 200' to surface. I instructed the company to reclaim the site in accordance with 1509.072.
1668780202 2014-07-02 Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
PL7609 Preliminary Restoration done information from Data Point