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34-105-22738

Well Details

Well ID: 34-105-22738
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2006-07-05
Unconventional:
Horizontal:
Producing: No
Violations: 18
Latitude: 39.0532160619
Longitude: -82.0955970568

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1015311589 2006-08-10 No one on site.
-1019772435 2006-05-17 The needle valve was replaced. However, the 2 inch valve on the annulus will not open. The dike needs further cleanup.
-1031969427 2004-02-05 Well pressures were measured just after pump had shut off. No violations at the time of inspection.
-1134615602 2011-10-25 Accompanied J. Scott on SWIW inspection. No violations, loading pad may need have cement and drain installed.
-1253271848 2003-03-05 No violations, unable to check pressures need small wrench.
-1496623811 2014-05-20 Follow up to 935681809. Dike patched. No noted violations. Flow meter read 7256 Barrels at 15 gallons/minutes.
-1618094538 2013-01-18 Pump running during inspection. The upper dike with the 210 Barrel steel tank is developing small cracks in the bottom. The dike shall be repaired or replaced so that it is water tight. 9-3-08(A)
-1649795380 2012-08-22 No violations.
-1680881677 2005-06-16 The owner's representative increased the pressure on the annulus to 1220 psi. The pressures on both sides were monitored for 30 minutes. As the tubing pressure dropped, the annular pressure increased 25 psi. Overall, the well demonstrated mechanical integrity.

(Injection: start 758 psi / stop 738 psi Annulus: start 1220 psi / stop 1245 psi)

-1685942370 2008-12-03 There were no violations at the time of inspection.
-1689183921 2007-09-10 There were no violations at the time of inspection. Pump was operating.
-216142501 2005-01-13 There were no violations at the time of inspection.
-309365208 2013-10-28 Inspected containment dike, tanks, annulus pressure, injection pressure and injection pump. Dike is free of water. Identification is on tank.
-314250351 2011-03-08 Dike free of fresh water.
-403589900 2013-07-17 No violations.
-458835377 2004-07-15 NOV FOLLOW-UP The well is in noncompliance. The valve on the annulus needs replaced. Spoke with the well tender regarding the required remedy.
-468537078 2014-02-20 Follow up to 935681809. Dike repairs not made yet.
-479986209 2006-06-27 The well was in compliance.
-492626496 2006-08-11 Preformed a mechanical integrity test on the well. Started the test with an annular pressure of 836 psi.. The well passed with a 0.6% loss in pressure, over a 15 minute period.
-753672285 2006-07-31
-760721356 2008-02-25 An inspection found that there was no fittings to monitor the annulus pressure. All other conditions were acceptable. 9-3-07(F)
-895875091 2006-03-29 Oil and water pooling inside the dike. The threads, inside the 1/4 inch needle valve on the backside, were corroded and no longer operational. 9-3-04(A)
-895875091 2006-03-29 Oil and water pooling inside the dike. The threads, inside the 1/4 inch needle valve on the backside, were corroded and no longer operational. 9-3-05(A)3
-954425920 2006-07-14 No one onsite.
-954425920193713 2006-07-14 No one onsite.
-954425920196463 2006-07-14 No one onsite.
-966095518 2005-05-06 Measured pressures while pump was off. The well was pumping at 830 psi.. 9-3-04(A)
-966095518 2005-05-06 Measured pressures while pump was off. The well was pumping at 830 psi.. 9-3-05(B)4
-966095518 2005-05-06 Measured pressures while pump was off. The well was pumping at 830 psi.. 9-3-07(G)
-97918536 2007-02-16 There were no violations at the time of inspection.
-985386220 2003-07-11 FOLLOW UP TO NOV # 1058282884 An inspection of the well site revealed the following:

A storage tank was leaking a stream of brine. The dike was half full of brine. There were several cracks in the dike walls. The two 1/4 inch valves on the well were inoperative.

R

9-9-05(A)9
-985386220 2003-07-11 FOLLOW UP TO NOV # 1058282884 An inspection of the well site revealed the following:

A storage tank was leaking a stream of brine. The dike was half full of brine. There were several cracks in the dike walls. The two 1/4 inch valves on the well were inoperative.

R

NONE(B)
1009030321 2009-11-24 Has identification. No violations observed during inspection.
1013875276 2011-08-24 Water truck on site.
1051658233 2007-06-04 No violations were found at the time.
1058282884 2003-07-11 An inspection of the well site revealed the following:

A storage tank was leaking a stream of brine. The dike was half full of brine. There were several cracks in the dike walls. The two 1/4 inch valves on the well were inoperative.

Repair or replace leaking storage tank. Remove brine and oil from inside the dike. Seal cracks in order to make the dike watertight. Repair or replace the valves to allow monitoring.

9-9-05(A)9
1058282884 2003-07-11 An inspection of the well site revealed the following:

A storage tank was leaking a stream of brine. The dike was half full of brine. There were several cracks in the dike walls. The two 1/4 inch valves on the well were inoperative.

Repair or replace leaking storage tank. Remove brine and oil from inside the dike. Seal cracks in order to make the dike watertight. Repair or replace the valves to allow monitoring.

NONE(B)
1132155442 2005-11-15 Unable to screw gauge into the needle valve on annulus. 9-3-05(B)4
1159462003 2006-09-28 Plumbing in the flow lines.
1166557908 2006-12-18 The pressures were measured, while the pump was operating.
1186407148 2007-04-12 No violations were found.
1223813687 2004-07-20 NOV FOLLOW-UP The well has a new needle valve, on the annulus. The dike will require some clean-up work.
1260645893 2009-03-11 The two inch annulus valve froze and broke. Therefore, the annulus pressure was not gauged.
1279819432 2010-07-14 Pump is dripping. 2" steel line is leaking between 90 and hammer union. I have talked to Jonathan Reese and it will be repaired next week. Parts have to be ordered. All brine drips are being contained with in the dike. 9-3-07(H)
1313315948 2010-09-27 New 2" pipe from the union to "flex" line has multiple leaks. One major leak is on the welded 90 ELL. The Other major leak has a rag (held in place with black tape) covering the leak. The leaks must be fixed. All materials used on the line must be able to with stand the max injection pressures of 1245 psi. Please provide documentation on the "flex stainless steel line" as to pressure rating. 9-3-07(H)
1391522268 2014-02-04 Follow up to 935681809. Unable to verify dike repairs due to frozen conditions. No noted violations, pump running at time of inspection.
1406232116 2014-07-24 No noted violations.
1440344665 2009-06-08 There were no violations at the time.
1484468400 2004-04-08 Bad valve on annulus.
1488255564 2008-06-02 There were no violations found at the time of inspection.
1574195057 2013-11-26 Accompanied Inspector Josh Garland on inspection. He checked pressures on the well. Water was flowing into tank battery containment via a crack in the concrete. The pumper stopped by and we talked with him about repair options.
1621905531 2010-09-30 Replaced leaking fittings and pipe with yellow flex pipe. Writing on side of yellow flex pipe is: 4805 wire air 600 psi wp 40 bar. No leaks observed.
162411494 2006-09-12 Old tanks and concrete dike have been removed. Approximately half the site was graded. Upper concrete pad was constructed with a new 210 bbl tank in place. Work on hold due to rain.
1681259005 2006-10-04 Surface facility construction was complete.
1723700535 2013-12-19 Inspected the containment dike, tanks, injection pump, injection line, injection pressure, and annulus pressure. Identification is posted on the 1st tank. Dike is free of water.
1752871480 2006-09-21 Concrete dike completed. In the process of setting the tanks (a 210 bbl knockout, two 210 bbl brine tanks and one 100 bbl oil tank.)
184754198 2006-08-03 Witnessed a cement squeeze job on the 4 1/2 inch casing. Wiper plug sent to 2630 feet.
1847702381 2011-08-09 Vegetation reestablished, no erosion, no drilling equipment, good ID. PR passed.
1902001620 2013-04-08 Inspected containment dike, injection pressure and annulus pressure. Good identification on tank. Dike is free of water.
2018145642 2006-07-27 Tested the well (bottom plug) with 1810 psi. on the 4 1/2 inch casing. The well passed, losing 5 psi. total over a 15 minutes period.
2025019888 2004-05-03 Unable to measure the pressure on the annulus, because the valve is corroded shut. 9-3-05(A)3
2025019888 2004-05-03 Unable to measure the pressure on the annulus, because the valve is corroded shut. 9-3-07(F)
208058352 2005-07-28 Oil and water inside dike. Notified the operator that the dike needed cleaned-up.
2083295145 2006-10-18 No violations at the time. Spoke with Spence Carpenter, regarding the rainwater run-off.
26148579 2006-07-11 The wire line tool (tubing cutter) got hung inside the tubing and lost at approximately 1120 feet. The job was postponed.
264255952 2006-06-14 No action has been taken to remedy the violations.
266102610 2004-08-17 Oil pooling inside dike. Notified well tender. 9-3-04(A)
348166438 2007-07-17 No violations were found at the time of inspection.
34888376 2006-06-30 Pumped cement plug through the tubing into the injection zone.
405495453 2010-11-24 Dike is free of water. New injection line connections are not leaking.
434129276 2006-08-30 Work on the surface facility progressing.
447604848 2006-10-17 No violations. Accompanied by Jon Scott.
532289267 2006-07-26 Completed the plug-back of the well.
546468863 2006-09-07 Work on the surface facility progressing.
560004650 2008-09-11 No violations were found at the time of inspection.
584938746 2010-03-18 Good identification. Dike is clean with no water in it.
586316528 2008-04-21 There were no violations at the time at the time of inspection.
606662405 2007-10-22 There were no violations.
612619482 2006-07-18 Washing out the tubing (just below 900 feet) in order to retrieve the wire line tool at 1120 feet.
734557798 2013-06-06 Follow up to -1618094538. The cracks in the dikes have been sealed.
780271050 2012-06-25 No violations.
7890950 2003-12-04 No violations at the time of inspection.
905121282 2004-10-08 There were no violations at the time of inspection.
908607114 2009-08-18 Good identification. No violations at the time of inspection.
915878355 2008-11-06 Notified the well tender that the gauge on the annulus was started to round-off.
935681809 2013-11-26 Flow meter at well read 2242 Barrels. A small crack was noticed in the dike and water was flowing into dike. Dike shall be repaired or replaced in order to be water tight. Spoke with field manager on site and discussed repairs. 9-3-08(A)
994581678 2011-10-25 No violations observed during inspection.
UIC119 1987-03-09 1501:9-3-07(E)&(F)