X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-093-60473"

m
m
Line 1: Line 1:
__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-093-60473
 
| Well ID: 34-093-60473
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.39446431, -82.03992329 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.394510857, -82.03979046 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Lorain County, Ohio|Lorain]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Lorain_County,_Ohio|Lorain]]
 +
|-
 +
| Municipality: Ridgeville Township
 
|-
 
|-
 
| Operator Name: [[FJD PROPERTIES LLC]]
 
| Operator Name: [[FJD PROPERTIES LLC]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: FJD PROPERTIES LLC (WINCKLES)
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2014-03-26
 
|-
 
|-
 
| Spud Date: 1941-10-09
 
| Spud Date: 1941-10-09
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1941-11-06
 +
|-
 +
| Well Total Depth: 2478 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.394510857
 +
|-
 +
| Longitude: -82.03979046
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| Original Spud
 +
| 1941-10-09
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 
|-
 
|-
| Latitude: 41.39446431
+
| Completed
 +
| 1941-11-06
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 
|-
 
|-
| Longitude: -82.03992329
+
| Reached Total Depth
 +
| 1941-11-06
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 +
|-
 +
| Correction to Well
 +
| 2007-09-28
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 +
|-
 +
| Change of Owner
 +
| 2014-01-13
 +
| Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM
 +
|-
 +
| APP
 +
| 2014-01-17
 +
| Proposed Formations:SHALE, Issued Date:1/17/2014, Expired Date:1/17/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Change of Owner
 +
| 2014-02-12
 +
| Operator changed from 40004, COTTRELL AARON to 40005, FJD PROPERTIES LLC
 +
|-
 +
| Change of Owner
 +
| 2014-02-12
 +
| Operator changed from 8318, ORPHAN WELL PROGRAM to 40004, COTTRELL AARON
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2014-03-07
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2014-03-07
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 +
|-
 +
| Construction Permit Expires
 +
| 2016-01-17
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 +
|-
 +
| Record Last Modified
 +
| 2017-02-10
 +
| UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0046932437
 +
| 2014-02-13
 +
| Orphan
 +
| No Violations
 +
|    A follow-up inspection was conducted on 02/13/2014 for contract compliance.
 +
 
 +
  1. Excavating continues and contractor is placing the excavated clay
 +
      material in the northwest stockpile.
 +
 
 +
  2. Sewer line was removed and the water is continuing to flow  from the
 +
      gravel base of the sewer ditch.
 +
 
 +
 
 +
    Note: Keeping Mark Bruce (ODNR Communication Department) apprised of
 +
              progress at the site.
 +
 
 +
END
 +
|-
 +
| 0064861059
 +
| 2014-02-12
 +
| Plug / Plug Back
 +
| No Violations
 +
| Visited location on 02/12/2014 with Norburt Lowder to check on status of excavation operations and discuss plan forward.  At time of visit, Whipstock Drilling was excavating at approximately 15 below ground level.
 +
|-
 +
| 0253263923
 +
| 2014-02-06
 +
| Orphan
 +
| No Violations
 +
|  Shut down due to subzero weather.
 +
|-
 +
| 0464544559
 +
| 2014-03-03
 +
| Orphan
 +
| No Violations
 +
| A follow-up inspection  was conducted on 03/03/2014 for contract compliance.
 +
 
 +
  1.Equipment freezing up due to the subzero weather.
 +
 
 +
  2. Started to clean out at 13:00 hrs, working on the obstruction at 60 using a 4.3750 tri cone bit. At first the circulating fluid was clear but then it turned to a blackish color. Drilled down to 76.
 +
 
 +
  3. Circulating out large pieces of Red Bedford Shale, due to fresh water that is being used to circulate.
 +
 
 +
  4. Shut down for the day at 16:00 hrs.
 +
 
 +
    END
 +
|-
 +
| 0638603913
 +
| 2014-02-11
 +
| Plug / Plug Back
 +
| No Violations
 +
| Visited location on 02/11/2014 with Norburt Lowder to check on status of excavation.  Whipstock Drilling is continuining to excavate down to wellhead.  At the time of the visit, they were at approximately 12 down from ground level.
 +
|-
 +
| 0849949934
 +
| 2014-02-12
 +
| Orphan
 +
| No Violations
 +
|  A follow-up inspection was conducted on 02/12/2014 for contract compliance.
 +
 
 +
  1. A replacement pump arrived and was placed close to the vault so 
 +
      the water can be pumped from it. Once the waterwas pumped out of the
 +
      well vault and the casing was exposed, the gas leakage from the well
 +
      diminished.  No gas was detected in excavation, however elevated gas
 +
      readings were detected in the vault. 
 +
 
 +
  2. Whipstock completed excavation down to the sewer line (approximately
 +
 
 +
 
 +
  3. The sewer contractors arrived to determine if the lines needed to be
 +
      removed or worked around it. They decided to remove it.
 +
 
 +
 
 +
  END
 +
|-
 +
| 0964372000
 +
| 2014-02-10
 +
| Plug / Plug Back
 +
| No Violations
 +
| Visited location on 02/10/2014 with Norburt Lowder to check-on status of excavation operations.  Whipstock Drilling excavating at approximately 6 below ground level to reach wellhead.
 +
|-
 +
| 0972176465
 +
| 2014-02-15
 +
| Orphan
 +
| No Violations
 +
|
 +
RECORD OF CONVERSATION ON 02/15/2014
 +
 
 +
    Phone call received from Chris Corso (Whipstock) advising me they 
 +
 
 +
  collar. He also noted that marks were present on the casing that appeared to
 +
  be from the teeth of a large track hoe bucket.
 +
 
 +
    No work will be done on Sunday 02/16/2014.
 +
 +
   
 +
 
 +
  END
 
|-
 
|-
 
| 1157642099
 
| 1157642099
 
| 2006-09-07
 
| 2006-09-07
|  
+
| Orphan
| Case # I&O 06-004, Met with Chris Teater to locate leaking gas well on housing development property at 37000 Center Ridge Rd. in North Ridgeville. Located a concrete column 23' underground with gas bubbling thru center of concrete column at 100% lel.. There is casing inside concrete but not sure of diameter. From photo's it is 5'' casing and it is bent over in bottom of 60'' corregated plastic pipe over  well . Construction company located gas leaking during removal of trees. Concrete around well will have to be chipped away to determine casing size. No houses are around well location at this time but construction to begin in October 2006. Sun, 70 degrees.
+
| No Violations
|
+
| Case # I&O 06-004, Met with Chris Teater to locate leaking gas well on housing development property at 37000 Center Ridge Rd. in North Ridgeville. Located a concrete column 23 underground with gas bubbling thru center of concrete column at 100% lel.. There is casing inside concrete but not sure of diameter. From photos it is 5 casing and it is bent over in bottom of 60 corregated plastic pipe over  well . Construction company located gas leaking during removal of trees. Concrete around well will have to be chipped away to determine casing size. No houses are around well location at this time but construction to begin in October 2006. Sun, 70 degrees.
|
 
|
 
 
|-
 
|-
|-
+
| 1170796367
| -1170796367
 
 
| 2008-08-06
 
| 2008-08-06
|  
+
| Orphan
| I&O case # 06-004 Chris Teeter. Requested by Mike McCormac to inspect well site for orphan well program. Well is in a new development and houses are getting closer to well site since last materix evaluation. Well has increased in gas leakage to 100 % lel 5' above well. My recommendation would be to plug the well this fall, to eliminate costs, due to hazards near a house. Nearest home now is 500' in diameter. I am submitting a new matrix to Mike McCormac. Dry, sun, 85 degrees.
+
| No Violations
|
+
| I&O case # 06-004 Chris Teeter. Requested by Mike McCormac to inspect well site for orphan well program. Well is in a new development and houses are getting closer to well site since last materix evaluation. Well has increased in gas leakage to 100 % lel 5 above well. My recommendation would be to plug the well this fall, to eliminate costs, due to hazards near a house. Nearest home now is 500 in diameter. I am submitting a new matrix to Mike McCormac. Dry, sun, 85 degrees.
|
 
|
 
|-
 
 
|-
 
|-
| -1193531815
+
| 1193531815
 
| 2014-02-18
 
| 2014-02-18
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Visited location 0n 02/18/2014 to check-on status of excavation operations and assist with filming of ODNR video with Norburt Lowder.
 
| Visited location 0n 02/18/2014 to check-on status of excavation operations and assist with filming of ODNR video with Norburt Lowder.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1306816129
 
| 1306816129
 
| 2014-03-26
 
| 2014-03-26
|  
+
| Final Restoration
 +
| No Violations
 
| A follow-up inspection was conducted on 03/26/2014 for contract compliance.
 
| A follow-up inspection was conducted on 03/26/2014 for contract compliance.
  
 
     1)  This well is located in the next phase of a housing development of K. Hovnanian Homes. This well is on the south side of Tailfeather Drive, in the block of address 1088 to 1091. There is no paved street in this area yet. The housing contractor has installed the water and sewer main lines and several lateral lines.
 
     1)  This well is located in the next phase of a housing development of K. Hovnanian Homes. This well is on the south side of Tailfeather Drive, in the block of address 1088 to 1091. There is no paved street in this area yet. The housing contractor has installed the water and sewer main lines and several lateral lines.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1340797127
 
| 1340797127
 
| 2012-06-22
 
| 2012-06-22
|  
+
| Orphan
 +
| No Violations
 
| On this inspection, I was uUnable to locate the well site.
 
| On this inspection, I was uUnable to locate the well site.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1391692683
 
| 1391692683
 
| 2014-02-03
 
| 2014-02-03
|  
+
| Orphan
 +
| No Violations
 
| Inspection on 02/03/2014 was conducted for contract compliance.
 
| Inspection on 02/03/2014 was conducted for contract compliance.
  
 
   1.  The snow was removed from the area to be excavated.
 
   1.  The snow was removed from the area to be excavated.
   2. Temporary fencing was installed around perimeter (approximately 150
+
 
|
+
      Corso, Whipstock Superintendent, to put orange flagging on each fence post and KEEP OUT
|
+
 
|
+
   3. Excavating was started around well vault (black culvert). The projected excavation will be
|-
+
 
 +
  4. All excavated material will be stockpiled at the perimeter of the site. The first stockpile will be
 +
      located in the southwest corner.
 +
 +
    Note:
 +
 +
    a. The Sewer line, which had been installed by the developer of the complex, is located
 +
        approximately 10-15 to the south of the well vault and at a depth of 18.
 +
 
 +
        the north of well, will need to be removed to continue excavating.
 +
 
 +
    END
 
|-
 
|-
 
| 1392649672
 
| 1392649672
 
| 2014-02-10
 
| 2014-02-10
|  
+
| Orphan
 +
| No Violations
 
|  
 
|  
 
  A follow-up inspection; 02/10/2014 was conducted for contract compliance.
 
  A follow-up inspection; 02/10/2014 was conducted for contract compliance.
Line 117: Line 342:
  
 
   END
 
   END
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1392779866
 
| 1392779866
 
| 2014-02-13
 
| 2014-02-13
|  
+
| Orphan
 +
| No Violations
 
| Crews from Whipstock are in the process of excavating the existing overburden to allow access to the damaged remaining casing of the well. Work is ongoing and work at the wellhead will not take place until later in the week.
 
| Crews from Whipstock are in the process of excavating the existing overburden to allow access to the damaged remaining casing of the well. Work is ongoing and work at the wellhead will not take place until later in the week.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1393248892
 
| 1393248892
 
| 2014-02-05
 
| 2014-02-05
|  
+
| Orphan
 +
| No Violations
 
| Shut down due to sudzero weather.
 
| Shut down due to sudzero weather.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1393337156
 
| 1393337156
 
| 2014-02-07
 
| 2014-02-07
|  
+
| Orphan
 +
| No Violations
 
| No on site inspection done on 02/07/2014.
 
| No on site inspection done on 02/07/2014.
 
Shut down due to subzero weather.
 
Shut down due to subzero weather.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1394469632
 
| 1394469632
 
| 2014-03-10
 
| 2014-03-10
|  
+
| Orphan
 +
| No Violations
 
| Plugging and abandonment operations are being completed. Cementing was completed on Friday 3/7/14. The cement is firm and set at a nominal 24 inches below the top of the casing collar. Whipstock crews indicated that the plan is to cut the casing off at 4 feet below the existing grade and install a short section of black, corrugated drain pipe around the well once the cap is welded on with ID#. I inspected both the cement in the casing and samples of the cement retained in cups. Both look firm and solid. No gas detected via meter. I collected a GPS location data as well as triangulation measurements from selected locations for future reference.
 
| Plugging and abandonment operations are being completed. Cementing was completed on Friday 3/7/14. The cement is firm and set at a nominal 24 inches below the top of the casing collar. Whipstock crews indicated that the plan is to cut the casing off at 4 feet below the existing grade and install a short section of black, corrugated drain pipe around the well once the cap is welded on with ID#. I inspected both the cement in the casing and samples of the cement retained in cups. Both look firm and solid. No gas detected via meter. I collected a GPS location data as well as triangulation measurements from selected locations for future reference.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1395242127
 
| 1395242127
 
| 2014-02-20
 
| 2014-02-20
|  
+
| Orphan
 +
| No Violations
 
|  
 
|  
 
   A follow-up inspection  was conducted on 02/20/2014 for contract compliance.
 
   A follow-up inspection  was conducted on 02/20/2014 for contract compliance.
Line 170: Line 380:
  
 
     END
 
     END
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1513686661
 
| 1513686661
 
| 2014-02-04
 
| 2014-02-04
|  
+
| Orphan
|  
+
| No Violations
 +
|   
 
     A follow-up inspection was conducted on 02/04/2014 for contract compliance.
 
     A follow-up inspection was conducted on 02/04/2014 for contract compliance.
 
      
 
      
   1. Whipstock is currently excavating at a depth of 12
+
 
|
+
 
|
+
   2. The water line on the north side of the excavation, that was installed by the developer was
|
+
      exposed.Whipstock contacted the developer to shut water off.
|-
+
 
 +
      east and west sides of the excavation.  
 +
 +
Note:           
 +
      When Whipstock was excavating in the area of the sewer line, which was previously installed by
 +
    the developer, they encountered black material that appeared to be high in organic matter (corn
 +
    stalks, vegtation, tree limbs and roots). Whipstock segregated this material and stockpiled it in
 +
    the southwest corner of the location. This material will not be used as back fill.
 +
 
 +
    END
 
|-
 
|-
 
| 1541231752
 
| 1541231752
 
| 2014-03-20
 
| 2014-03-20
|  
+
| Plug / Plug Back
| Visited well on 03/20/2014 to determine the status of the location at the request of Norburt Lowder.  All rig-related equipment has been removed, and the location has been rough-graded.  A 12 plastic culvert pipe is around the well, sticking out of the ground ~2'.  The water level within the pipe is down ~4' from the top of the pipe.  Occasional bubbles were noted in the water in the pipe.
+
| No Violations
|
+
| Visited well on 03/20/2014 to determine the status of the location at the request of Norburt Lowder.  All rig-related equipment has been removed, and the location has been rough-graded.  A 12 plastic culvert pipe is around the well, sticking out of the ground ~2.  The water level within the pipe is down ~4 from the top of the pipe.  Occasional bubbles were noted in the water in the pipe.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1608252901
 
| 1608252901
 
| 2014-03-05
 
| 2014-03-05
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Visited location on 03/05/2014 to observe plugging operations with Norburt Lowder.  Whipstock Drilling had run in the hole with tubing to circulate out old oil in the hole.  Will tag bottom with tubing and then prepare to plug out the well.
 
| Visited location on 03/05/2014 to observe plugging operations with Norburt Lowder.  Whipstock Drilling had run in the hole with tubing to circulate out old oil in the hole.  Will tag bottom with tubing and then prepare to plug out the well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1739275544
+
| 1739275544
 
| 2014-02-19
 
| 2014-02-19
|  
+
| Orphan
 +
| No Violations
 
|  
 
|  
 
   A follow-up inspection was conducted on 02/19/2014 for contract compliance.
 
   A follow-up inspection was conducted on 02/19/2014 for contract compliance.
Line 218: Line 429:
  
 
END.
 
END.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1894238965
 
| 1894238965
 
| 2014-02-11
 
| 2014-02-11
|  
+
| Orphan
 +
| No Violations
 
| A follow-up inspection was conducted on 02/11/2014 for contract compliance.
 
| A follow-up inspection was conducted on 02/11/2014 for contract compliance.
 
    
 
    
Line 234: Line 442:
 
  excavation will be backfilled.  I advised him to contact Gene Chini, Orphan Well Manager,
 
  excavation will be backfilled.  I advised him to contact Gene Chini, Orphan Well Manager,
 
  with any questions.
 
  with any questions.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1981808815
 +
| 2015-12-31
 +
| Final Restoration
 +
| No Violations
 +
| Collecting photographic evidence of final restoration.  Final restoration is approved.
 
|-
 
|-
| -2011015490
+
| 2011015490
 
| 2014-03-04
 
| 2014-03-04
|  
+
| Orphan
| A follow-up inspection on 03/04/2014 was conducted for contract compliance.
+
| No Violations
 +
|    A follow-up inspection on 03/04/2014 was conducted for contract compliance.
  
 
     1.Due subzero weather the equipment lines are freezing up.
 
     1.Due subzero weather the equipment lines are freezing up.
Line 249: Line 460:
 
         freezing. The salt water will help keep the Red Bedford from caving in on the  drill stem.
 
         freezing. The salt water will help keep the Red Bedford from caving in on the  drill stem.
  
     3. Started to drill out with same bit 4.8750 on 2.3750 tubing at approximately 96.6'
+
     3. Started to drill out with same bit 4.8750 on 2.3750 tubing at approximately 96.6  
  
     4. During drill out, at a depth of approximately 100', the well started to unload. The contractor  
+
     4. During drill out, at a depth of approximately 100, the well started to unload. The contractor  
 
       slowed their pump down to keep well under control, letting the well flow into half tank. The  
 
       slowed their pump down to keep well under control, letting the well flow into half tank. The  
 
       initial flow back produced approximately 100 gallons of a thick black oil and then changed to   
 
       initial flow back produced approximately 100 gallons of a thick black oil and then changed to   
Line 258: Line 469:
 
     5. I advised Whipstock crew to put a trap over half tank to keep the odor in.
 
     5. I advised Whipstock crew to put a trap over half tank to keep the odor in.
 
    
 
    
     6.The crew ran tubing to 225' and shut down for the day.
+
     6.The crew ran tubing to 225 and shut down for the day.
  
 
   END
 
   END
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 2139366242
 
| 2139366242
 
| 2014-03-07
 
| 2014-03-07
|  
+
| Orphan
| I conducted this follow-up inspection on 03/07/2014 for contract compliance.
+
| No Violations
 +
I conducted this follow-up inspection on 03/07/2014 for contract compliance.
  
 
   1.Confirmed that the half tank, to be used to contain flow back  from the plugging, was delivered.
 
   1.Confirmed that the half tank, to be used to contain flow back  from the plugging, was delivered.
   2. Tubing was run for first plug (1334' to 850') will cement with 110 sacks of Class A cement.
+
   2. Tubing was run for first plug (1334 to 850) will cement with 110 sacks of Class A cement.
   3. Gel will be from 850' to 400'.
+
   3. Gel will be from 850 to 400.
   4. Cement plug from 400' to surface with 160 sacks of Class A cement.
+
   4. Cement plug from 400 to surface with 160 sacks of Class A cement.
  
 
   END
 
   END
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -253263923
+
|}-->
| 2014-02-06
 
|
 
| Shut down due to subzero weather.
 
|
 
|
 
|
 
|-
 
|-
 
| -464544559
 
| 2014-03-03
 
|
 
| A follow-up inspection  was conducted on 03/03/2014 for contract compliance.
 
 
 
  1.Equipment freezing up due to the subzero weather.
 
 
 
  2. Started to clean out at 13:00 hrs, working on the obstruction at 60' using a 4.3750 tri cone bit. At first the circulating fluid was clear but then it turned to a blackish color. Drilled down to 76'.
 
 
 
  3. Circulating out large pieces of Red Bedford Shale, due to fresh water that is being used to circulate.
 
 
 
  4. Shut down for the day at 16:00 hrs.
 
 
 
    END
 
|
 
|
 
|
 
|-
 
|-
 
| -46932437
 
| 2014-02-13
 
|
 
| A follow-up inspection was conducted on 02/13/2014 for contract compliance.
 
 
 
  1. Excavating continues and contractor is placing the excavated clay
 
      material in the northwest stockpile.
 
 
 
  2. Sewer line was removed and the water is continuing to flow  from the
 
      gravel base of the sewer ditch.
 
 
 
 
 
    Note: Keeping Mark Bruce (ODNR Communication Department) apprised of
 
              progress at the site.
 
 
 
END
 
|
 
|
 
|
 
|-
 
|-
 
| -638603913
 
| 2014-02-11
 
|
 
| Visited location on 02/11/2014 with Norburt Lowder to check on status of excavation.  Whipstock Drilling is continuining to excavate down to wellhead.  At the time of the visit, they were at approximately 12' down from ground level.
 
|
 
|
 
|
 
|-
 
|-
 
| -64861059
 
| 2014-02-12
 
|
 
| Visited location on 02/12/2014 with Norburt Lowder to check on status of excavation operations and discuss plan forward.  At time of visit, Whipstock Drilling was excavating at approximately 15' below ground level.
 
|
 
|
 
|
 
|-
 
|-
 
| -849949934
 
| 2014-02-12
 
|
 
| A follow-up inspection was conducted on 02/12/2014 for contract compliance.
 
 
 
  1. A replacement pump arrived and was placed close to the vault so 
 
      the water can be pumped from it. Once the waterwas pumped out of the
 
      well vault and the casing was exposed, the gas leakage from the well
 
      diminished.  No gas was detected in excavation, however elevated gas
 
      readings were detected in the vault. 
 
 
 
  2. Whipstock completed excavation down to the sewer line (approximately
 
      18
 
|
 
|
 
|
 
|-
 
|-
 
| -964372000
 
| 2014-02-10
 
|
 
| Visited location on 02/10/2014 with Norburt Lowder to check-on status of excavation operations.  Whipstock Drilling excavating at approximately 6' below ground level to reach wellhead.
 
|
 
|
 
|
 
|-
 
|-
 
| 972176465
 
| 2014-02-15
 
|
 
|
 
RECORD OF CONVERSATION ON 02/15/2014
 
 
 
    Phone call received from Chris Corso (Whipstock) advising me they 
 
  excavated approximately 5
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 20:09, 24 July 2019

Well Details

Well ID: 34-093-60473
Loading map...
Country: United States
State: Ohio
County: Lorain
Municipality: Ridgeville Township
Operator Name: FJD PROPERTIES LLC
Well Pad ID:
Farm/Lease Name: FJD PROPERTIES LLC (WINCKLES)
License Status: Final Restoration
License Date: 2014-03-26
Spud Date: 1941-10-09
Spud Drilling Contractor:
Final Drill Date: 1941-11-06
Well Total Depth: 2478 ft
Configuration: Vertical
Latitude: 41.394510857
Longitude: -82.03979046

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1941-10-09 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
Completed 1941-11-06 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
Reached Total Depth 1941-11-06 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
Correction to Well 2007-09-28 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
Change of Owner 2014-01-13 Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM
APP 2014-01-17 Proposed Formations:SHALE, Issued Date:1/17/2014, Expired Date:1/17/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2014-02-12 Operator changed from 40004, COTTRELL AARON to 40005, FJD PROPERTIES LLC
Change of Owner 2014-02-12 Operator changed from 8318, ORPHAN WELL PROGRAM to 40004, COTTRELL AARON
Plugged by Orphan Well Program 2014-03-07 Plugged by Orphan Well Program
Plugged/Abandoned 2014-03-07 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
Construction Permit Expires 2016-01-17 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.
Record Last Modified 2017-02-10 UNCOVERED A LEAKING CLINTON GAS WELL 23' UNDERGROUND. CASING IS SURROUNDED BY CONCRETE. GAS IS LEAKING THRU CENTER OF CONCRETE AT 100% LEL. A NEW HOUSING DEVELOPMENT IN PROCESS AT TIME OF INPECTION OF 0/7/06. EXISTING GAS WELL WILL BE UNDER NEW ROAD,TAIL FEATHER DR. I&O CASE # 2006 10 052.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0046932437 2014-02-13 Orphan No Violations A follow-up inspection was conducted on 02/13/2014 for contract compliance.
  1.	Excavating continues and contractor is placing the excavated clay 
     material in the northwest stockpile.
  2.	Sewer line was removed and the water is continuing to flow  from the 
     gravel base of the sewer ditch.


   Note: Keeping Mark Bruce (ODNR Communication Department) apprised of 
              progress at the site. 

END

0064861059 2014-02-12 Plug / Plug Back No Violations Visited location on 02/12/2014 with Norburt Lowder to check on status of excavation operations and discuss plan forward. At time of visit, Whipstock Drilling was excavating at approximately 15 below ground level.
0253263923 2014-02-06 Orphan No Violations Shut down due to subzero weather.
0464544559 2014-03-03 Orphan No Violations A follow-up inspection was conducted on 03/03/2014 for contract compliance.
 1.Equipment freezing up due to the subzero weather.
 2. Started to clean out at 13:00 hrs, working on the obstruction at 60 using a 4.3750 tri cone bit. At first the circulating fluid was clear but then it turned to a blackish color. Drilled down to 76.
 3. Circulating out large pieces of Red Bedford Shale, due to fresh water that is being used to circulate.
 4. Shut down for the day at 16:00 hrs.
   END
0638603913 2014-02-11 Plug / Plug Back No Violations Visited location on 02/11/2014 with Norburt Lowder to check on status of excavation. Whipstock Drilling is continuining to excavate down to wellhead. At the time of the visit, they were at approximately 12 down from ground level.
0849949934 2014-02-12 Orphan No Violations A follow-up inspection was conducted on 02/12/2014 for contract compliance.
  1. A replacement pump arrived and was placed close to the vault so  
      the water can be pumped from it. Once the waterwas pumped out of the 
      well vault and the casing was exposed, the gas leakage from the well 
      diminished.  No gas was detected in excavation, however elevated gas 
      readings were detected in the vault.  
  2.	Whipstock completed excavation down to the sewer line (approximately 


  3.	The sewer contractors arrived to determine if the lines needed to be 
     removed or worked around it. They decided to remove it.


  END
0964372000 2014-02-10 Plug / Plug Back No Violations Visited location on 02/10/2014 with Norburt Lowder to check-on status of excavation operations. Whipstock Drilling excavating at approximately 6 below ground level to reach wellhead.
0972176465 2014-02-15 Orphan No Violations
RECORD OF CONVERSATION ON 02/15/2014
   Phone call received from Chris Corso (Whipstock) advising me they  
 collar. He also noted that marks were present on the casing that appeared to 
 be from the teeth of a large track hoe bucket.
    No work will be done on Sunday 02/16/2014.

   
  END
1157642099 2006-09-07 Orphan No Violations Case # I&O 06-004, Met with Chris Teater to locate leaking gas well on housing development property at 37000 Center Ridge Rd. in North Ridgeville. Located a concrete column 23 underground with gas bubbling thru center of concrete column at 100% lel.. There is casing inside concrete but not sure of diameter. From photos it is 5 casing and it is bent over in bottom of 60 corregated plastic pipe over well . Construction company located gas leaking during removal of trees. Concrete around well will have to be chipped away to determine casing size. No houses are around well location at this time but construction to begin in October 2006. Sun, 70 degrees.
1170796367 2008-08-06 Orphan No Violations I&O case # 06-004 Chris Teeter. Requested by Mike McCormac to inspect well site for orphan well program. Well is in a new development and houses are getting closer to well site since last materix evaluation. Well has increased in gas leakage to 100 % lel 5 above well. My recommendation would be to plug the well this fall, to eliminate costs, due to hazards near a house. Nearest home now is 500 in diameter. I am submitting a new matrix to Mike McCormac. Dry, sun, 85 degrees.
1193531815 2014-02-18 Plug / Plug Back No Violations Visited location 0n 02/18/2014 to check-on status of excavation operations and assist with filming of ODNR video with Norburt Lowder.
1306816129 2014-03-26 Final Restoration No Violations A follow-up inspection was conducted on 03/26/2014 for contract compliance.
   1)  This well is located in the next phase of a housing development of K. Hovnanian Homes. This well is on the south side of Tailfeather Drive, in the block of address 1088 to 1091. There is no paved street in this area yet. The housing contractor has installed the water and sewer main lines and several lateral lines.
1340797127 2012-06-22 Orphan No Violations On this inspection, I was uUnable to locate the well site.
1391692683 2014-02-03 Orphan No Violations Inspection on 02/03/2014 was conducted for contract compliance.
 1.  The snow was removed from the area to be excavated.
     Corso, Whipstock Superintendent, to put orange flagging on each fence post and KEEP OUT 
 3. Excavating was started around well vault (black culvert). The projected excavation will be 
 4. All excavated material will be stockpiled at the perimeter of the site. The first stockpile will be 
     located in the southwest corner.

   Note: 

    a.	The Sewer line, which had been installed by the developer of the complex, is located 
       approximately 10-15 to the south of the well vault and at a depth of 18.
        the north of well, will need to be removed to continue excavating.
   END
1392649672 2014-02-10 Orphan No Violations
A follow-up inspection; 02/10/2014 was conducted for contract compliance.
    
   1.Whipstock is still excavating and stockpiling this material at the northwest corner of the 
      location.  This material will be used to backfill the excavation.

    2.Water is entering the excavation from the gravel fill at the base of the sewer line. A
       dewatering ditch was excavated along southern edge of the excavation to direct the water
       to the sump which is located in the southwest corner of the excavation.
 END
1392779866 2014-02-13 Orphan No Violations Crews from Whipstock are in the process of excavating the existing overburden to allow access to the damaged remaining casing of the well. Work is ongoing and work at the wellhead will not take place until later in the week.
1393248892 2014-02-05 Orphan No Violations Shut down due to sudzero weather.
1393337156 2014-02-07 Orphan No Violations No on site inspection done on 02/07/2014.

Shut down due to subzero weather.

1394469632 2014-03-10 Orphan No Violations Plugging and abandonment operations are being completed. Cementing was completed on Friday 3/7/14. The cement is firm and set at a nominal 24 inches below the top of the casing collar. Whipstock crews indicated that the plan is to cut the casing off at 4 feet below the existing grade and install a short section of black, corrugated drain pipe around the well once the cap is welded on with ID#. I inspected both the cement in the casing and samples of the cement retained in cups. Both look firm and solid. No gas detected via meter. I collected a GPS location data as well as triangulation measurements from selected locations for future reference.
1395242127 2014-02-20 Orphan No Violations
  A follow-up inspection  was conducted on 02/20/2014 for contract compliance.
  
  
         1.	Sewer Contractors on site reinstalling the sewer line.


   END
1513686661 2014-02-04 Orphan No Violations
   A follow-up inspection was conducted on 02/04/2014 for contract compliance.
   


  2. The water line on the north side of the excavation, that was installed by the developer was 
      exposed.Whipstock contacted the developer to shut water off. 
      east and west sides of the excavation. 

Note:

      When Whipstock was excavating in the area of the sewer line, which was previously installed by 
    the developer, they encountered black material that appeared to be high in organic matter (corn 
    stalks, vegtation, tree limbs and roots). Whipstock segregated this material and stockpiled it in
    the southwest corner of the location. This material will not be used as back fill.
   END
1541231752 2014-03-20 Plug / Plug Back No Violations Visited well on 03/20/2014 to determine the status of the location at the request of Norburt Lowder. All rig-related equipment has been removed, and the location has been rough-graded. A 12 plastic culvert pipe is around the well, sticking out of the ground ~2. The water level within the pipe is down ~4 from the top of the pipe. Occasional bubbles were noted in the water in the pipe.
1608252901 2014-03-05 Plug / Plug Back No Violations Visited location on 03/05/2014 to observe plugging operations with Norburt Lowder. Whipstock Drilling had run in the hole with tubing to circulate out old oil in the hole. Will tag bottom with tubing and then prepare to plug out the well.
1739275544 2014-02-19 Orphan No Violations
  A follow-up inspection was conducted on 02/19/2014 for contract compliance.
   1.	Plugging equipment removed from site.
   2.	Excavation was backfilled and compacted in 8-10 lifts. 
   3.	Site is ready for the Sewer Contractor to reinstall the sewer lines.


END.

1894238965 2014-02-11 Orphan No Violations A follow-up inspection was conducted on 02/11/2014 for contract compliance.
 1.	Pump problems due to sub-zero weather.
 2.	Whipstock continues to excavate and this material is being stockpiled at the northwest perimeter.
  Note: 	Cody Bruce, of FJD/Hovnanian Homes, arrived on site. He inquired about how the 
excavation will be backfilled.  I advised him to contact Gene Chini, Orphan Well Manager,
with any questions.
1981808815 2015-12-31 Final Restoration No Violations Collecting photographic evidence of final restoration. Final restoration is approved.
2011015490 2014-03-04 Orphan No Violations A follow-up inspection on 03/04/2014 was conducted for contract compliance.
   1.Due subzero weather the equipment lines are freezing up.
   2. Whipstock order 2 load saltwater from Cargill to add to circulating half tank to keep water from 
       freezing. The salt water will help keep the Red Bedford from caving in on the  drill stem.
   3. Started to drill out with same bit 4.8750 on 2.3750 tubing at approximately 96.6 
   4. During drill out, at a depth of approximately 100, the well started to unload. The contractor 
     slowed their pump down to keep well under control, letting the well flow into half tank. The 
     initial flow back produced approximately 100 gallons of a thick black oil and then changed to   
     black water with a strong petroleum odor. I notified Asst Fire Chief Bement (cell 440-653-6362)
     of the odor and that he might get complaints from the area.
   5. I advised Whipstock crew to put a trap over half tank to keep the odor in.
 
   6.The crew ran tubing to 225 and shut down for the day.
 END
2139366242 2014-03-07 Orphan No Violations I conducted this follow-up inspection on 03/07/2014 for contract compliance.
  1.Confirmed that the half tank, to be used to contain flow back   from the plugging, was delivered.
  2. Tubing was run for first plug (1334 to 850) will cement with 110 sacks of Class A cement.
  3. Gel will be from 850 to 400.
  4. Cement plug from 400 to surface with 160 sacks of Class A cement.
  END

For data sources see[3]

References