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| State: Ohio | | State: Ohio | ||
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− | | County: | + | | County: <County> |
|- | |- | ||
| Municipality: | | Municipality: |
Well ID: 34-173-21213 | |
Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
License Status: | |
License Date: | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: | |
Latitude: N/A | |
Longitude: N/A |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2010-12-30 | Proposed Formations:TRENTON, Issued Date:12/30/2010, Expired Date:12/29/2012 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2011-04-27 | ACID | 15 | 2500 Gal | 0 | Universal Well Services Inc. | Intended on using 5000 gal in a 3 stage job but formation never appeared to react as anticipated. Breakdown pressure at 930psi. 2500gal was squeezed in but not at sufficient rate. Suspect poor perforations so planning to re-perforate in morning (Appalachian) then follow up w/ a 20% HCl solution. 5 min shut in pressure not available. Average rate to low, about .6 bbl/min. Displaced w/ 920 gal fresh water. |
2011-04-28 | ACID | 20 | 5000 Gal | 0 | Universal Well Services Inc. | Started with 20% HCl (2500gal) then switched to the remaining 15% HCl (2500 gal). 25 Balls total in 3 stages to seal perfs. Average rate was 1.3 bbl/ min. Displaced hole with 920 gal water when completed. Breakdown pressure occurred during event on previous day. Both owner and Universal happy with results. |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1821371431 | 2011-04-28 | Production Wells | No Violations | Universal performed a frac on well. |
For data sources see[4]