X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-121-23136"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-121-23136
 
| Well ID: 34-121-23136
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6035231919, -81.4940405001 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.60352319, -81.4940405 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Noble County, Ohio|Noble]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[NORTHWOOD ENERGY CORP]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1984-05-29
 
| Spud Date: 1984-05-29
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.6035231919
+
| Latitude: 39.60352319
 
|-
 
|-
| Longitude: -81.4940405001
+
| Longitude: -81.4940405
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 10522.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 16495.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 2141.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 5854.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 2091.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 994.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 2865.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 6.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 2127.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 2477.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 2372.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 2452.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 2458.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 2364.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 2272.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 1053.0
 +
|
 +
|
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 120.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 121.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 59.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 91.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 283:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -126321449
 
| -126321449
 
| 2004-03-23
 
| 2004-03-23
|
+
|  
 
| Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phot's indicate
 
| Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phot's indicate
 
H2S gas odor present.
 
H2S gas odor present.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1362360061
 
| 1362360061
 
| 2014-05-02
 
| 2014-05-02
|
+
|  
| My inspection today finds the service rig crew pulled the collar off of the 4.5" casing while trying to rip the pipe.  The cement crew was sent back.
+
| My inspection today finds the service rig crew pulled the collar off of the 4.5 casing while trying to rip the pipe.  The cement crew was sent back.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1399049324
 
| 1399049324
 
| 2014-05-01
 
| 2014-05-01
|
+
|  
 
| My inspection today finds Davis Well Service moved a rig onto the location.  The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042'.
 
| My inspection today finds Davis Well Service moved a rig onto the location.  The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042'.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1399309060
 
| 1399309060
 
| 2014-05-05
 
| 2014-05-05
|
+
|  
 
| My inspection today finds the casing was ripped at 3660'.  Cemenco circulated a 38 sk class A 2% gel plug.  The casing was pulled up to 1950'.  Cemenco circulated a 52 sk 2% gel plug into place.  A 200' 54 sk plug was placed from 200' to surface.  I instructed the company to reclaim the site in accordance with 1509.072.
 
| My inspection today finds the casing was ripped at 3660'.  Cemenco circulated a 38 sk class A 2% gel plug.  The casing was pulled up to 1950'.  Cemenco circulated a 52 sk 2% gel plug into place.  A 200' 54 sk plug was placed from 200' to surface.  I instructed the company to reclaim the site in accordance with 1509.072.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1668780202
 
| 1668780202
 
| 2014-07-02
 
| 2014-07-02
|
+
|  
 
| Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
 
| Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| PL7609
 
| PL7609
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 02:23, 16 July 2015

Well Details

Well ID: 34-121-23136
Loading map...
County: Noble
Municipality:
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-05-29
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.60352319
Longitude: -81.4940405

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 10522.0 0.0
1985-0 16495.0 0.0
1986-0 2141.0 0.0
1987-0 5854.0 0.0
1988-0 2091.0 0.0
1989-0 994.0 0.0
1990-0 2865.0 6.0
1991-0 2127.0 0.0
1992-0 2477.0 0.0
1993-0 2372.0 0.0
1994-0 2452.0 0.0
1995-0 2458.0 0.0
1996-0 2364.0 0.0
1997-0 2272.0 0.0
1998-0 1053.0
1999-0 120.0 0.0
2000-0 0.0 0.0
2001-0 0.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 121.0 0.0
2012-0 0.0 0.0
2013-0 0.0 59.0
2014-0 0.0 365.0 91.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-126321449 2004-03-23 Inspection revealed wel to be idle no I.D.posted 4x2 swedge on top valves shut as phot's indicate

H2S gas odor present.

1362360061 2014-05-02 My inspection today finds the service rig crew pulled the collar off of the 4.5 casing while trying to rip the pipe. The cement crew was sent back.
1399049324 2014-05-01 My inspection today finds Davis Well Service moved a rig onto the location. The rig crew ran the wire line tools in the well and found the top of the lime plug at 4042'.
1399309060 2014-05-05 My inspection today finds the casing was ripped at 3660'. Cemenco circulated a 38 sk class A 2% gel plug. The casing was pulled up to 1950'. Cemenco circulated a 52 sk 2% gel plug into place. A 200' 54 sk plug was placed from 200' to surface. I instructed the company to reclaim the site in accordance with 1509.072.
1668780202 2014-07-02 Site has met 1509.072B restoration requirements. There was no evidence of production equipment left behind.
PL7609 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.