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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-055-22108 | | Well ID: 34-055-22108 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.37655526, -81.10232038 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Geauga County, Ohio|Geauga]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[EXCALIBUR EXPLORATION INC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 2009-11-02 | | Spud Date: 2009-11-02 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.37655526 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.10232038 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 2661.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1045.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 4603.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1090.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 3128.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 618.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 2027.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 379.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 1517.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 334.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 112: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
| -1203125869 | | -1203125869 | ||
| 2014-09-02 | | 2014-09-02 | ||
− | | | + | | |
| My inspection found the well to be equipped with a pump jack. The annulus valve was plumbed into a pop off valve. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. | | My inspection found the well to be equipped with a pump jack. The annulus valve was plumbed into a pop off valve. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. | ||
− | + | | | |
− | + | | | |
− | + | | | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | | | ||
− | | | ||
− | | | ||
|- | |- | ||
|- | |- | ||
| 1257861114 | | 1257861114 | ||
| 2009-11-10 | | 2009-11-10 | ||
− | | | + | | |
| On site for surface cement. Operator ran surface casing with no issues. Requested 100% extra cement to be ran during job. Operator hung drill string on 11/05/09, had to use jars to loosen and remove drill string. Drill string freed on 11/09/2009. Operator went back in and reamed hole. Petroset cement company on site for cement job. Operator broke circulation, while switching over to start cement, fluid in the conductor was bubbling. Surface hole was gassing a minor amount. Instructed cementer to mix cement heavy at the end of the job. Petroset ran cement, 10BBL return of good cement to surface. Cement was static. Cement head started to leak at the end of job. Driller had cleaned threads on both the cement head and the landing joint. Cement head stopped leaking about 5 minutes after job was complete. | | On site for surface cement. Operator ran surface casing with no issues. Requested 100% extra cement to be ran during job. Operator hung drill string on 11/05/09, had to use jars to loosen and remove drill string. Drill string freed on 11/09/2009. Operator went back in and reamed hole. Petroset cement company on site for cement job. Operator broke circulation, while switching over to start cement, fluid in the conductor was bubbling. Surface hole was gassing a minor amount. Instructed cementer to mix cement heavy at the end of the job. Petroset ran cement, 10BBL return of good cement to surface. Cement was static. Cement head started to leak at the end of job. Driller had cleaned threads on both the cement head and the landing joint. Cement head stopped leaking about 5 minutes after job was complete. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1694825345 | | 1694825345 | ||
| 2013-04-29 | | 2013-04-29 | ||
− | | | + | | |
| My inspection found the well to be equipped with a pump jack. The annulus valve was plumbed into a pop off valve. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. | | My inspection found the well to be equipped with a pump jack. The annulus valve was plumbed into a pop off valve. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1734575133 | | 1734575133 | ||
| 2010-07-12 | | 2010-07-12 | ||
− | | | + | | |
| Lease road is stable and rocked to the tank battery. Turn around located at the tank battery. Well is a pump jack well. Annulus has a pop-off and needle gauge on it. Tank battery has one 210BBL tank, 100 BBL tank and an mechanical separator. Dike is in good repair. PVC drain pipe has been installed south east corner of the dike. Pipe has a riser and a screw in cap on it. Vegetation is established on location. Site is stable. Spacing is meets 1509 ORC. | | Lease road is stable and rocked to the tank battery. Turn around located at the tank battery. Well is a pump jack well. Annulus has a pop-off and needle gauge on it. Tank battery has one 210BBL tank, 100 BBL tank and an mechanical separator. Dike is in good repair. PVC drain pipe has been installed south east corner of the dike. Pipe has a riser and a screw in cap on it. Vegetation is established on location. Site is stable. Spacing is meets 1509 ORC. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 299531960 | | 299531960 | ||
| 2009-11-05 | | 2009-11-05 | ||
− | | | + | | |
| On site for surface cement. Operator was tripping out of the hole and got hung in the Berea. Operator was having issues with the Berea swelling. At the start of tripping out once the bit was hung operator could go down but not up, Berea then locked up, operator could not go in either directions. Operator did have and could maintain circulation. Operator attempted to turn drill pipe with tongs. Attempting to free drill pipe with tongs resulted in a twisted drill pipe. Operator was going rethink strategy to free hung drill pipe. Will contact when ready to cement surface casing. | | On site for surface cement. Operator was tripping out of the hole and got hung in the Berea. Operator was having issues with the Berea swelling. At the start of tripping out once the bit was hung operator could go down but not up, Berea then locked up, operator could not go in either directions. Operator did have and could maintain circulation. Operator attempted to turn drill pipe with tongs. Attempting to free drill pipe with tongs resulted in a twisted drill pipe. Operator was going rethink strategy to free hung drill pipe. Will contact when ready to cement surface casing. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -453817613 | ||
+ | | 2009-11-09 | ||
+ | | | ||
+ | | Operator has backed out 8 joints of drill pipe from hole. Operator was setting up drill collars with a set of jars to go in and retrieve the last 3 joints of drill string and bit. Pits were in good repair. Driller inquired if he could use caustics down hole to make the Berea Sandstone heave to release bit. Request to use caustics was denied. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -907144000 | ||
+ | | 2010-01-08 | ||
+ | | | ||
+ | | Annulus pressure report submitted by company. Long string cemented 11/20/09. 11/21/09 to 11/30/09 no recordable pressure readings. Well frac 12/02/09. 12/03/09 to 12/07/09 no readings. 12/07/09 annulus left open. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -908562975 | ||
+ | | 2009-11-04 | ||
+ | | | ||
+ | | Pits are in good repair. Lease road is stable, rocked to site. Silt fence has been installed at the entrance to the site and around affected area. Drill depth 200'. Operator is going to be shutting down to repair mud pump. Mud pump is leaking around site. Operator is drilling on fresh water mud. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-055-22108 | Loading map...
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County: Geauga | |
Municipality: | |
Operator Name: EXCALIBUR EXPLORATION INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2009-11-02 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.37655526 | |
Longitude: -81.10232038 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 2661.0 | 1045.0 | ||||
2011-0 | 4603.0 | 1090.0 | ||||
2012-0 | 3128.0 | 618.0 | ||||
2013-0 | 2027.0 | 379.0 | ||||
2014-0 | 1517.0 | 365.0 | 334.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1203125869 | 2014-09-02 | My inspection found the well to be equipped with a pump jack. The annulus valve was plumbed into a pop off valve. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. | ||||
1257861114 | 2009-11-10 | On site for surface cement. Operator ran surface casing with no issues. Requested 100% extra cement to be ran during job. Operator hung drill string on 11/05/09, had to use jars to loosen and remove drill string. Drill string freed on 11/09/2009. Operator went back in and reamed hole. Petroset cement company on site for cement job. Operator broke circulation, while switching over to start cement, fluid in the conductor was bubbling. Surface hole was gassing a minor amount. Instructed cementer to mix cement heavy at the end of the job. Petroset ran cement, 10BBL return of good cement to surface. Cement was static. Cement head started to leak at the end of job. Driller had cleaned threads on both the cement head and the landing joint. Cement head stopped leaking about 5 minutes after job was complete. | ||||
1694825345 | 2013-04-29 | My inspection found the well to be equipped with a pump jack. The annulus valve was plumbed into a pop off valve. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. | ||||
1734575133 | 2010-07-12 | Lease road is stable and rocked to the tank battery. Turn around located at the tank battery. Well is a pump jack well. Annulus has a pop-off and needle gauge on it. Tank battery has one 210BBL tank, 100 BBL tank and an mechanical separator. Dike is in good repair. PVC drain pipe has been installed south east corner of the dike. Pipe has a riser and a screw in cap on it. Vegetation is established on location. Site is stable. Spacing is meets 1509 ORC. | ||||
299531960 | 2009-11-05 | On site for surface cement. Operator was tripping out of the hole and got hung in the Berea. Operator was having issues with the Berea swelling. At the start of tripping out once the bit was hung operator could go down but not up, Berea then locked up, operator could not go in either directions. Operator did have and could maintain circulation. Operator attempted to turn drill pipe with tongs. Attempting to free drill pipe with tongs resulted in a twisted drill pipe. Operator was going rethink strategy to free hung drill pipe. Will contact when ready to cement surface casing. | ||||
-453817613 | 2009-11-09 | Operator has backed out 8 joints of drill pipe from hole. Operator was setting up drill collars with a set of jars to go in and retrieve the last 3 joints of drill string and bit. Pits were in good repair. Driller inquired if he could use caustics down hole to make the Berea Sandstone heave to release bit. Request to use caustics was denied. | ||||
-907144000 | 2010-01-08 | Annulus pressure report submitted by company. Long string cemented 11/20/09. 11/21/09 to 11/30/09 no recordable pressure readings. Well frac 12/02/09. 12/03/09 to 12/07/09 no readings. 12/07/09 annulus left open. | ||||
-908562975 | 2009-11-04 | Pits are in good repair. Lease road is stable, rocked to site. Silt fence has been installed at the entrance to the site and around affected area. Drill depth 200'. Operator is going to be shutting down to repair mud pump. Mud pump is leaking around site. Operator is drilling on fresh water mud. |
For data sources see[2]