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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-087-20206 | | Well ID: 34-087-20206 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 38. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 38.56525932, -82.48166146 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Lawrence County, Ohio|Lawrence]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[EQUITY OIL & GAS FUNDS IN]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 2009-09-17 | | Spud Date: 2009-09-17 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Final Restoration |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: 38. | + | | Latitude: 38.56525932 |
|- | |- | ||
− | | Longitude: -82. | + | | Longitude: -82.48166146 |
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|} | |} | ||
== Inspection Data == | == Inspection Data == | ||
Line 64: | Line 42: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | 114113799 | ||
+ | | 2009-12-17 | ||
+ | | | ||
+ | | Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection. | ||
+ | | | ||
+ | | | ||
+ | | Compliance Notice | ||
+ | |- | ||
+ | |- | ||
+ | | 114113799 | ||
+ | | 2009-12-17 | ||
+ | | | ||
+ | | Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection. | ||
+ | | | ||
+ | | | ||
+ | | Compliance Notice | ||
+ | |- | ||
+ | |- | ||
+ | | 114113799 | ||
+ | | 2009-12-17 | ||
+ | | | ||
+ | | Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection. | ||
+ | | | ||
+ | | | ||
+ | | Compliance Notice | ||
+ | |- | ||
|- | |- | ||
| -116531345 | | -116531345 | ||
| 2009-09-22 | | 2009-09-22 | ||
− | | | + | | |
− | | Rig pulled on 4.5 | + | | Rig pulled on 4.5 casing and it parted at 5' down hole. Directly above a collar. Rig down and move to # 207 while they excavate around 10 and cut off 10 to expose 4.5 collar. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1179704353 | | -1179704353 | ||
| 2007-07-18 | | 2007-07-18 | ||
− | | | + | | |
| I talked to John Murphy at 740-215-1011 at 1:00 pm on 7-18-07 about this well's status. John said that he sent a letter asking for an extension on the NOV to Joe Hoerst. John said that it is not cost effective to produce the well due to the low price that he is getting for gas right now. He also stated that it is hard to get a rig down there. I told John that I will follow up with Joe to see what action is taken. | | I talked to John Murphy at 740-215-1011 at 1:00 pm on 7-18-07 about this well's status. John said that he sent a letter asking for an extension on the NOV to Joe Hoerst. John said that it is not cost effective to produce the well due to the low price that he is getting for gas right now. He also stated that it is hard to get a rig down there. I told John that I will follow up with Joe to see what action is taken. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1199897804 | ||
+ | | 2008-01-08 | ||
+ | | | ||
+ | | Well is disconnected and idle. No production equipment is on site. The only work that has been done is the clearing of the brush around the wellhead. Well is leaking a small amount of gas. The Id is damaged and was face down in the mud. I moved the Id. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1238598205 | ||
+ | | 2009-02-26 | ||
+ | | | ||
+ | | Well has been swabbed by Craig Ross. Well is being monitored at this time. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1242061032 | ||
+ | | 2009-05-11 | ||
+ | | | ||
+ | | Talked to John Murphy 12:42pm. I informed him that the plug permit has been issued. John told me that they are writing a letter to outline the plug plans. He also said that they want to wait until July and plug 4 or 5 wells in Lawrence County. I told John to submit a written plan this week. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1260362792 | ||
+ | | 2009-09-09 | ||
+ | | | ||
+ | | I talked to John Murphy (Equity Oil & Gas) and he informed me that Knox will be moving a plug rig in this week. He wanted to review the plug depths and methods to plug with cement. He asked that I coordinate with Bill Mitton (Knox). I told John that would be fine. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1260374937 | ||
+ | | 2009-09-18 | ||
+ | | | ||
+ | | Run tubing to 2650'. Fluid at approximately 800'. Attempted to circulate water using 1/2 bag flake (12.5 lbs). Pumped a total of 86 bbls fluid. LCM material mixed with the 86bbls is 1.5 bags cotton seed hulls (45lbs each bag), 1 gallon polymer, 20 lbs flake (Total including the 12.5 lbs mentioned ) Did not achieve circulation. Water truck had mechanical problems had to be repaired on site. After repairs another 68 bbls was pumped in effort to achieve circulation. John Murphy decided to pump cement plug. Pumped 500' cement plug from 2650' to 2150'. After plug pumped tubing was pulled. Fluid level could be seen on tubing at 460'. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -1438869994 | | -1438869994 | ||
| 2006-01-27 | | 2006-01-27 | ||
− | | | + | | |
| FOLLOW UP TO NOV # -453435440 Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head. | | FOLLOW UP TO NOV # -453435440 Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1472342804 | | -1472342804 | ||
| 2007-09-12 | | 2007-09-12 | ||
− | | | + | | |
| Called and left a message for John Murphy Re: Well is disconnected and idle. No work has been done to the well. I asked for a update on the well status and asked for a return phone call. | | Called and left a message for John Murphy Re: Well is disconnected and idle. No work has been done to the well. I asked for a update on the well status and asked for a return phone call. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1530333138 | | -1530333138 | ||
| 2009-09-17 | | 2009-09-17 | ||
− | | | + | | |
| Knox plug rig moving on location from #207. Ran tools to 2758'. | | Knox plug rig moving on location from #207. Ran tools to 2758'. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1612389942 | | -1612389942 | ||
| 2007-07-13 | | 2007-07-13 | ||
− | | | + | | |
| I called John Murphy 740-215-1011 on 7-13-07 at 7:58am and left a voice mail about his NOV's for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged. | | I called John Murphy 740-215-1011 on 7-13-07 at 7:58am and left a voice mail about his NOV's for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1726523897 | | -1726523897 | ||
| 2007-07-10 | | 2007-07-10 | ||
− | | | + | | |
| I called John Murphy 740-215-1011 on 7-10-07 at 1:14pm and left a voice mail about his NOV's for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged. | | I called John Murphy 740-215-1011 on 7-10-07 at 1:14pm and left a voice mail about his NOV's for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1858224102 | ||
+ | | 2009-09-21 | ||
+ | | | ||
+ | | TD TOC plug at 2450'. Pumped cement plug from 2450' to 2150' used 28 sacks cement. Brian Jasper (Formation Cementing) pumped the plug. I was unable to witness the plug. I arrived on location after plug set and tubing pulled. Brian did not give me a cement ticket. He told me that he wants to add it to the next days ticket. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2016145019 | ||
+ | | 2009-09-30 | ||
+ | | | ||
+ | | Measure TOC plug at 20'. Top off with sack cement. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2064754156 | ||
+ | | 2009-01-14 | ||
+ | | | ||
+ | | Talked to Craig Ross (Contractor) he is going to the well today to test for pressure and to look at the well. He told me that he will have his rig on location in 2 weeks to start swabbing and evaluating the well. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -2072987963 | | -2072987963 | ||
| 2009-09-28 | | 2009-09-28 | ||
− | | | + | | |
− | | Run tubing back to 1918'. Cement plug fell. Was able to achieve circulation to the surface. On both the inside and outside of the 4.5 | + | | Run tubing back to 1918'. Cement plug fell. Was able to achieve circulation to the surface. On both the inside and outside of the 4.5 casing. A piece of wooden 4 by 4 by 24 was circulated to the surface from the backside of the 4.5 casing along with some oil and water. Pumped cement plug from 1918' to 1500'. Rip 4.5 at 1480'. Pull 2 joints, pump gel spacer and circulate. Then pull 1 joint and circulate to surface. Pump a 600' plug. Pull 10 joints to clear cement and then pull 3 more and shut down. Haul 1 load pit water to injection well. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -293415005 | | -293415005 | ||
| 2007-08-21 | | 2007-08-21 | ||
− | | | + | | |
| Well is disconnected and idle. No work has been done to the well. | | Well is disconnected and idle. No work has been done to the well. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -31373732 | | -31373732 | ||
| 2009-11-04 | | 2009-11-04 | ||
− | | | + | | |
| Pit is filled in. Site graded. Seed and mulch applied. Vegetative growth is starting. | | Pit is filled in. Site graded. Seed and mulch applied. Vegetative growth is starting. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 432323847 | ||
+ | | 2007-04-17 | ||
+ | | | ||
+ | | Well is idle. Well is not connected to any production equipment or pipe line. Id is fadded no emergency company phone numbers. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -453435440 | | -453435440 | ||
| 2006-01-27 | | 2006-01-27 | ||
− | | | + | | |
| Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head. | | Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -458756012 | | -458756012 | ||
| 2009-09-24 | | 2009-09-24 | ||
− | | | + | | |
− | | Rip 4.5 | + | | Rip 4.5 casing at 1918' Casing not free, Run tubing to 1918'. Pump cement plug from 1918' to 1718'. Unable to circulate. Plug pumped through tubing. Wait and tag TOC plug before continuing. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 608509602 | ||
+ | | 2009-09-29 | ||
+ | | | ||
+ | | Tried to pump on 4.5 it locked up. 4.5 full of water. Pressured up to 800psi. Ran tools down inside 4.5 tools sat down at 490'. Pulling all 4.5 out of hole. Then run tubing back down. 5 joints of 4.5 have cement in them. Tubing ran to 700' and tag TOC plug. Pump gel and circulate to surface. Pump 300' plug pull tubing to 400' circulate hole to surface. Pump another 300' plug. Pull tubing to 100' circulate to surface. Pump 100' to surface. Top off with cement hose. Cement stayed at surface. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -717012640 | | -717012640 | ||
| 2009-02-10 | | 2009-02-10 | ||
− | | | + | | |
| Craig Ross has his swab rig on the well and they are swabbing now. They are making a lot of water. John Murphy (Well owner) has not decided if going to plug or produce the well. | | Craig Ross has his swab rig on the well and they are swabbing now. They are making a lot of water. John Murphy (Well owner) has not decided if going to plug or produce the well. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 823393498 | ||
+ | | 2014-12-31 | ||
+ | | | ||
+ | | Preliminary restoration requirements met. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -845116638 | | -845116638 | ||
| 2008-08-18 | | 2008-08-18 | ||
− | | | + | | |
| I showed Craig Ross (contractor for Murphy Oil) the location of the well and discussed the NOV and that they need to get a correct id on the well and then the well needs to be capable of production or plugged. The well is not connected to any lines. No lines have been ran to the well. The valves are corroded shut. A small amount of gas is leaking from the well. The well is located in a hay field and has easy access from the road. | | I showed Craig Ross (contractor for Murphy Oil) the location of the well and discussed the NOV and that they need to get a correct id on the well and then the well needs to be capable of production or plugged. The well is not connected to any lines. No lines have been ran to the well. The valves are corroded shut. A small amount of gas is leaking from the well. The well is located in a hay field and has easy access from the road. | ||
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|- | |- | ||
|- | |- | ||
| -926806558 | | -926806558 | ||
| 2008-12-29 | | 2008-12-29 | ||
− | | | + | | |
− | | No identification. Wellhead is disconnected. 4 | + | | No identification. Wellhead is disconnected. 4 casing has a valve that is closed but leaking a small amount of gas through the valve. No pipe line or production equipment is on location. The well is located off a township road and is in a hay field. |
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|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-087-20206 | Loading map...
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County: Lawrence | |
Municipality: | |
Operator Name: EQUITY OIL & GAS FUNDS IN | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2009-09-17 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 38.56525932 | |
Longitude: -82.48166146 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
114113799 | 2009-12-17 | Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection. | Compliance Notice | |||
114113799 | 2009-12-17 | Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection. | Compliance Notice | |||
114113799 | 2009-12-17 | Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection. | Compliance Notice | |||
-116531345 | 2009-09-22 | Rig pulled on 4.5 casing and it parted at 5' down hole. Directly above a collar. Rig down and move to # 207 while they excavate around 10 and cut off 10 to expose 4.5 collar. | ||||
-1179704353 | 2007-07-18 | I talked to John Murphy at 740-215-1011 at 1:00 pm on 7-18-07 about this well's status. John said that he sent a letter asking for an extension on the NOV to Joe Hoerst. John said that it is not cost effective to produce the well due to the low price that he is getting for gas right now. He also stated that it is hard to get a rig down there. I told John that I will follow up with Joe to see what action is taken. | ||||
1199897804 | 2008-01-08 | Well is disconnected and idle. No production equipment is on site. The only work that has been done is the clearing of the brush around the wellhead. Well is leaking a small amount of gas. The Id is damaged and was face down in the mud. I moved the Id. | ||||
1238598205 | 2009-02-26 | Well has been swabbed by Craig Ross. Well is being monitored at this time. | ||||
1242061032 | 2009-05-11 | Talked to John Murphy 12:42pm. I informed him that the plug permit has been issued. John told me that they are writing a letter to outline the plug plans. He also said that they want to wait until July and plug 4 or 5 wells in Lawrence County. I told John to submit a written plan this week. | ||||
1260362792 | 2009-09-09 | I talked to John Murphy (Equity Oil & Gas) and he informed me that Knox will be moving a plug rig in this week. He wanted to review the plug depths and methods to plug with cement. He asked that I coordinate with Bill Mitton (Knox). I told John that would be fine. | ||||
1260374937 | 2009-09-18 | Run tubing to 2650'. Fluid at approximately 800'. Attempted to circulate water using 1/2 bag flake (12.5 lbs). Pumped a total of 86 bbls fluid. LCM material mixed with the 86bbls is 1.5 bags cotton seed hulls (45lbs each bag), 1 gallon polymer, 20 lbs flake (Total including the 12.5 lbs mentioned ) Did not achieve circulation. Water truck had mechanical problems had to be repaired on site. After repairs another 68 bbls was pumped in effort to achieve circulation. John Murphy decided to pump cement plug. Pumped 500' cement plug from 2650' to 2150'. After plug pumped tubing was pulled. Fluid level could be seen on tubing at 460'. | ||||
-1438869994 | 2006-01-27 | FOLLOW UP TO NOV # -453435440 Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head. | ||||
-1472342804 | 2007-09-12 | Called and left a message for John Murphy Re: Well is disconnected and idle. No work has been done to the well. I asked for a update on the well status and asked for a return phone call. | ||||
-1530333138 | 2009-09-17 | Knox plug rig moving on location from #207. Ran tools to 2758'. | ||||
-1612389942 | 2007-07-13 | I called John Murphy 740-215-1011 on 7-13-07 at 7:58am and left a voice mail about his NOV's for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged. | ||||
-1726523897 | 2007-07-10 | I called John Murphy 740-215-1011 on 7-10-07 at 1:14pm and left a voice mail about his NOV's for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged. | ||||
1858224102 | 2009-09-21 | TD TOC plug at 2450'. Pumped cement plug from 2450' to 2150' used 28 sacks cement. Brian Jasper (Formation Cementing) pumped the plug. I was unable to witness the plug. I arrived on location after plug set and tubing pulled. Brian did not give me a cement ticket. He told me that he wants to add it to the next days ticket. | ||||
2016145019 | 2009-09-30 | Measure TOC plug at 20'. Top off with sack cement. | ||||
2064754156 | 2009-01-14 | Talked to Craig Ross (Contractor) he is going to the well today to test for pressure and to look at the well. He told me that he will have his rig on location in 2 weeks to start swabbing and evaluating the well. | ||||
-2072987963 | 2009-09-28 | Run tubing back to 1918'. Cement plug fell. Was able to achieve circulation to the surface. On both the inside and outside of the 4.5 casing. A piece of wooden 4 by 4 by 24 was circulated to the surface from the backside of the 4.5 casing along with some oil and water. Pumped cement plug from 1918' to 1500'. Rip 4.5 at 1480'. Pull 2 joints, pump gel spacer and circulate. Then pull 1 joint and circulate to surface. Pump a 600' plug. Pull 10 joints to clear cement and then pull 3 more and shut down. Haul 1 load pit water to injection well. | ||||
-293415005 | 2007-08-21 | Well is disconnected and idle. No work has been done to the well. | ||||
-31373732 | 2009-11-04 | Pit is filled in. Site graded. Seed and mulch applied. Vegetative growth is starting. | ||||
432323847 | 2007-04-17 | Well is idle. Well is not connected to any production equipment or pipe line. Id is fadded no emergency company phone numbers. | ||||
-453435440 | 2006-01-27 | Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head. | ||||
-458756012 | 2009-09-24 | Rip 4.5 casing at 1918' Casing not free, Run tubing to 1918'. Pump cement plug from 1918' to 1718'. Unable to circulate. Plug pumped through tubing. Wait and tag TOC plug before continuing. | ||||
608509602 | 2009-09-29 | Tried to pump on 4.5 it locked up. 4.5 full of water. Pressured up to 800psi. Ran tools down inside 4.5 tools sat down at 490'. Pulling all 4.5 out of hole. Then run tubing back down. 5 joints of 4.5 have cement in them. Tubing ran to 700' and tag TOC plug. Pump gel and circulate to surface. Pump 300' plug pull tubing to 400' circulate hole to surface. Pump another 300' plug. Pull tubing to 100' circulate to surface. Pump 100' to surface. Top off with cement hose. Cement stayed at surface. | ||||
-717012640 | 2009-02-10 | Craig Ross has his swab rig on the well and they are swabbing now. They are making a lot of water. John Murphy (Well owner) has not decided if going to plug or produce the well. | ||||
823393498 | 2014-12-31 | Preliminary restoration requirements met. | ||||
-845116638 | 2008-08-18 | I showed Craig Ross (contractor for Murphy Oil) the location of the well and discussed the NOV and that they need to get a correct id on the well and then the well needs to be capable of production or plugged. The well is not connected to any lines. No lines have been ran to the well. The valves are corroded shut. A small amount of gas is leaking from the well. The well is located in a hay field and has easy access from the road. | ||||
-926806558 | 2008-12-29 | No identification. Wellhead is disconnected. 4 casing has a valve that is closed but leaking a small amount of gas through the valve. No pipe line or production equipment is on location. The well is located off a township road and is in a hay field. |
For data sources see[1]