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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-067-21313 | | Well ID: 34-067-21313 | ||
| + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.22483263, -81.17852898 | width=100% | height=100% }} | ||
|- | |- | ||
| − | | County: | + | | County: [[Harrison County, Ohio|Harrison]] |
|- | |- | ||
| − | | Municipality: | + | | Municipality: |
|- | |- | ||
| − | | Operator Name: | + | | Operator Name: [[AMERICAN ENERGY UTICA LLC]] |
|- | |- | ||
| − | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
| − | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
| − | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
| − | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| − | | Spud Date: | + | | Spud Date: 2014-04-08 |
|- | |- | ||
| − | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
| − | | | + | | Configuration: Vertical |
|- | |- | ||
| − | | | + | | Well Status: Well Drilled |
|- | |- | ||
| − | | Violations: | + | | Violations: 0 |
|- | |- | ||
| − | | Latitude: | + | | Latitude: 40.22483263 |
|- | |- | ||
| − | | Longitude: | + | | Longitude: -81.17852898 |
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|} | |} | ||
== Inspection Data == | == Inspection Data == | ||
| Line 63: | Line 42: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
| − | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
| 1397071165 | | 1397071165 | ||
| 2014-04-09 | | 2014-04-09 | ||
| − | | | + | | |
| − | | I am on site today to witness the running and cementing of the 20 | + | | I am on site today to witness the running and cementing of the 20 inch diameter casing string. Express Drilling drilled a 26 inch diameter hole to 105 ft and set 105 ft of casing. Express Cementing Service cemented with 200 sacks of class A cement at 15.6 lbs and 1.20 yield . Circulate 9 bbls of cement to surface. |
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|- | |- | ||
| 1404958373 | | 1404958373 | ||
| 2014-07-07 | | 2014-07-07 | ||
| − | | | + | | |
| − | | I am on site tonight to witness the rnnning and the cementing of the 9-5/ | + | | I am on site tonight to witness the rnnning and the cementing of the 9-5/8inch diameter casing string. Patterson Drilling has casing at 7100 ft and is trying to wash casing to bottom. They could not get casing to total depth and will cement it where it is. They will circulate bottoms up 1.5 times and then rig up to cement. They are to call me at that time. |
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|- | |- | ||
| 1405002816 | | 1405002816 | ||
| 2014-07-09 | | 2014-07-09 | ||
| − | | | + | | |
| − | | I arrived today to find that Patterson Drilling Rig # 256 was not able to wash casing down. They have the 13-3/8 | + | | I arrived today to find that Patterson Drilling Rig # 256 was not able to wash casing down. They have the 13-3/8 inch diameter casing at 7095 ft. O-Tex Cementing service cemented with 1340 sacks of lead cement at 12.0 lbs and a yield of 2.15 tail cement of 210 aacks of class H cement at 15.3 lbs and a yield of 1.27. Next the D.V.Tool at 3610 ft was pumped open and all of the cement was circulated out of the annulus to surface. They will continue to circulate for 6 more hours and then will cement again to surface. |
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|- | |- | ||
| 1406199699 | | 1406199699 | ||
| 2014-07-23 | | 2014-07-23 | ||
| − | | | + | | |
| On the date of inspection I checked in with American Energy Utica, LLC Company Man Burl Miller. The Patterson 256 rig was at a Total Depth of 14,880 feet. 5.5 inch casing was seated on bottom within a 8.75 inch open hole up to 7,102 feet. I was present on site to witness the beginning stages of production casing cementing. | | On the date of inspection I checked in with American Energy Utica, LLC Company Man Burl Miller. The Patterson 256 rig was at a Total Depth of 14,880 feet. 5.5 inch casing was seated on bottom within a 8.75 inch open hole up to 7,102 feet. I was present on site to witness the beginning stages of production casing cementing. | ||
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|- | |- | ||
| 406367132 | | 406367132 | ||
| 2014-07-10 | | 2014-07-10 | ||
| − | | | + | | |
| I am on site today to witness the 2nd stage of a two stage cement job. The first stage used 1340 sacks of class H cement at 12 lb and a yield of 2.15 for the lead cement. A tail cement of class H at 15.3 lb and a yield of 1.27 with a total of 210 sacks. After the cement was displaced a ball was dropped to open the DV Tool which is at 3610 ft. All of the cement in the annular space was circulated to surface. Circulation continued for 6 hours and then the 2nd stage filled the annular space from 3610 ft to surface. O-Tex Cementing Service used class H cement at 12 lb and a yield of 2.15 a total of 740 sacks was used. 74 bbls of cement circulated to surface. The plug was bumped at 500 PSI over displacement pressure and held when released. | | I am on site today to witness the 2nd stage of a two stage cement job. The first stage used 1340 sacks of class H cement at 12 lb and a yield of 2.15 for the lead cement. A tail cement of class H at 15.3 lb and a yield of 1.27 with a total of 210 sacks. After the cement was displaced a ball was dropped to open the DV Tool which is at 3610 ft. All of the cement in the annular space was circulated to surface. Circulation continued for 6 hours and then the 2nd stage filled the annular space from 3610 ft to surface. O-Tex Cementing Service used class H cement at 12 lb and a yield of 2.15 a total of 740 sacks was used. 74 bbls of cement circulated to surface. The plug was bumped at 500 PSI over displacement pressure and held when released. | ||
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|- | |- | ||
| 4477858 | | 4477858 | ||
| 2014-07-25 | | 2014-07-25 | ||
| − | | | + | | |
| Patterson Drilling Rig # 256 is done with this well and will move to the # 8 H well next. They will spud today and be ready to set surface Friday late or early Sat. | | Patterson Drilling Rig # 256 is done with this well and will move to the # 8 H well next. They will spud today and be ready to set surface Friday late or early Sat. | ||
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|- | |- | ||
| 893852478 | | 893852478 | ||
| 2014-07-09 | | 2014-07-09 | ||
| − | | | + | | |
| − | | I am on site today to check on the drilling status of Patterson Drilling Rig # 256 and found that they are at 6580 ft drilling a 12-1/4 | + | | I am on site today to check on the drilling status of Patterson Drilling Rig # 256 and found that they are at 6580 ft drilling a 12-1/4 inch diameter hole. They will be ready to set casing tonight. |
| − | | | + | | |
| − | | | + | | |
| − | | | + | | |
|- | |- | ||
|} | |} | ||
| + | For data sources see<ref>{{cite web | ||
| + | | title = Ohio Department of Natural Resources RBDMS | ||
| + | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
| + | | date = 2015-06-19 | ||
| + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
| + | | accessdate = 2015-06-20 }}</ref> | ||
| + | == References == | ||
| + | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] | ||
| Well ID: 34-067-21313 | Loading map...
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| County: Harrison | |
| Municipality: | |
| Operator Name: AMERICAN ENERGY UTICA LLC | |
| Well Pad ID: | |
| Farm/Lease Name: | |
| First Permit Date: | |
| Last Permit Date: | |
| Spud Date: 2014-04-08 | |
| Unconventional: No | |
| Configuration: Vertical | |
| Well Status: Well Drilled | |
| Violations: 0 | |
| Latitude: 40.22483263 | |
| Longitude: -81.17852898 |
| INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
|---|---|---|---|---|---|---|
| 1397071165 | 2014-04-09 | I am on site today to witness the running and cementing of the 20 inch diameter casing string. Express Drilling drilled a 26 inch diameter hole to 105 ft and set 105 ft of casing. Express Cementing Service cemented with 200 sacks of class A cement at 15.6 lbs and 1.20 yield . Circulate 9 bbls of cement to surface. | ||||
| 1404958373 | 2014-07-07 | I am on site tonight to witness the rnnning and the cementing of the 9-5/8inch diameter casing string. Patterson Drilling has casing at 7100 ft and is trying to wash casing to bottom. They could not get casing to total depth and will cement it where it is. They will circulate bottoms up 1.5 times and then rig up to cement. They are to call me at that time. | ||||
| 1405002816 | 2014-07-09 | I arrived today to find that Patterson Drilling Rig # 256 was not able to wash casing down. They have the 13-3/8 inch diameter casing at 7095 ft. O-Tex Cementing service cemented with 1340 sacks of lead cement at 12.0 lbs and a yield of 2.15 tail cement of 210 aacks of class H cement at 15.3 lbs and a yield of 1.27. Next the D.V.Tool at 3610 ft was pumped open and all of the cement was circulated out of the annulus to surface. They will continue to circulate for 6 more hours and then will cement again to surface. | ||||
| 1406199699 | 2014-07-23 | On the date of inspection I checked in with American Energy Utica, LLC Company Man Burl Miller. The Patterson 256 rig was at a Total Depth of 14,880 feet. 5.5 inch casing was seated on bottom within a 8.75 inch open hole up to 7,102 feet. I was present on site to witness the beginning stages of production casing cementing. | ||||
| 406367132 | 2014-07-10 | I am on site today to witness the 2nd stage of a two stage cement job. The first stage used 1340 sacks of class H cement at 12 lb and a yield of 2.15 for the lead cement. A tail cement of class H at 15.3 lb and a yield of 1.27 with a total of 210 sacks. After the cement was displaced a ball was dropped to open the DV Tool which is at 3610 ft. All of the cement in the annular space was circulated to surface. Circulation continued for 6 hours and then the 2nd stage filled the annular space from 3610 ft to surface. O-Tex Cementing Service used class H cement at 12 lb and a yield of 2.15 a total of 740 sacks was used. 74 bbls of cement circulated to surface. The plug was bumped at 500 PSI over displacement pressure and held when released. | ||||
| 4477858 | 2014-07-25 | Patterson Drilling Rig # 256 is done with this well and will move to the # 8 H well next. They will spud today and be ready to set surface Friday late or early Sat. | ||||
| 893852478 | 2014-07-09 | I am on site today to check on the drilling status of Patterson Drilling Rig # 256 and found that they are at 6580 ft drilling a 12-1/4 inch diameter hole. They will be ready to set casing tonight. |
For data sources see[1]