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Difference between revisions of "37-115-20496"

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| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.716958, -75.686247 | width=100% | height=100% }}  
 
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.716958, -75.686247 | width=100% | height=100% }}  
 
|-
 
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| County: [[wikipedia:Susquehanna County, Pennsylvania|Susquehanna]]
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| County: [[Susquehanna County, Pennsylvania|Susquehanna]]
 
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| Municipality: [[wikipedia:Lenox Township, Susquehanna County, Pennsylvania|Lenox Township]]
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| Municipality: [[Lenox Township, Susquehanna County, Pennsylvania|Lenox Township]]
 
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| Operator Name: [[wikipedia:CABOT OIL & GAS CORP|CABOT OIL & GAS CORP]]
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| Operator Name: [[CABOT OIL & GAS CORP|CABOT OIL & GAS CORP]]
 
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| Farm/Lease Name: STALTER 2
 
| Farm/Lease Name: STALTER 2

Revision as of 20:05, 4 May 2014

Well Details

Well ID: 115-20496
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County: Susquehanna
Municipality: Lenox Township
Operator Name: CABOT OIL & GAS CORP
Farm/Lease Name: STALTER 2
First Permit Date: 2011-02-07
Last Permit Date: 2011-02-07
Spud Date: 2010-04-11
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 41.716958
Longitude: -75.686247

Well Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1984074 2011-06-27 No Violations Noted Pioneer 63. Attempted to cement 9 5/8". Could not get plug to burst. Pressured up to 4500 psi. Pipe filled with @140 sks cement. Will drill out dement with 8 3/4 PDC bit, and then re-cement pipe. Operator to call DEP when re-cementing casing.
1987236 2011-07-12 No Violations Noted Pioneer 63. Currently drilling on mud in lateral. Drilled on air to 6664'. No misting, soap, or defoamer used during process so far. Initial string of 9 5/8" was pulled, and a new string was installed. Drillers log on site and up to date. Follow up on report of cracked casing complaint. reported downhole issues thus far on well. No violations observed.
2000341 2011-08-16 Pending Inspected cellar of well. Approx. 1- 1 1/2' of fluid in cellar. Observed small consisten bubbling coming to surface approx 6" from well head. Operator called for pump turck to remove fluid from cellar. Steve Watson and Ryan Klemish returned to site @14:10. Pumped down cellar bubbling appears to be leaking from weld o hanger/conductor. Requested to install gauges on 2H well 20 x13 3/8" and will monitor pressures as part of investigation.
2009308 2011-10-05 No Violations Noted DEP on site @ 11:45. Follow up on status of well as part of onging gas migration investigation. Well is shut in. Well has not been fracced. Vents are open and vented to poly tank. No bubbling observed in cellar. Fluid level below tops of casing strings. No personnel or activity on site. DEP off site at 11:55.
2027836 2011-12-08 No Violations Noted No activity on site. Well is currently shut in. Backsides vented to poly tank. Approcximately 1' of water in cellar. No visual signs of bubbling in cellar. Bank of frac tanks on pad. Entrance in gated.
2059461 2012-04-13 No Violations Noted No activity on site. Well is not online. 13x9" and 9 x 5" vented to poly tank. Gauge on production reads 0 psi. No bubbling observed in cellar.
2106818 2012-09-25 No Violations Noted On site to perform 72 hour shut in on annular spaces of all wells on pad. DEP - Steve WAtson and Andrea Schmid on site with flow meter. Cabot on site to facilitate data collection and install digital pressure recorders on all annuli. Reading on Stalter 2H at time of inspection: 9 5/8" x 13 3/8" = 0 psi with digital gauge and O flow detected with 1/8" plate. 9 5/8" x 5 1/2" annulus showed 0 psi on digital gauge, and 0 flow with 1/8" plate.
2106876 2012-09-28 No Violations Noted On site to complete 72 hour shut in test. Started test on 9/25/12. shut in 13 x9" and 9 x 5" annuli. Cabot installed digital pressure recorders on each vent. Pressure readings were collected just before ending test. Readings were= 13 x 9" was 2.9 psi. 9 x 5" was 79.8 psi. Cabot disconnected recorders and will submit data to DEP. Also collected data from Stalter 1H and 8V.
2135086 2013-01-24 No Violations Noted Met Mr. Edward Lorenzo on site - Co. Man. Currently rigging up to drill out frac plugs and flow back. Will flowback while drilling out plugs so will not require flaring. Pressures on backside are 0 psi. Secondary containment in place. No violations observed.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2011-1 DRILL CUTTINGS 317.6 Tons LANDFILL 101247 KEYSTONE SANITARY LANDFILL DUNMORE PA
2011-2 DRILL CUTTINGS 535.54 Tons LANDFILL 101247 KEYSTONE SANITARY LANDFILL DUNMORE PA
2011-2 DRILL CUTTINGS 0.92 Tons LANDFILL 101534 LAUREL HIGHLANDS LANDFILL JOHNSTOWN PA
2011-2 DRILLING FLUID WASTE 324.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE OF BRINE TO FRAC A WELL
2011-2 DRILL CUTTINGS 741.07 Tons LANDFILL THR029 TUNNELL HILL RECLAMATION LANDFILL NEWLEXINGTON OH