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34-127-27223

Well Details

Well ID: 34-127-27223
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Country: United States
State: Ohio
County: Perry
Municipality: Thorn Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: SWISHER PAUL
License Status: Producing
License Date: 1999-09-08
Spud Date: 1999-12-14
Spud Drilling Contractor: FMS DRILLING
Final Drill Date: 1999-12-28
Well Total Depth: 4443.00 ft
Configuration: Vertical
Latitude: 39.910000
Longitude: -82.450000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 1999-09-08 Proposed Formations:CLINTON/ROSE RUN, Issued Date:9/8/99, Expired Date:9/7/00 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 1999-12-14 RBDMS Rec
Completed 1999-12-28 RBDMS Rec
Plugged Back 1999-12-28 RBDMS Rec
Reached Total Depth 1999-12-28 RBDMS Rec
Construction Permit Expires 2000-09-07 RBDMS Rec
Completion Report Received 2001-07-16 RBDMS Rec
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2001-09-14 2432 2444 18
2432 2444 18
2432 2444 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1500 Bbl 30000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2000 HOPEWELL OIL & GAS DEVELOPMENT 0.00 0.00 180
2001 HOPEWELL OIL & GAS DEVELOPMENT 2166.00 0.00 365
2002 HOPEWELL OIL & GAS DEVELOPMENT 2275.00 0.00 365
2003 HOPEWELL OIL & GAS DEVELOPMENT 1983.00 0.00 365
2004 HOPEWELL OIL & GAS DEVELOPMENT 2192.00 0.00 365
2005 HOPEWELL OIL & GAS DEVELOPMENT 1815.00 0.00 365
2006 HOPEWELL OIL & GAS DEVELOPMENT 1807.00 0.00 365
2007 HOPEWELL OIL & GAS DEVELOPMENT 1487.00 0.00 0
2008 HOPEWELL OIL & GAS DEVELOPMENT 1287.00 0.00 365
2009 HOPEWELL OIL & GAS DEVELOPMENT 1565.00 0.00 365
2010 HOPEWELL OIL & GAS DEVELOPMENT 1833.00 0.00 0
2011 HOPEWELL OIL & GAS DEVELOPMENT 1145.00 0.00 0
2012 HOPEWELL OIL & GAS DEVELOPMENT 1644.00 0.00 366
2013 HOPEWELL OIL & GAS DEVELOPMENT 1196.00 0.00 365
2014 HOPEWELL OIL & GAS DEVELOPMENT 1143.00 0.00 365
2015 HOPEWELL OIL & GAS DEVELOPMENT 879.00 0.00 365
2016 HOPEWELL OIL & GAS DEVELOPMENT 130.00 0.00 60
2017 HOPEWELL OIL & GAS DEVELOPMENT 0.00 0.00 0
2018 HOPEWELL OIL & GAS DEVELOPMENT 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2000 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 180
2001 HOPEWELL OIL & GAS DEVELOPMENT Brine 74 365
2002 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2003 HOPEWELL OIL & GAS DEVELOPMENT Brine 75 365
2004 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2005 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2006 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2007 HOPEWELL OIL & GAS DEVELOPMENT Brine
2008 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2009 HOPEWELL OIL & GAS DEVELOPMENT Brine 50 365
2010 HOPEWELL OIL & GAS DEVELOPMENT Brine 25 0
2011 HOPEWELL OIL & GAS DEVELOPMENT Brine 0
2012 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 366
2013 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2014 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2015 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2016 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 60
2017 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 0
2018 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1566969772 2019-1-18 0:00: PW No Violations 0.30
-1604734178 2013-6-20 0:00: PW No Violations 1.00
-1661234411 2016-3-10 0:00: PW No Violations 1.00
-1877127130 2020-10-14 0:00 PW No Violations 0.60
-260830796 2016-1-25 0:00: PW No Violations 1.00
-900743811 2003-6-3 0:00:0 PL No Violations
0260830796 2016-01-25 Production Wells No Violations This well appears to be in production at this time. The well has a pumping unit on it with rods and 1.5 tubing down hole. The valves are open at the well head and the pressure gauge is showing over 75lbs. There are no violations at this time.
0900743811 2003-06-03 Preliminary Restoration No Violations
1555417437 2019-04-16 Production Wells No Violations My inspection revealed that the gas leak has been corrected. I did not observe any gas leaks at the well. Identification has been posted at the tank battery. Time of inspection: 8:25 AM. Weather: 41 degrees F, Sunny
1566969772 2019-01-18 Production Wells No Violations I conducted a compliance notice follow-up on this well today. My inspection revealed that the well was still leaking gas just as it was on 11/19/2018. Hopewell Oil and Gas Development is no longer in business. Time of inspection: 11:10 AM. Weather: 35 degrees F, Overcast
1604734178 2013-06-20 Production Wells No Violations This well is capable of production. It has a pumping unit on it with rods and tubing in it. The valve from the well to the tank is open. The identification for this well is on the tank. No violations at this time.
1661234411 2016-03-10 Production Wells No Violations This well appears to be capable of production. The well has a pumping unit on it with rods and tubing in it. The identification for the well is located on the production tank. There are no violations at this time.
1682720132 2016-12-28 Production Wells No Violations This well appears to be in production at this time. The well has a pumping unit on it with rods and 1.5 inch diameter tubing down hole. The valves are open at the wellhead and the pressure gauge is showing over 75lbs. There is 1-100 barrel production tank at the tank pad. There are no violations at this time.
1996413311 2018-11-19 Production Wells No Violations The landowner Paul Swisher contacted the DOGRM on 11/18/2018 regarding a gas leak at this well. I arrived at 1:00 PM to check on the status of the leak. I was accompanied by Mr. Swisher. The well was leaking gas from around the 4.5 inch casing, the 1.5 inch tubing, and stuffing box. I could hear the leak from Zartman Rd. which is approximately 500 feet from the well. The well was equipped with a pumping unit and motor. The tank battery consists of (1) 100 barrel tank and a separator. I did not observe identification at the well or tank battery. Time of inspection: 1:00 PM. Weather: 39 degrees F, Overcast

For data sources see[9]

References