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Well ID: 34-119-28233 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Highland Township | |
Operator Name: BIG SKY ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: MORROW RUSSELL & DOROTHY | |
License Status: Producing | |
License Date: 1999-08-31 | |
Spud Date: 1999-12-09 | |
Spud Drilling Contractor: G & H DRLG | |
Final Drill Date: 1999-12-22 | |
Well Total Depth: 7020.00 ft | |
Configuration: Vertical | |
Latitude: 40.080000 | |
Longitude: -81.750000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 1999-08-31 | Proposed Formations:MT. SIMON (MAY NOT PRODUCE CLINTON0, Issued Date:8/31/99, Expired Date:8/30/2000 6:00:00 AM, Drilling unit acres:153.72, Proposed Well Type:OG, Proposed Well Class:EDPW |
Original Spud | 1999-12-09 | RBDMS Rec |
Completed | 1999-12-22 | RBDMS Rec |
Reached Total Depth | 1999-12-22 | RBDMS Rec |
Construction Permit Expires | 2000-08-30 | RBDMS Rec |
Completion Report Received | 2001-04-11 | RBDMS Rec |
Change of Owner | 2007-12-13 | Operator changed from 4431, VALLEY ENTERPRISES to 1333, BIG SKY ENERGY INC |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2001-06-07 | 6690 | 6702 | 48 |
6690 | 6702 | 48 | |
6690 | 6702 | 48 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 20 | 1000 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | VALLEY ENTERPRISES | 8428.00 | 30.00 | 270 |
2014 | BIG SKY ENERGY INC | 965.00 | 0.00 | 365 |
2016 | BIG SKY ENERGY INC | 0.00 | 0.00 | 0 |
2017 | BIG SKY ENERGY INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | VALLEY ENTERPRISES | Brine | 35 | 270 |
2014 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2016 | BIG SKY ENERGY INC | Brine | 0 | 0 |
2017 | BIG SKY ENERGY INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1726392481 | 2016-4-16 0:00: | PW | No Violations | 0.50 |
-244566721 | 2003-6-6 0:00:0 | PW | No Violations | |
-593038824 | 2008-3-21 0:00: | PW | No Violations | |
0244566721 | 2003-06-06 | Production Wells | No Violations | |
0538838185 | 2008-03-19 | Production Wells | No Violations | Shut in. At well and sales point. |
0593038824 | 2008-03-21 | Production Wells | No Violations | Shut in at well and at sales point. 550psi on casing. |
0979472399 | 2016-05-05 | Production Wells | No Violations | The follow-up inspection is due to a Temporary Restraining Order issued in the Trumble County Court of Common Pleas and the Chiefs Order #2015-535, Chiefs Order #2016-105
The tubing valve is shut but the tubing annulus is open. The well is shut in at the separator. The master meter at Dominion has been shut in. The landowner is getting gas from Permit Number 119-22236. |
1726392481 | 2016-04-16 | Production Wells | Violations Noted | The follow-up inspection is due to a Temporary Restraining Order issued in the Trumble County Court of Common Pleas and the Chiefs Order #2015-535, Chiefs Order #2016-105.
- |
538838185 | 2008-3-19 0:00: | PW | No Violations | |
979472399 | 2016-5-5 0:00:0 | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1726392481 | US-OH-117134 | 2016-06-06 | Failure to legibly identify well | |
1726392481 | US-OH-117135 | 2016-06-06 | Non urban - failure to meet tank battery setbacks from an inhabited structure | |
1726392481 | US-OH-117136 | 2016-06-06 | Failure to meet well and/or tank battery setbacks from a railroad or roads |
For data sources see[9]