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34-119-28230

Well Details

Well ID: 34-119-28230
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Country: United States
State: Ohio
County: Muskingum
Municipality: Falls Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: MUSKINGUM RIVER PARTNERS
License Status: Producing
License Date: 1999-08-13
Spud Date: 1999-08-22
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS
Final Drill Date: 1999-08-29
Well Total Depth: 5962.00 ft
Configuration: Vertical
Latitude: 39.990000
Longitude: -81.980000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 1999-08-13 Proposed Formations:CLINTON/KNOX, Issued Date:8/13/99, Expired Date:8/12/2000 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW
Original Spud 1999-08-22 RBDMS Rec
Completed 1999-08-29 RBDMS Rec
Reached Total Depth 1999-08-29 RBDMS Rec
Plugged Back 1999-08-30 RBDMS Rec
Completion Report Received 2000-02-11 RBDMS Rec
Construction Permit Expires 2000-08-12 RBDMS Rec
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-17 3678 3729 19
3678 3729 19
3678 3729 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 38000 Gal 20000 500 GALLONS HCL ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2000 HOPEWELL OIL & GAS DEVELOPMENT 828.00 0.00 210
2001 HOPEWELL OIL & GAS DEVELOPMENT 8719.00 0.00 365
2002 HOPEWELL OIL & GAS DEVELOPMENT 6027.00 0.00 365
2003 HOPEWELL OIL & GAS DEVELOPMENT 6187.00 0.00 365
2004 HOPEWELL OIL & GAS DEVELOPMENT 6115.00 0.00 365
2005 HOPEWELL OIL & GAS DEVELOPMENT 4164.00 0.00 365
2006 HOPEWELL OIL & GAS DEVELOPMENT 3843.00 0.00 365
2007 HOPEWELL OIL & GAS DEVELOPMENT 3317.00 0.00 0
2008 HOPEWELL OIL & GAS DEVELOPMENT 3364.00 47.00 365
2009 HOPEWELL OIL & GAS DEVELOPMENT 4335.00 0.00 365
2010 HOPEWELL OIL & GAS DEVELOPMENT 3436.00 0.00 0
2011 HOPEWELL OIL & GAS DEVELOPMENT 3605.00 0.00 0
2012 HOPEWELL OIL & GAS DEVELOPMENT 2798.00 0.00 366
2013 HOPEWELL OIL & GAS DEVELOPMENT 2402.00 0.00 365
2014 HOPEWELL OIL & GAS DEVELOPMENT 1924.00 0.00 365
2015 HOPEWELL OIL & GAS DEVELOPMENT 1475.00 0.00 365
2016 HOPEWELL OIL & GAS DEVELOPMENT 0.00 0.00 60
2017 HOPEWELL OIL & GAS DEVELOPMENT 0.00 0.00 0
2018 HOPEWELL OIL & GAS DEVELOPMENT 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2000 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 210
2001 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2002 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2003 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2004 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2005 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2006 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2007 HOPEWELL OIL & GAS DEVELOPMENT Brine
2008 HOPEWELL OIL & GAS DEVELOPMENT Brine 5 365
2009 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2010 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 0
2011 HOPEWELL OIL & GAS DEVELOPMENT Brine 0
2012 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 366
2013 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2014 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2015 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 365
2016 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 60
2017 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 0
2018 HOPEWELL OIL & GAS DEVELOPMENT Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1296312392 2016-4-21 0:00: PW No Violations 4.50
-1361757759 2010-2-4 0:00:0 PW No Violations
1118164143 2005-11-07 Production Wells No Violations Okay
1296312392 2016-04-21 Production Wells No Violations I had received a call from Muskingum Emergency Management. There was a gas leak at North Linden Avenue across from the Boat club. The well in question is 119-28230. Austin Gutridge is accompanying me on the inspection. The well is currently shut in due to a bankruptcy. Complaint Number is 5307. The well is dumping gas out of the horizontal separator. I placed a call into Howard Harrop. He will come over and shut the line off. I witnessed Howard shutting off the gas. Complaint was resolved on the day of this inspection.
1306722507 2003-12-11 Production Wells No Violations
1361757759 2010-02-04 Production Wells No Violations Producing, noproblems noted at time of inspection.
1621793184 2016-03-07 Production Wells No Violations

-100 barrel steel tank and all valves are shut and bull plugged. There is a horizontal separator that appears to opened and working. The gas may be going into the National Line directly. There is identification at the tank. The company is current with production records with the Division of Oil and Gas.

iDIAN00607 2001-06-01 Preliminary Restoration No Violations
iDIAN006077 2001-6-1 0:00:0 PL No Violations

For data sources see[9]

References