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Well ID: 34-089-26186 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Licking Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: MARY JO LLC | |
License Status: Final Restoration | |
License Date: 2017-06-29 | |
Spud Date: 2017-08-30 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2017-09-11 | |
Well Total Depth: 4390.00 ft | |
Configuration: Vertical | |
Latitude: 39.990000 | |
Longitude: -82.460000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-06-29 | Proposed Formations:KNOX, Issued Date:6/29/2017, Expired Date:6/29/2019 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EOUT |
Reached Total Depth | 2017-09-11 | |
Plugged/Abandoned | 2017-09-14 | |
Completion Report Received | 2017-10-27 | |
Record Last Modified | 2017-12-16 | |
Construction Permit Expires | 2019-06-29 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1097501027 | 2017-8-31 0:00: | DD | No Violations | 1.50 |
-924469525 | 2017-10-2 0:00: | FR | No Violations | 0.50 |
-941660866 | 2017-9-15 0:00: | PB | No Violations | 0.50 |
0924469525 | 2017-10-02 | Final Restoration | No Violations | This inspection was conducted as a final restoration status check. Equipment has been removed from the well location. The pits have not been closed. The final restoration is not complete as of this inspection. No violations. Time of inspection: 10:00 AM. Weather: 55*F, Sunny |
0941660866 | 2017-09-15 | Plug / Plug Back | No Violations | This inspection was conducted to witness the surface plug be topped off. Formation Cementing pumped 15 sacks of Class A cement to surface. Plugging operations were complete. |
1097501027 | 2017-08-31 | Drill / Deepen / Reopen | No Violations | Kilbarger Drilling is setup on location and has started drilling this well. They are currently at 312 feet deep and will be drilling to a depth of 400 feet. They will be contacting me when they are ready to cement the pipe in the hole. Formation Cementing will be used for the cement job. |
1446278481 | 2017-09-14 | Plug / Plug Back | No Violations | This inspection revealed Bishop Well Service was contracted to plug this well for Artex Oil Company. Artex Oil Company did not run or cement 4.5 inch casing as mentioned in the previous inspection. Formation Cementing was the cement contractor for the plug job. Artex Oil Company was advised to fill out a plug report and have it notarized. The well was plugged this date. The surface plug did not stay at the surface. It was decided to come back the next day and pump cement to surface. |
1505224131 | 2017-09-12 | Drill / Deepen / Reopen | No Violations | An inspection of drilling operations revealed Kilbarger Rig #5 has drilled in and cemented the 4.5 inch production casing. The rig was in the process of being disassembled and moving to a new location in another county. No violations. Time of inspection: 9:30 AM. Weather: 59*F, Mostly cloudy |
1805342264 | 2017-12-07 | Final Restoration | No Violations | I inspected this location accompanied by Joe Snider of Artex Oil Company. The well location has been graded and the pits were closed. The well is located in an agricultural field and therefore will not be planted in grass. All equipment was removed. The well location meets ORC 1509.072 requirements. Time of inspection: 1:00 PM. Weather: 33*F, Partly cloudy |
1891270631 | 2017-10-31 | Final Restoration | No Violations | The inspection revealed that the restoration has not been completed as of this date. The pits were still open and topsoil was still stockpiled. The company will be contacted and advised to start working on the restoration. Time of inspection: 8:30 AM. Weather: 35*F, Sunny |
2062045537 | 2017-09-06 | Drill / Deepen / Reopen | No Violations | I stopped by this well to pick up the cement paperwork from where they cemented the 8 inch casing in the well back to surface. The crew said the cement job went good. Formation Cementing was the company used to cement the casing back to the surface. They used 200 sks of Class A cement with 15 barrel returns back to the surface. The rig crew is now at 690 feet of total depth for drilling. |
For data sources see[3]