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34-005-60181

Well Details

Well ID: 34-005-60181
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Country: United States
State: Ohio
County: Ashland
Municipality: Green Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: FROUTZ HENRY
License Status: Storage Well
License Date:
Spud Date: 1912-05-07
Spud Drilling Contractor: UNKNOWN OWNER
Final Drill Date: 1912-07-05
Well Total Depth: 2748.00 ft
Configuration: Vertical
Latitude: 40.710000
Longitude: -82.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1912-05-07
Completed 1912-07-05
Reached Total Depth 1912-07-05
Change of Owner 2011-08-03 Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION
Record Last Modified 2013-05-23

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1044511926 2016-10-26 0:00 SO No Violations 0.50
-1103395753 2014-10-23 0:00 SO No Violations 0.50
-1202353160 2012-5-10 0:00: SO No Violations
-1259132028 2012-5-16 0:00: SO No Violations
-1380026441 2020-1-29 0:00: SO No Violations
-146080725 2019-3-20 0:00: SO No Violations
-1622371878 2018-11-19 0:00 SO No Violations
-279903358 2015-10-21 0:00 SO No Violations 0.50
-766752749 2019-4-18 0:00: SO No Violations
-992639850 2017-7-27 0:00: SO No Violations
0279903358 2015-10-21 Storage Well No Violations ID is posted and the location is maintained. The annulus valve is closed and plugged.
0416241613 2014-01-16 Storage Well No Violations ID posted, location maintained.
0766752749 2019-04-18 Storage Well No Violations Performed annual inspection for Columbia Gas Storage Well #0289 on 04/18/2019. The well is equipped with a flanged wellhead with 1-master valve and 1-wing valve, and a drip. Well identification is clearly displayed. The well is located ~120 from its RBDMS location. A map showing the location discrepancy, as well as a request for the location to be updated in RBDMS was sent to Aaron Lantz (DOGRM Columbus). No other problems were noted at the time of the inspection.
0992639850 2017-07-27 Storage Well No Violations ID is posted and the location is maintained. The well is equipped with a separator.
1044511926 2016-10-26 Storage Well No Violations ID is posted and the location is maintained. The well is equipped with a separator.
1103395753 2014-10-23 Storage Well No Violations ID posted, location maintained.
1202353160 2012-05-10 Storage Well No Violations Inspect well. Operator is rehabbing well. Run 5.5 inch casing to 2730 ft. Log well original depth of 2744 ft. Drill well to depth of 2811 ft. Cement liner in across Formation; top of cement liner at 2619.71 ft., latch down set at 2792.05 ft, shoe set at 2797 ft. Pump 50 sacks to set 3.5 inch liner. Well drilled in 1912 and was open hole construction.
1259132028 2012-05-16 Storage Well No Violations Inspect well. operator is reworking the surface casing. Pulled 789.04 ft. of 7 inch casing, the 8 inch casing would not pull out. Install new 7 inch casing 787.10 ft. 20 lb/ft. set perfs at 782 to 783 ft. and set a plug. Good returns on cement with 3 % Calcium.
1622371878 2018-11-19 Storage Well No Violations ID is posted and the location is maintained. The annulus is shut in. The well is equipped with a separator.
416241613 2014-1-16 0:00: SO No Violations 0.50

For data sources see[4]

References