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37-129-28963

Well Details

Well ID: 37-129-28963
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Washington Township
Operator Name: CNX GAS CO LLC
Well Pad ID: 147584
Farm/Lease Name: SHAW 1GHSU
License Status:
Spud Date:
Permit Date: 2017-12-06
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 40.503875
Longitude: -79.572447

For data sources see[1][2][3]

Well History

Date Event
2017-12-06 New Permit Application
2018-05-08 Performed Spud Operation
2018-08-24 MOD

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2019 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2018 CNX GAS CO LLC Drill Cuttings 512.42 Tons LANDFILL 100172
2018 CNX GAS CO LLC Drilling Fluid Waste 1,361.41 Bbl RESIDUAL WASTE PROCESSING FACILITY
2018 CNX GAS CO LLC Drilling Fluid Waste 18.67 Bbl SURFACE IMPOUNDMENT 95-7-37312-17
2018 CNX GAS CO LLC Drilling Fluid Waste 41.03 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE ORDER 2016-415
2018 CNX GAS CO LLC Produced Fluid 225.40 Bbl REUSE (AT WELL PAD)
2018 CNX GAS CO LLC Drilling Fluid Waste 167.78 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2018 CNX GAS CO LLC Drill Cuttings 1,158.48 Tons LANDFILL 06-08438
2018 CNX GAS CO LLC Produced Fluid 21.65 Bbl SURFACE IMPOUNDMENT 95-7-37312-21
2018 CNX GAS CO LLC Produced Fluid 133.88 Bbl RESIDUAL WASTE PROCESSING FACILITY
2018 CNX GAS CO LLC Other Oil & Gas Wastes 5.00 Bbl REUSE (AT WELL PAD)
2018 CNX GAS CO LLC Produced Fluid 679.61 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2018 CNX GAS CO LLC Other Oil & Gas Wastes 282.44 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29
2018 CNX GAS CO LLC Other Oil & Gas Wastes 353.98 Bbl RESIDUAL WASTE PROCESSING FACILITY
2018 CNX GAS CO LLC Produced Fluid 153.03 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29
2018 CNX GAS CO LLC Drill Cuttings 507.08 Tons LANDFILL 100277
2018 CNX GAS CO LLC Other Oil & Gas Wastes 10.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 2014-184
2018 CNX GAS CO LLC Other Oil & Gas Wastes 141.47 Bbl SURFACE IMPOUNDMENT 95-7-37312-21
2018 CNX GAS CO LLC Synthetic Liner Materials 2.26 Tons LANDFILL 100280
2018 CNX GAS CO LLC Other Oil & Gas Wastes 577.75 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2018 CNX GAS CO LLC Produced Fluid 56.00 Bbl SURFACE IMPOUNDMENT 95-7-37312-17
2018 CNX GAS CO LLC Other Oil & Gas Wastes 12.86 Bbl REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA
2018 CNX GAS CO LLC Drilling Fluid Waste 215.35 Bbl RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2018 CNX GAS CO LLC Drill Cuttings 311.37 Tons LANDFILL 100280
2018 CNX GAS CO LLC Drilling Fluid Waste 16.67 Bbl SURFACE IMPOUNDMENT 95-7-37312-21
2018 CNX GAS CO LLC Other Oil & Gas Wastes 71.66 Bbl RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2018 CNX GAS CO LLC Produced Fluid 12.14 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 2014-184
2018 CNX GAS CO LLC Drilling Fluid Waste 1,238.06 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29
2018 CNX GAS CO LLC Other Oil & Gas Wastes 14.16 Bbl INJECTION DISPOSAL WELL 34-119-28780
2018 CNX GAS CO LLC Drilling Fluid Waste 93.58 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 2014-184
2018 CNX GAS CO LLC Synthetic Liner Materials 0.98 Tons LANDFILL 100663
2019 CNX GAS CO LLC Synthetic Liner Materials 0.82 Tons LANDFILL 100280
2019 CNX GAS CO LLC Drilling Fluid Waste 27.86 Bbl REUSE (AT WELL PAD)
2019 CNX GAS CO LLC Produced Fluid 508.09 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2019 CNX GAS CO LLC Soil Contaminated by Oil 0.84 Tons LANDFILL CID: 29084
2019 CNX GAS CO LLC Drill Cuttings 35.37 Tons LANDFILL 06-08438
2019 CNX GAS CO LLC Drilling Fluid Waste 1.11 Tons LANDFILL CID: 38042
2019 CNX GAS CO LLC Produced Fluid 14.29 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29
2019 CNX GAS CO LLC Other Oil & Gas Wastes 212.86 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2019 CNX GAS CO LLC Other Oil & Gas Wastes 386.42 Bbl RESIDUAL WASTE PROCESSING FACILITY
2019 CNX GAS CO LLC Produced Fluid 56.36 Bbl SURFACE IMPOUNDMENT 95-7-37312-21
2019 CNX GAS CO LLC Drilling Fluid Waste 20.72 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29
2019 CNX GAS CO LLC Produced Fluid 22.00 Bbl INJECTION DISPOSAL WELL 34-009-23821
2019 CNX GAS CO LLC Soil Contaminated by Oil & Gas Related Spills 1.55 Tons LANDFILL 100280
2019 CNX GAS CO LLC Produced Fluid 2.68 Tons RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2019 CNX GAS CO LLC Filter Socks 1.42 Tons RESIDUAL WASTE PROCESSING FACILITY 2014-541
2019 CNX GAS CO LLC Other Oil & Gas Wastes 278.44 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2019 CNX GAS CO LLC Synthetic Liner Materials 6.56 Tons LANDFILL 100663
2019 CNX GAS CO LLC Soil Contaminated by Oil 1.55 Tons LANDFILL 100280
2019 CNX GAS CO LLC Other Oil & Gas Wastes 16.31 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW019
2019 CNX GAS CO LLC Produced Fluid 77.43 Bbl SURFACE IMPOUNDMENT 95-7-37312-17
2019 CNX GAS CO LLC Other Oil & Gas Wastes 146.00 Bbl RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2019 CNX GAS CO LLC Produced Fluid 289.01 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2019 CNX GAS CO LLC Produced Fluid 16.27 Tons RESIDUAL WASTE PROCESSING FACILITY 2014-541
2019 CNX GAS CO LLC Produced Fluid 62.51 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW019
2019 CNX GAS CO LLC Soil Contaminated by Oil & Gas Related Spills 0.84 Tons LANDFILL CID: 29084
2019 CNX GAS CO LLC Other Oil & Gas Wastes 44.28 Bbl REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA
2019 CNX GAS CO LLC Other Oil & Gas Wastes 14.29 Bbl REUSE (AT WELL PAD)
2019 CNX GAS CO LLC Other Oil & Gas Wastes 140.72 Bbl SURFACE IMPOUNDMENT 95-7-37312-17
2019 CNX GAS CO LLC Produced Fluid 142.14 Bbl RESIDUAL WASTE PROCESSING FACILITY
2019 CNX GAS CO LLC Produced Fluid 144.84 Bbl REUSE (AT WELL PAD)
2019 CNX GAS CO LLC Drilling Fluid Waste 448.99 Bbl RESIDUAL WASTE PROCESSING FACILITY
2019 CNX GAS CO LLC Other Oil & Gas Wastes 42.86 Bbl SURFACE IMPOUNDMENT 95-7-37312-21
2019 CNX GAS CO LLC Produced Fluid 177.13 Bbl REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA
2019 CNX GAS CO LLC Drilling Fluid Waste 180.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW005
2019 CNX GAS CO LLC Drilling Fluid Waste 193.03 Bbl RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2019 CNX GAS CO LLC Other Oil & Gas Wastes 65.00 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2726989 Primary Facility 2018-05-07 Drilling/Alteration No Violations Noted This Utica well was spudded on 5/6/2018. The Spud Rig was drilling a 36" hole at a depth of 56' at the time of this inspection. The permit copy , drilling information and all equipment on site looked ok.
2734520 Primary Facility 2018-05-24 Routine/Complete Inspection No Violations Noted Inspection in response to receipt of spud notification. At the time of inspection drill rig on site, setting up to commence drilling operations. All material equipment associated with drilling activity located within secondary containment.
2734878 Primary Facility 2018-05-29 Drilling/Alteration No Violations Noted This Utica well was spudded on 5/6/2018. The rig ran and cemented 129' of 30" casing. The next string of casing ran and cemented was 817' of 18" casing which was cemented with 250 bbl's of cement with a 22 bbl return. At the time of this inspection the rig had shanked the bit at 1450', had fished two pieces of the bit back out of the hole and was fishing for the final piece of the bit. The permit copy, drilling information and all equipment on site looked ok.
2736567 Primary Facility 2018-06-01 Drilling/Alteration No Violations Noted This Utica well was spudded on 5/6/2018. The rig ran and cemented 129' of 30" casing. The next string of casing ran and cemented was 817' of 18" casing which was cemented with 250 bbl's of cement with a good return on cement. The rig had shanked the bit at 1450', had fished all 3 pieces of the bit back out of the hole, had drilled on down to 1861', lost their air and were tripping back out of the hole to check their bit at the time of this inspection.The permit copy, drilling information and all equipment on site looked ok.
2766423 Primary Facility 2018-08-23 Drilling/Alteration No Violations Noted Well drilled to 2013'. Rig will move on 8/24/18 to complete drilling.
2771646 Primary Facility 2018-09-06 Routine/Complete Inspection No Violations Noted At the time of inspection drill rig on site and drilling activity ongoing. All materials and equipment located within secondary containment. No E&S issues.
2780034 Primary Facility 2018-09-20 Drilling/Alteration No Violations Noted 9/20/18 - 5.5" csg. Hung in well bore due to air locked sub malfunction. Well drilled to 21945' csg. @ 21280.
2840489 Primary Facility 2019-01-30 Incident- Response to Accident or Event Violation(s) Noted
2844211 Primary Facility 2019-02-21 Routine/Complete Inspection No Violations Noted Operator rep on site during inspection.

According to operator rep, well is shut in and a USIT log was run on this well earlier in the week. Well cellar does not appear to contain fluids at this time. Well head is covered by plastic tarp. Liner is installed on pad. This liner appears structurally sound. Three brine tanks on site. Roll off boxes on site.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2840489 842252 2019-01-26 78.73(a) Environmental Health & Safety
2840489 842253 2019-01-26 OGA3219 Environmental Health & Safety

For data sources see[7]

References