X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-129-00737

Well Details

Well ID: 37-129-00737
Loading map...
Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Rostraver Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: D. HOUSEMAN 2
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.162833
Longitude: -79.841306

For data sources see[1][2][3]

Well History

Date Event
1941-11-01 Drilling Completion
1989-12-30 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 2922.00 365 0.00 0 0.00 0
1992 3225.00 366 0.00 0 0.00 0
1993 3230.00 334 0.00 0 0.00 0
1994 2097.00 307 0.00 0 0.00 0
1995 3275.00 306 0.00 0 0.00 0
1996 3275 365 0.00 0 0.00 0
1998 2700 365 0.00 0 0.00 0
1999 CONSOL GAS CO 3594 365 0.00 0 0.00 0
2000 CONSOL GAS CO 2909 365 0.00 0 0.00 0
2001 CONSOL GAS CO 3901 365 0.00 0 0.00 0
2002 CONSOL GAS CO 3668 365 0.00 0 0.00 0
2003 CONSOL GAS CO 3048 365 0.00 0 0.00 0
2005 CONSOL GAS CO 3132 365 0.00 0 0.00 0
2006 CONSOL GAS CO 827.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 3650.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 3456.00 365 0.00 0 0.00 0
2009 CONSOL GAS CO 3773.00 365 0.00 0 0.00 0
2010 CONSOL GAS CO 3,710.00 365 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 2,816.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 3,088.00 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 2,687.00 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 3,137.00 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 2,930.00 366 0.00 0 0.00 0
2017 CNX GAS CO LLC 2,881.00 365 0.00 0 0.00 0
2018 CNX GAS CO LLC 2,052.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 3,113.00 334 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2476299 Primary Facility 2016-04-19 Routine/Partial Inspection No Violations Noted At the time of inspection the well was drilled and appeared to be in production. No sign of accelerated erosion or sedimentation.

For data sources see[6]

References