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37-125-24006

Well Details

Well ID: 37-125-24006
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Country: United States
State: Pennsylvania
County: Washington
Municipality: West Pike Run Township
Operator Name: ANTERO RESOURCES CORP
Well Pad ID:
Farm/Lease Name: HILL UNIT 4H
License Status:
Spud Date:
Permit Date: 2010-03-02
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 40.088194
Longitude: -79.974144

For data sources see[1][2][3]

Well History

Date Event
2010-03-02 New Permit Application
2011-03-25 Permit Renewal Application

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 ANTERO RESOURCES CORP 0.00 0 0.00 0 0.00 0
2011 ANTERO RESOURCES CORP 0.00 0 0.00 0 0.00 0
2012 ANTERO RESOURCES CORP 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2509338 Primary Facility 2016-06-20 Complaint Inspection No Violations Noted On 6/20/16, I performed a complaint inspection at the Hill/Hopkins site and JM Sphar 4 well in response to complaint 320508 and made the following observations:

•Water samples were collected for SAC 946 analysis in response to the complaint. •Hill/Hopkins Site:

    -Site was in generally good condition with two wells drilled.
    -Containment appeared to be well maintained.
    -Vegetation on site was patchy in some areas (behind production units and on cut slope above impoundment).
    -The depression around well 2H was filled with water.
    -No evidence was found of spills or leaks on the site at the time of inspection.

•J M Sphar 4: The well and surrounding area were in good condition with no evidence of spills or leakage. Vegetation and berm around the well head and associated tank were also intact.

2511085 Primary Facility 2016-07-13 Administrative/File Review No Violations Noted Administrative review of lab results on 7/13/16 indicates that the water supply does not appear to have been impacted by oil & gas activity. Results and documentation for complaint 320508 forwarded for final determination.

For data sources see[6]

References