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37-125-21260

Well Details

Well ID: 37-125-21260
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Cecil Township
Operator Name: PROSPERITY OIL CO INC
Well Pad ID:
Farm/Lease Name: CONSOLIDATION COAL CO H & I CASCIOLA 3
License Status: ABANDONED
Spud Date:
Permit Date: 1979-06-08
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.314333
Longitude: -80.204389

For data sources see[1][2][3]

Well History

Date Event
1979-06-08 New Permit Application
1979-06-18 Performed Spud Operation
1979-07-12 Drilling Completion
1979-08-15 Perforation
1979-08-15 Performed Stimulation
1984-06-13 NEWLY DRILLED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1979-08-15 0 0 0

For data sources see[5]


Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2421851 Primary Facility 2015-06-19 Routine/Complete Inspection Pending Well is intact, not leaking oil, but leaking gas at tubinghead (leak may stop by hammering tighter). No identification on wellhead. Well is 54 feet from nearest home and 57 feet from gravel lane off Ridgewood Drive. Additional houses to be built nearby. DEP currently lists well as "DEP Plugged", so there is some internal confusion about well identity and status.
2421872 Primary Facility 2015-08-21 Routine/Complete Inspection Pending Response to a call 8/20/15 from resident @ 51 Ridgewood Drive (house next to well) asking about the status of the well and to comment they could smell gas from the well recently. Went to well following day (8/21/15) to check well for any change since my prior inspection on 6/19/15. No notable change, still leaking small amount of gas from the tubinghead. Brush has been cleared around well in preparation for future development.
2461176 Primary Facility 2016-03-04 Routine/Partial Inspection No Adverse Event or Action Reported Visited site to check status of well and adjacent site excavation for development. Well remains in same condition as other inspections, w/ very slight gas leak @ tubinghead. Nearby excavation activity has not affected the wellhead in any way.
2479524 Primary Facility 2016-04-27 Routine/Partial Inspection No Adverse Event or Action Reported Visited site to check status of well and adjacent site excavation for development. Well remains in same condition as other inspections, w/ very slight gas leak @ tubinghead. Nearby excavation activity has not affected the wellhead in any way.
2488821 Primary Facility 2016-05-27 Routine/Partial Inspection No Adverse Event or Action Reported Inspected well for any disturbance to wellhead from neaby construction; none noted. Well lightly venting gas.
2598710 Primary Facility 2017-03-27 Routine/Partial Inspection No Violations Noted Wellhead is intact, unchanged from prior visits w/ a very slight gas leak @ tubinghead.
2613919 Primary Facility 2017-07-10 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to update status of wellhead & surrounding construction. Wellhead remains intact and has not been affected by work on housing development. Well still has small gas leak.
2678883 Primary Facility 2018-01-05 Routine/Partial Inspection No Viols - Permanently Shut Down Well is intact and unchanged from prior inspections. There does not appear to have been any excavation activities around the well for several months.
2773864 Primary Facility 2018-08-27 Routine/Partial Inspection No Viols - Permanently Shut Down Intact and unchanged from prior visit. Nearby development activity has ceased for now. No leaks noted.
751269 Primary Facility 1988-08-25 Routine/Complete Inspection Violation(s) Noted NO ID; E&S OK
764641 Primary Facility 1994-05-04 Routine/Complete Inspection Violation(s) Noted NO ID;E&S OK;ABANDONED
765068 Primary Facility 1994-06-28 Routine/Complete Inspection Violation(s) Noted NO TAG;ABANDONED-NOV SENT
766667 Primary Facility 1995-02-13 Routine/Complete Inspection Violation(s) Noted ABANDONED, NO TAG

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
751269 89022 08/25/1988 1988-08-25 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative NO ID TAG
764641 102494 05/04/1994 1994-05-04 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative NO ID
765068 102820 06/28/1994 1994-06-28 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative NO ID
766667 103898 02/13/1995 1995-02-13 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative NOT TAGGED W/PERMIT NO
766667 103899 02/13/1995 1995-02-13 210A - Failure to adequately plug or schedule plugging of a well upon abandonment Administrative WELL ABANDONED

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
102494 14051 NOV - Notice of Violation Unresolvable 1995-02-06
103898 12008 NOV - Notice of Violation Legacy Data 1999-09-13
103899 12008 NOV - Notice of Violation Legacy Data 1999-09-13

For data sources see[6]

References

  1. "Permits Issued Detail Report". Pennsylvania Department of Environmental Protection. 2019-05-20. Retrieved 2019-05-21. 
  2. "Spud Data Report". Pennsylvania Department of Environmental Protection. 2019-04-30. Retrieved 2019-05-16. 
  3. "Oil and Gas Well Pad Report". Pennsylvania Department of Environmental Protection. 2019-05-20. Retrieved 2019-05-21. 
  4. "Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources". 2020-02-27. Retrieved 2020-02-27. 
  5. "Completion Reports - Stimulations". Pennsylvania Department of Conservation and Natural Resources. 2020-03-02. Retrieved 2020-03-02. 
  6. "Oil and Gas Compliance Report". Pennsylvania Department of Environmental Protection. 2019-05-20. Retrieved 2019-05-21.