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37-125-21119

Well Details

Well ID: 37-125-21119
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Cecil Township
Operator Name: PROSPERITY OIL CO INC
Well Pad ID:
Farm/Lease Name: IRK A MCCONNELL ET UX 3
License Status: ACTIVE
Spud Date:
Permit Date: 1978-01-06
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.314972
Longitude: -80.191028

For data sources see[1][2][3]

Well History

Date Event
1978-01-06 New Permit Application
1978-03-08 Performed Spud Operation
1978-03-15 Drilling Completion
1978-04-10 Perforation
1978-04-10 Performed Stimulation
1978-08-28 NEWLY DRILLED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1978-04-10 0 0 0

For data sources see[5]


Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2755390 Primary Facility 2018-07-16 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Kriebel rig tagged TD inside 4 1/2" casing at 2516', fluid level at ~ 1000'. Bottom perfs at 2502' per completion report
2755818 Primary Facility 2018-07-20 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Cement contractor pumped two 450' cement plugs (calculated). Kriebel rig TOOH with work string. Keystone logged well, found 4 1/2" casing cemented into 8 5/8" casing up to ~835'. Cut casing at 800'. Kriebel pulled casing free after cut.
2757377 Primary Facility 2018-07-23 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Kriebel TIH with work string, having difficulty getting tubing stabbed into stub of remaining 4 1/2" casing at 800'.
2757391 Primary Facility 2018-07-24 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Kriebel continuing effort to snub work string into 4 1/2" casing top at 800'. Shut down to consider options.
2757722 Primary Facility 2018-07-30 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Kriebel plugged well to surface, demobilized to McConnell 2.
766673 Primary Facility 1995-02-15 Routine/Complete Inspection Violation(s) Noted ABANDONED, NO TAG
779400 Primary Facility 1998-11-08 Routine/Complete Inspection No Violations Noted ABANDONED
920284 Primary Facility 2000-03-01 Routine/Complete Inspection No Violations Noted Location: South pasture above the Montour Walking Trail. No sign of the well being tended. Wellhead, large pumpjack, upright metal-type tank here on bench. Pole electric service wires are disconnected. Idle, untended well.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
766673 103910 02/15/1995 1995-02-15 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative NOT TAGGED W/PERMIT NO
766673 103911 02/15/1995 1995-02-15 210A - Failure to adequately plug or schedule plugging of a well upon abandonment Administrative WELL ABANDONED

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
103910 12008 NOV - Notice of Violation Legacy Data 1999-09-13
103911 12008 NOV - Notice of Violation Legacy Data 1999-09-13

For data sources see[6]

References

  1. "Permits Issued Detail Report". Pennsylvania Department of Environmental Protection. 2019-05-20. Retrieved 2019-05-21. 
  2. "Spud Data Report". Pennsylvania Department of Environmental Protection. 2019-04-30. Retrieved 2019-05-16. 
  3. "Oil and Gas Well Pad Report". Pennsylvania Department of Environmental Protection. 2019-05-20. Retrieved 2019-05-21. 
  4. "Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources". 2020-02-27. Retrieved 2020-02-27. 
  5. "Completion Reports - Stimulations". Pennsylvania Department of Conservation and Natural Resources. 2020-03-02. Retrieved 2020-03-02. 
  6. "Oil and Gas Compliance Report". Pennsylvania Department of Environmental Protection. 2019-05-20. Retrieved 2019-05-21.