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37-125-01707

Well Details

Well ID: 37-125-01707
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Cecil Township
Operator Name: PA TURNPIKE COMM
Well Pad ID:
Farm/Lease Name: PLUNKETT
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.307281
Longitude: -80.152831

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1988-10-03 OLD WELL
2019-01-09 Begin Plugging
2019-01-24 Finished Plugging
2020-02-14 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 ONEXXX PROD & EXPLORATION CORP 1,218.00 365 0.00 0 0.00 0
2010 ONEXXX PROD & EXPLORATION CORP 1,121.00 365 0.00 0 0.00 0
2011 ONEXXX PROD & EXPLORATION CORP 438.00 365 0.00 0 0.00 0
2012 ONEXXX PROD & EXPLORATION CORP 612.00 365 0.00 0 0.00 0
2013 ONEXXX PROD & EXPLORATION CORP 358.00 365 0.00 0 0.00 0
2014 ONEXXX PROD & EXPLORATION CORP 235.00 365 0.00 0 0.00 0
2015 ONEXXX PROD & EXPLORATION CORP 223.00 365 0.00 0 0.00 0
2016 ONEXXX PROD & EXPLORATION CORP 0.00 0 0.00 0 0.00 0
2017 ONEXXX PROD & EXPLORATION CORP 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2778950 Primary Facility 2018-09-24 Routine/Partial Inspection No Viols - Fac Inactive for Inspection Visited site of this shut in well (Beltway well #C2-2.1) to check status of recent repairs (9/7/18) by Yost per request of Turnpike Commission. This well may have been damaged by vandals who appear to have twisted the production casing and caused flow line to part. A leak was created in the annulus of the production casing-surface casing that Yost successfully repaired by filling annulus with concrete until well can be plugged. A low volume of gas is leaking past closed valve on parted flowline.
2830416 Primary Facility 2019-01-04 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Road into well and small pad built for rig mobilization next week.
2830940 Primary Facility 2019-01-14 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost attempted repeatedly to pull 3" from well, but 7" also coming. Loggers scheduled to perf bottom 200' of 3" so bottom hole plug can be set.
2830953 Primary Facility 2019-01-16 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost pulling 3" after cutting collar at 1753'. Have about 30 joints out so far. First joint had a 3' section of 7" attached. The 7" was rusted off of remaining string left in well.
2831009 Primary Facility 2019-01-17 Plugging(Includes Plugged/Mined Through) In Compliance with Policy TIMCO ran ccl/caliper log, found 6 5/8" casing down to 1542'. Will perf to surface.
2831024 Primary Facility 2019-01-22 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost warming up equipment, rig won't start (temperature is zero degrees). Set 60 sack plug last Friday. Will tag TOC and pump next plug later today.
2831114 Primary Facility 2019-01-24 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Yost plugged well to surface. Rig stacked off location nearby. Demobilizing.

For data sources see[6]

References