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37-117-21890

Well Details

Well ID: 37-117-21890
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Country: United States
State: Pennsylvania
County: Tioga
Municipality: Sullivan Township
Operator Name: SWEPI LP
Well Pad ID: 153979
Farm/Lease Name: COTTON HANLON 595 7H
License Status:
Spud Date: 2017-01-11
Permit Date: 2016-12-28
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.739553
Longitude: -76.959753

For data sources see[1][2][3]

Well History

Date Event
Deviated
2016-12-28 New Permit Application
2017-01-11 Performed Spud Operation
2017-06-01 Drilling Completion

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2017-08-08 2017-08-14 7,634 9,569,380 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 HCL Acid (3% to 7.5%) U.S. Well Services, LLC Bulk Acid Water 7732-18-5 97 0.066152 60612.8
Hydrogen Chloride 7647-01-0 7.5 0.005939 5441.85
WFRC-2100 U.S. Well Services, LLC Friction Reducer Hydrotreated Petroleum Distillates 64742-47-8 30 0.020796 19054.3
Cationic copolymer of acrylamide 69418-26-4 30 0.003078 2820.6
Alcohol Ethoxylate 68551-12-2 5 0.004279 3920.63
K-BAC 1020 U.S. Well Services, LLC Anti-Bacterial Agent 2,2-dibromo-3-nitrilopropionamide 10222-01-2 21 0.008606 7885.66
Polyethylene glycol 25322-68-3 50 0.00836 7660.29
Deionized Water 7732-18-5 30 0.005016 4596.17
SI-1200s U.S. Well Services, LLC Scale Inhibitor Alkyl Phosphonic Acid Proprietary 5 0.000847 776.454
Ammonia 7664-41-7 0.5 0.00013 118.797
Water Shell Carrier/Base Fluid Water 7732-18-5 100 87.1017 79,808,600.0
AI-303 U.S. Well Services, LLC Acid Corrosion Inhibitors Butyl cellosolve 111-76-2 20 0.00001300 12.0229
Ethylene glycol 107-21-1 40 0.00004200 38.1638
Cinnamaldehyde 104-55-2 20 0.00001500 13.7977
Acetophenone,thiourea,formaldehyde polymer 68527-49-1 5 0.00000400 3.336
Formic acid 64-18-6 20 0.00001500 13.344
Polyether 60828-78-6 10 0.00000700 6.672
HCL Acid (12.6%-17.5%) U.S. Well Services, LLC Bulk Acid Hydrogen Chloride 7647-01-0 17.5 0.023097 21162.8
Water 7732-18-5 87.4 0.099341 91023.4
Sand U.S. Well Services, LLC Proppant Crystalline Silica, quartz 14808-60-7 100 12.6525 11,593,100.0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2017 SWEPI LP 817,568.14 89 0.00 0 0.00 0
2018 SWEPI LP 2,393,408.18 363 0.00 0 0.00 0
2019 SWEPI LP 1,557,927.13 364 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2017 SWEPI LP Drilling Fluid Waste 108.20 Bbl REUSE (AT WELL PAD)
2017 SWEPI LP Waste Water Treatment Sludge 2.26 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123
2017 SWEPI LP Soil Contaminated by Oil & Gas Related Spills 22.10 Tons LANDFILL 301358
2017 SWEPI LP Produced Fluid 2,763.38 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC022
2017 SWEPI LP Synthetic Liner Materials 11.15 Tons LANDFILL 301358
2017 SWEPI LP Produced Fluid 2,127.59 Bbl REUSE (AT WELL PAD)
2017 SWEPI LP Other Oil & Gas Wastes 25.82 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2017 SWEPI LP Drill Cuttings 716.85 Tons LANDFILL 301358
2017 SWEPI LP Soil Contaminated by Oil 22.10 Tons LANDFILL 301358
2018 SWEPI LP Waste Water Treatment Sludge 31.50 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 SWEPI LP Produced Fluid 395.95 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2018 SWEPI LP Soil Contaminated by Oil & Gas Related Spills 1.26 Tons LANDFILL 301358
2018 SWEPI LP Produced Fluid 200.77 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 SWEPI LP Produced Fluid 5,542.39 Bbl REUSE (AT WELL PAD)
2018 SWEPI LP Produced Fluid 1,080.20 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC022
2018 SWEPI LP Soil Contaminated by Oil 1.26 Tons LANDFILL 301358
2019 SWEPI LP Produced Fluid 151.13 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2019 SWEPI LP Produced Fluid 40.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC022
2019 SWEPI LP Waste Water Treatment Sludge 6.38 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123
2019 SWEPI LP Produced Fluid 1,015.80 Bbl REUSE (AT WELL PAD)
2019 SWEPI LP Produced Fluid 168.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR119
2019 SWEPI LP Produced Fluid 48.81 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123
2019 SWEPI LP Produced Fluid 0.14 Bbl LANDFILL 301358

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2546657 Primary Facility 2016-12-21 Preoperation Inspection No Violations Noted slopes and soil stockpiles stabilized w/ straw. met w/ Scott Livermore on site. He said they plan to spud wells here on January 10, 2017.
2578090 Primary Facility 2017-04-03 Routine/Complete Inspection No Violations Noted
2584505 Primary Facility 2017-04-14 Routine/Partial Inspection No Violations Noted Water in basin 0.20 mS/cm Oakton PCSTestr 35
2596471 Primary Facility 2017-05-23 Routine/Complete Inspection No Violations Noted I arrived on-site @ 11:30 hrs. and met Brett McCoy, SWEPI company man. Ensign rig 192 on location drilling the 5H well; Mr. McCoy expected to be at TD sometime on Tuesday (currently @ 11460'). The foam berm had gravel added in drive-over areas, and in spots was compressing the berm. Mr. McCoy and I discussed some long-term solutions for this, including adding a hard berm such as a timber in these areas. As it was impossible to tell how high the berm still was, no violation will be issued for insufficient containment, but I recommend that this potential issue be taken into account for the move to the Lingle pad. I departed the site @ 12:20 hrs.
2602540 Primary Facility 2017-06-07 Drilling/Alteration No Violations Noted
2616559 Primary Facility 2017-07-18 Incident- Response to Accident or Event No Violations Noted Spoke with Dean Albright (SWEPI) on site. He and Keystone Clearwater explained that an open valve on the small pad allowed fracturing liquid flow through the plastic pipe to the battery of 30 wheelie trailers on liner containment on the well pad last night. The liquid overflowed from the top of 1 of the wheelie trailers. They removed most of that liquid; the residual liquid on the liner gave reading of "Or" (>19.99 mS/cm) with an Oakton PCSTestr 35. The highest reading of liquid off containment at this site was 0.90 mS/cm. US Well Services plan to start fracturing operations on the 5 Marcellus wells tonight.
2619548 Primary Facility 2017-07-21 Incident- Response to Accident or Event No Violations Noted EC readings with PCSTestr 35 (mS/cm): near water line breach--0.31, small pad containment--0.16, pad--0.75, well pad containment where fracturing liquid spilled on July 17, 2017 ( inspection record 2616184)--15.5.
2629816 Primary Facility 2017-08-23 Routine/Complete Inspection No Violations Noted I met Matt Jentsh and Rafael Diaz when I arrived on-site. Frac had ended earlier in the day, and most fracing equipment had already been removed from the site. A sitewide liner was in use with 4" foam berms for containment. On the west side of the pad between the foam berm and the soil berm, I discovered numerous puddles with elevated conductance (see sketch for details). A large volume of water showing elevated conductance (12-18mS/cm) was present in containment at the foam berm immediately next to these puddles. I continued field screening puddles on my way down to the sediment trap, finding puddles of 2.2 and 2.8 mS/cm on my way; conductance readings in the sediment trap were much lower (.595 mS/cm). I then discovered a large puddle (20-25 gallons) on the pad surface off the north side of the containment that showed elevated conductance (4.6-10.2 mS/cm). I informed Matt and Rafael of what I had found, and Matt immediately got a vac truck driver to go to the areas I located on the west side of the p
2638549 Primary Facility 2017-09-21 Administrative/File Review No Violations Noted I received a final analysis from the Departmen's Bureau of Laboratories on 9/21/2017 for sample #0939053, which I took at the Cotton Hanlon pad on 8/23/2017 from a puddle exhibiting elevated conductance. Elevated barium (781.8 mg/l), strontium (533.7 mg/l), and chlorides (11474 mg/l) indicate that a pollutional substance was released to the pad surface. Violations assigned to API # 117-21866.
2658387 Primary Facility 2017-11-08 Routine/Partial Inspection No Violations Noted I spoke with Kevin Morgan (SWEPI , Flowback OSR) on site. He said the row of trailers (photo) contains production liquid form the 5 Marcellus wells on site.

Air temp: 32F. Some ice on top of puddles today. Electrical conductivity (mS/cm) readings taken with an Oakton PCSTestr 35. JLP

2668644 Primary Facility 2017-12-06 Routine/Partial Inspection No Violations Noted
2677780 Primary Facility 2018-01-03 Routine/Partial Inspection No Violations Noted No electrical conductivity readings today because I did not see any standing liquid on site. JLP
2696285 Primary Facility 2018-02-21 Routine/Complete Inspection No Violations Noted At time of inspection all the wells on the pad were being flowed back

Unable to check annulus vents for combustible gas at time of inspection due to flowback being done

2706156 Primary Facility 2018-03-15 Routine/Partial Inspection No Violations Noted Site snow covered. I did not see any standing liquid on site. SWEPI inspection log in mailbox near pRoduction tanks lists last inspection on March 12, 2018. Air temp 29F. JLP
2788362 Primary Facility 2018-10-03 Site Restoration No Violations Noted The DEP conducted a RESTORATION inspection of SWEPI's Cotton Hanlon 595 Well Pad in Sullivan Twp, Tioga County on 10/3/2018 at 1400 hours. The weather was 64 degrees, 71% humidity and cloudy.

The inspection was conducted in response to a Notice of Termination received by the DEP. The pad appears very well vegetated and the pony pad to the North is completely restored. All PCSM BMPs are in place and appear to be functioning properly. No temporary E&S BMPs were observed. There are currently 5 producing wells onsite with two highland production tanks.

This Notice of Termination is recommended for approval. No violations noted at this time.

I departed the site at 1435.

For data sources see[8]

References