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37-117-21793

Well Details

Well ID: 37-117-21793
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Country: United States
State: Pennsylvania
County: Tioga
Municipality: Osceola Township
Operator Name: SWEPI LP
Well Pad ID:
Farm/Lease Name: STANLEY 1106 25H
License Status:
Spud Date:
Permit Date: 2015-08-06
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 41.943094
Longitude: -77.356236

For data sources see[1][2][3]

Well History

Date Event
2015-08-06 New Permit Application

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2446973 Primary Facility 2016-02-02 Incident- Response to Accident or Event No Violations Noted The Department inspected the SWEPI LP - Stanley 1106 (ESX10-117-0243) located in Osceola Twp., Tioga Co. in response to notification of a spill by Patrick Bernethy, Environmental/Regulatory Tech from Shell Appalachia. Mr. Bernethy contact the WSQ @ 1150 hours on 1/26/2016 to notify the Department that SWEPI LP removed the temporary containment liner used during well completion activities on the 23 H well (API#117-21792) at the Stanley 1106 pad. As part of SWEPI LP’s standard procedures, soil conductivity readings were collected from the pad following the liner removal. Soil conductivity measurement points exhibited readings above background in the area of the temporary liner; approximately 6-8 mS. SWEPI LP was not notified during completion activities of any spills by the completions contractor, US Well Services.
2487542 Primary Facility 2016-05-26 Routine/Complete Inspection No Violations Noted he Department of Environmental Protection (DEP) inspected the SWEPI LP – Stanley 1106 site, in Osceola Twp., Tioga Co. on 5/26/2016 @0950 hours, in response to notification by SWEPI of suspected vandalism. The weather was mostly cloudy 75 degrees with winds S 7mph. SWEPI Env. Coordinator, Pat Bernethy stated the production tank that was installed for the 23H well appeared to have a faulty gasket around the heater. This had allowed production fluid to seep into the permanent causing elevated conductivity in the accumulated fluid. The gasket was repaired and the fluid was removed from the containment. According to Mr. Bernethy ~1-2 weeks later a small area of damp soil appeared to be coming from underneath the permanent containment. The gravel inside the containment was removed and the liner was inspected for holes. Approximately 8 puncture holes and 1 large gash were observed along a 5 foot length of containment. SWEPI stated it suspects it was an act of vandalism. There is no gate at the site entrance and no
2580727 Primary Facility 2017-04-10 Routine/Complete Inspection No Violations Noted The DEP inspected the SWEPI LP Stanley 1106 well site on 4/10/2017 @1000 hours. The weather was 60 degrees and sunny. A restoration of the tank pad and installation of post-construction Stormwater management BMPs was ongoing at the time of the inspection. Perimeter BMPs appeared to be installed around the earth disturbance area. Two wells were observed in production on the main pad. No fluid was observed in secondary containment surrounding the baker tanks. No puddles were observed onsite. No violation are noted at this time. I departed the site @1100 hours.

For data sources see[5]

References