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37-117-21322

Well Details

Well ID: 37-117-21322
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Country: United States
State: Pennsylvania
County: Tioga
Municipality: Delmar Township
Operator Name: SWEPI LP
Well Pad ID: 148949
Farm/Lease Name: NESTOR E 551 5H
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date: 2011-09-28
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.769206
Longitude: -77.298092

For data sources see[1][2][3]

Well History

Date Event
2011-09-28 New Permit Application
2011-10-11 Performed Spud Operation
2012-02-07 Drilling Completion
2012-12-13 DEVIATED
2015-03-15 Drilling Completion
2015-07-01 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2011 SWEPI LP 0.00 0 0.00 0 0.00 0
2012 SWEPI LP 0.00 0 0.00 0 0.00 0
2013 SWEPI LP 0.00 0 0.00 0 0.00 0
2014 SWEPI LP 0.00 0 0.00 0 0.00 0
2015 SWEPI LP 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2012 SWEPI LP Produced Fluid 34.20 Bbl REUSE OTHER THAN ROAD SPREADING
2012 SWEPI LP Fracing Fluid Waste 8,008.87 Bbl REUSE OTHER THAN ROAD SPREADING
2012 SWEPI LP Drill Cuttings 608.28 Tons LANDFILL 9312
2013 SWEPI LP Produced Fluid 136.48 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR119
2013 SWEPI LP Fracing Fluid Waste 20.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR119
2013 SWEPI LP Produced Fluid 5,898.35 Bbl REUSE OTHER THAN ROAD SPREADING
2013 SWEPI LP Produced Fluid 763.15 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2013 SWEPI LP Fracing Fluid Waste 66.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2013 SWEPI LP Fracing Fluid Waste 14.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 SWEPI LP Produced Fluid 39.18 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123SW018
2014 SWEPI LP Produced Fluid 502.00 Bbl REUSE OTHER THAN ROAD SPREADING
2015 SWEPI LP Produced Fluid 80.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC018
2015 SWEPI LP Produced Fluid 419.40 Bbl REUSE OTHER THAN ROAD SPREADING
2015 SWEPI LP Produced Fluid 18.81 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NC010
2015 SWEPI LP Produced Fluid 43.33 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2038318 Primary Facility 2012-01-26 Drilling/Alteration No Violations Noted
2112565 Primary Facility 2012-11-01 Routine/Complete Inspection No Violations Noted
2248804 Primary Facility 2014-02-25 Routine/Complete Inspection No Violations Noted
2306503 Primary Facility 2014-09-15 Routine/Complete Inspection No Violations Noted
2497042 Primary Facility 2016-06-14 Routine/Complete Inspection No Violations Noted Routine inspection. Well site is permanently stabilized with exception of two slumped areas on the north fill slope of well pad-slumps are to be repaired and stabilized. Pad surface was dry and stable. 1H - 3H and 6H are in production. The 5H was plugged in March 2015. TLT
2772883 Primary Facility 2018-08-27 Site Restoration No Violations Noted The DEP conducted a RESTORATION inspection of the SWEPI LP - Nestor 551 well site located in Delmar Twp, Tioga Co. on 8/27/2018 1330 hours. The weather was 78 degrees and sunny. Present for the inspection were myself and Korey Starkey, DEP Env. Trainee.

The access road, well pad, and surrounding controls were observed during the inspection. The pony pad has been removed and the area restored. The well pad has been reduced to ~275'x400'. The reclaimed areas appear stabilized by 70% perennial vegetative cover. No erosion or sedimentation was observed. No temporary BMPs were observed onsite.

Due to conditions observed onsite during the course of this inspection, this NOT is recommended for approval.

No violations are noted at this time. We departed the site at 1400 hours.

For data sources see[7]

References