X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-117-20189

Well Details

Well ID: 37-117-20189
Loading map...
Country: United States
State: Pennsylvania
County: Tioga
Municipality: Clymer Township
Operator Name:
Well Pad ID:
Farm/Lease Name: WH HAUPT CO N2010S
License Status: INACTIVE
Spud Date:
Permit Date: 2008-02-08
Well Type: STORAGE WELL
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.865183
Longitude: -77.531344

For data sources see[1][2][3]

Well History

Date Event
2008-02-08 New Permit Application
2008-04-10 Performed Spud Operation
2008-12-17 Drilling Completion
2009-10-15 Perforation
2014-03-28 REWORKED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2009 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2010 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2011 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2012 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2013 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2014 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2015 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2016 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2017 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2018 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1698713 Primary Facility 2008-04-10 Drilling/Alteration No Violations Noted
1698714 Primary Facility 2008-04-09 Drilling/Alteration No Violations Noted
1698715 Primary Facility 2008-04-08 Drilling/Alteration No Violations Noted
1699464 Primary Facility 2008-04-14 Drilling/Alteration No Violations Noted
1699476 Primary Facility 2008-04-15 Drilling/Alteration No Violations Noted
1700555 Primary Facility 2008-04-17 Drilling/Alteration No Violations Noted
1742526 Primary Facility 2008-10-14 Routine/Complete Inspection Violation(s) Noted
1750722 Primary Facility 2008-11-18 Routine/Complete Inspection Outstanding Violations - No Viols Req'd
1813907 Primary Facility 2009-07-20 Routine/Complete Inspection Violation(s) Noted Drill waste leaching off site, potentially from leaking pit.
1819771 Primary Facility 2009-08-06 Routine/Complete Inspection No Violations Noted I met with Ms. Sheri Franz, Dominion Consulting Engineer, and Mr. Dave Wills, Consultant, regarding the apparent drill cutting pit leachate that is seeping from the fill slope. Ms. Franz indicated that Dominion intends on excavating and disposing of the pit contents in the near future. In addition, the affected water supplies below the site were also discussed. Ms. Franz indicated that Dominion will contact a company to explore treatment options for the affected water supplies. I requested a schedule of implementation for the pit remediation and drinking water restoration projects. Ms. Franz indicated that she will provide a schedule in the near future.
1821119 Primary Facility 2009-08-18 Compliance Evaluation No Violations Noted This site has been completely restored and vegetative cover is greater than 70%. Therefore, the previously documented E&S violations enter under inspection # 1750722 can now be resolved. The suspect leaking pit violation remains open and Dominion intends to excavate and properly dispose of the pit contents in the near future.
1842115 Primary Facility 2009-11-04 Routine/Complete Inspection No Violations Noted
1921035 Primary Facility 2010-10-19 Routine/Complete Inspection No Violations Noted
2026064 Primary Facility 2011-11-17 Routine/Complete Inspection No Violations Noted
2121026 Primary Facility 2012-11-13 Routine/Complete Inspection No Violations Noted
2214440 Primary Facility 2013-10-08 Routine/Complete Inspection No Violations Noted
2312949 Primary Facility 2014-10-07 Routine/Complete Inspection No Violations Noted
2411660 Primary Facility 2015-09-28 Routine/Complete Inspection No Violations Noted
2529096 Primary Facility 2016-10-18 Routine/Complete Inspection No Violations Noted
2641718 Primary Facility 2017-09-25 Routine/Complete Inspection No Violations Noted
2777856 Primary Facility 2018-09-18 Routine/Complete Inspection No Violations Noted Date: 9/18-19/2018

CASING PSI: 1.730

MAX ALLOWABLE PSI: 2,160

VENT: 1. 0 scf/day 2. 0 scf/day 3. 0 scf/day

  • NM= Not Measurable*
  • 0= Not Venting*
  • Scf/day= Standard Cubic Feet Per Day*

VENT: 1. 0.8¿ H2O on 1/8¿ plate 2. ¿ H2O on ¿ plate 3. ¿ H2O on ¿ plate


STATUS: I

  • I= In-Line*
  • P= Plugged*
  • S= Shut in*
  • TP= Temp Plugged*
  • OW= Observation Well*

COMMENTS: New paint 2018

  • TJ/WH= Top Joint/Well Head*

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1742526 549396 10/14/2008 2008-10-14 102.4INADPLN - E&S Plan not adequate Administrative See Insp ID 1813907 done 7/20/09, E&S viol corrected. MBC 8/12/09
1813907 567341 07/20/2009 2009-07-20 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used Administrative CSL 402
1813907 567342 07/20/2009 2009-07-20 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used Administrative SWMA 6018.301
1813907 567343 07/20/2009 2009-07-20 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used Administrative CSL 307

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
549396 239337 NOV - Notice of Violation Comply/Closed 2009-07-20
567341 248930 NOV - Notice of Violation Comply/Closed 2011-09-13
567342 248930 NOV - Notice of Violation Comply/Closed 2011-09-13
567343 248930 NOV - Notice of Violation Comply/Closed 2011-09-13

For data sources see[6]

References