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37-117-00034

Well Details

Well ID: 37-117-00034
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Country: United States
State: Pennsylvania
County: Tioga
Municipality: Farmington Township
Operator Name: UGI STORAGE CO
Well Pad ID:
Farm/Lease Name: HOYT #2 (TW 103) 2147
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: STORAGE WELL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.918750
Longitude: -77.283642

For data sources see[1][2][3]

Well History

Date Event
1931-11-15 Drilling Completion
1932-01-01 OLD WELL
1954-01-01 Drilling Completion
2001-03-09 CONVERTED TO STORAGE (GAS)
2017-10-16 Begin Plugging
2017-10-23 Finished Plugging
2019-04-04 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 NORTH PENN GAS CO 0.00 0 0.00 0 0.00 0
1995 NORTH PENN GAS CO 0.00 0 0.00 0 0.00 0
1996 NORTH PENN GAS CO 0.00 0 0.00 0 0.00 0
2017 UGI STORAGE CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1066056 Primary Facility 2001-10-04 Routine/Complete Inspection No Violations Noted
1085748 Primary Facility 2001-12-19 Routine/Complete Inspection No Violations Noted
1086324 Primary Facility 2001-12-27 Routine/Complete Inspection No Violations Noted
1107986 Primary Facility 2002-03-13 Routine/Complete Inspection No Violations Noted
1179625 Primary Facility 2002-10-22 Routine/Complete Inspection No Violations Noted
1179626 Primary Facility 2002-10-22 Routine/Complete Inspection No Violations Noted
1384285 Primary Facility 2004-10-05 Routine/Complete Inspection No Violations Noted
1436099 Primary Facility 2005-03-17 Routine/Complete Inspection No Violations Noted
1490059 Primary Facility 2005-10-25 Routine/Complete Inspection No Violations Noted
1490076 Primary Facility 2005-10-21 Routine/Complete Inspection No Violations Noted
1493228 Primary Facility 2005-11-01 Routine/Complete Inspection No Violations Noted
1493293 Primary Facility 2005-11-02 Routine/Complete Inspection No Violations Noted
1497827 Primary Facility 2005-11-21 Routine/Complete Inspection No Violations Noted
1497846 Primary Facility 2005-11-07 Routine/Complete Inspection No Violations Noted
1499843 Primary Facility 2005-12-01 Routine/Complete Inspection No Violations Noted
1504786 Primary Facility 2006-01-03 Routine/Complete Inspection No Violations Noted
1508954 Primary Facility 2006-01-20 Routine/Complete Inspection No Violations Noted
1508963 Primary Facility 2006-01-23 Routine/Complete Inspection No Violations Noted
1509782 Primary Facility 2006-01-26 Routine/Complete Inspection No Violations Noted
1512211 Primary Facility 2006-02-03 Routine/Complete Inspection No Violations Noted
1513776 Primary Facility 2006-02-06 Routine/Complete Inspection No Violations Noted
1514471 Primary Facility 2006-02-10 Routine/Complete Inspection No Violations Noted
1514487 Primary Facility 2006-02-08 Routine/Complete Inspection No Violations Noted
1517874 Primary Facility 2006-02-20 Routine/Complete Inspection No Violations Noted
1522283 Primary Facility 2006-03-13 Routine/Complete Inspection No Violations Noted
1523966 Primary Facility 2006-03-16 Routine/Complete Inspection No Violations Noted
1532218 Primary Facility 2006-04-24 Routine/Complete Inspection No Violations Noted
1533710 Primary Facility 2006-05-02 Routine/Complete Inspection No Violations Noted
1559446 Primary Facility 2006-08-22 Routine/Complete Inspection No Violations Noted
1569106 Primary Facility 2006-10-03 Routine/Complete Inspection No Violations Noted
1576576 Primary Facility 2006-11-02 Routine/Complete Inspection No Violations Noted
1578626 Primary Facility 2006-11-07 Routine/Complete Inspection No Violations Noted
1587267 Primary Facility 2006-12-12 Routine/Complete Inspection No Violations Noted
1587449 Primary Facility 2006-12-20 Routine/Complete Inspection No Violations Noted
1590330 Primary Facility 2007-01-04 Routine/Complete Inspection No Violations Noted
1593008 Primary Facility 2007-01-12 Routine/Complete Inspection No Violations Noted
1593010 Primary Facility 2007-01-11 Routine/Complete Inspection No Violations Noted
1594285 Primary Facility 2007-01-19 Routine/Complete Inspection No Violations Noted
1596528 Primary Facility 2007-01-30 Routine/Complete Inspection No Violations Noted
1598422 Primary Facility 2007-02-06 Routine/Complete Inspection No Violations Noted
1601292 Primary Facility 2007-02-20 Routine/Complete Inspection No Violations Noted
1605032 Primary Facility 2007-03-05 Routine/Complete Inspection No Violations Noted
1609395 Primary Facility 2007-03-20 Routine/Complete Inspection No Violations Noted
1613427 Primary Facility 2007-04-02 Routine/Complete Inspection No Violations Noted
1614137 Primary Facility 2007-04-09 Routine/Complete Inspection No Violations Noted
1617016 Primary Facility 2007-04-17 Routine/Complete Inspection No Violations Noted
1624706 Primary Facility 2007-05-22 Routine/Complete Inspection No Violations Noted
1637504 Primary Facility 2007-07-12 Routine/Complete Inspection No Violations Noted
1644481 Primary Facility 2007-08-15 Routine/Complete Inspection No Violations Noted
1662897 Primary Facility 2007-10-29 Routine/Complete Inspection No Violations Noted
1673500 Primary Facility 2007-12-14 Routine/Complete Inspection No Violations Noted
1688413 Primary Facility 2008-02-29 Routine/Complete Inspection No Violations Noted
1699505 Primary Facility 2008-04-15 Routine/Complete Inspection No Violations Noted
1701774 Primary Facility 2008-04-23 Routine/Complete Inspection No Violations Noted
1705337 Primary Facility 2008-05-08 Routine/Complete Inspection No Violations Noted
1709651 Primary Facility 2008-05-28 Routine/Complete Inspection No Violations Noted
1723674 Primary Facility 2008-07-22 Routine/Complete Inspection No Violations Noted
1750442 Primary Facility 2008-11-12 Routine/Complete Inspection No Violations Noted
1842078 Primary Facility 2009-11-03 Routine/Complete Inspection No Violations Noted
1920835 Primary Facility 2010-10-13 Routine/Complete Inspection No Violations Noted
2024532 Primary Facility 2011-11-03 Routine/Complete Inspection No Violations Noted
2123496 Primary Facility 2012-11-14 Routine/Complete Inspection No Violations Noted
2214669 Primary Facility 2013-10-10 Routine/Complete Inspection No Violations Noted
2323609 Primary Facility 2014-10-29 Routine/Complete Inspection No Violations Noted
2416324 Primary Facility 2015-10-16 Routine/Complete Inspection No Violations Noted
2536178 Primary Facility 2016-11-03 Routine/Complete Inspection No Violations Noted
2643456 Primary Facility 2017-09-19 Routine/Complete Inspection No Violations Noted
2649096 Primary Facility 2017-10-18 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig on location for plugging. WL Running in hole to tag TOC after setting ~1000' cement plug on top of bridge plug in 5 1/2". TOC will be estimated at 2500'. TOC on the backside at 3100'. 5 1/2" is dead, minor venting on annulus. They'll pull 5 1/2"' and isolate casing stub w/ cmt plug, gel uphole to shoe plug and fill remainder of well with gravel. No obvious issues observed.
2651898 Primary Facility 2017-10-25 Plugging(Includes Plugged/Mined Through) No Violations Noted Routine inspection of a recently plugged well. Rig has pulled off location following plug and abandonment. The well is buried and there is a candycane vent monument installed on the well. I checked the vent for gas. No gas was detected with an altair 5x gas meter. No gas was detected at ground level around the event. No obvious issues were observed.
2652401 Primary Facility 2017-10-26 Administrative/File Review No Violations Noted October 26, 2017: Certificate of Well Plugging for the Hoyt 2 (117-00034) has been received, reviewed, signed, and sent to file.
2713759 Primary Facility 2018-03-29 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of this plugged vertical well was conducted March 29, 2018. At the time of inspection, there was a 2" candy cane vent pipe installed on top of the plugged well. There was no visual or audible flow coming from the vent. No gas was detected with an Altair 5x gas meter at the opening in the 2" vent pipe. Combustible gas was detected near ground level next to the vent. I contacted the operator who plugged the well to inform them of my findings. The source of the gas is unknown, and the operator is planning to investigate by digging out the cellar to determine the cause of the venting outside the vent pipe.
2715332 Primary Facility 2018-04-06 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of this plugged, deep vertical well was conducted April 6, 2018. At the time of inspection; the plugged well monument consists of a 2" candy cane vent and marker plate. No flow was seen coming from inside the vent pipe. A trace of gas was detected with an Altair 5x gas meter inside the vent. The 2" vent pipe is installed in or on the 8 5/8" casing which is buried and not observable at the time. There was small, persistent bubbling observed in standing water in the immediate area outside the 2" vent pipe. The proximity of the bubbling to the vent pipe and comparable venting inside and outside the vent would seemingly indicate the bubbles are coming from inside the 8 5/8" casing, which may not be made up to the vent properly. This is not conclusive since the casing cannot be seen, and the operator plans to investigate further.
2726687 Primary Facility 2018-05-03 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of this deep, vertical, plugged well was conducted May 4th, 2018. At the time of inspection, the well has a 2" candy cane vent pipe with marker erected as a plugged well monument. No gas was detected at ground level outside of the vent pipe where gas was previously detected. The operator has properly made up the vent pipe to casing below ground level, and now the wellbore is being vented entirely out of the vent pipe and no longer leaking at the connection where the casing is made up to the vent. No pressure build up was felt at the mouth of the vent. A trace of gas was detected, and audible bubbling was heard coming from inside the vent.
2780973 Primary Facility 2018-09-25 Routine/Complete Inspection No Violations Noted Date: 9/25/2018

CASING PSI: 0

MAX ALLOWABLE PSI: 1,680

VENT: 1. 21 scf/day 2. scf/day 3. scf/day

  • NM= Not Measurable*
  • 0= Not Venting*
  • Scf/day= Standard Cubic Feet Per Day*

VENT: 1. 0.4¿ H2O on 1/8th¿ plate 2. ¿ H2O on 1/8th¿ plate 3. ¿ H2O on 1/8th¿ plate


STATUS: OW

  • I= In-Line*
  • P= Plugged*
  • S= Shut in*
  • TP= Temp Plugged*
  • OW= Observation Well*

COMMENTS:

  • TJ/WH= Top Joint/Well Head*
2790684 Primary Facility 2018-10-17 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of this plugged deep vertical well was conducted 10/18/2018, approximately one year after final plug and abandonment. There is a 2" candy cane vent pipe installed as a plugged well monument. There were no open holes, discharges, or visible venting observed. No obvious issues were observed.
2840861 Primary Facility 2019-02-14 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine, post-plugging, follow-up inspection of this plugged storage well was conducted February 14, 2019. At the time of inspection, the well has a 2" candy cane vent with marker plate erected as a plugged well monument. No visible venting was observed. Audible venting could be heard coming from inside the vent when standing close to it. No pressure could be felt at the vent. A field reading with an Altair 5x gas meter gave unsustained readings of ~0-60 LEL at the mouth of the vent and diminished to 0 LEL at 1" from the mouth of the vent. The location was snow-covered. No active discharge was observed. Spots of discoloration were observed in the snow surrounding the vent. The snow beneath the spots of discoloration appeared clean.
682412 Primary Facility 1988-10-28 Routine/Complete Inspection No Violations Noted
682413 Primary Facility 1989-03-17 Routine/Complete Inspection No Violations Noted
682414 Primary Facility 1989-10-03 Routine/Complete Inspection No Violations Noted
683195 Primary Facility 1990-11-08 Routine/Complete Inspection No Violations Noted
684100 Primary Facility 1991-10-15 Routine/Complete Inspection No Violations Noted
684692 Primary Facility 1992-11-17 Routine/Complete Inspection No Violations Noted
685191 Primary Facility 1993-10-19 Routine/Complete Inspection No Violations Noted
686076 Primary Facility 1994-10-25 Routine/Complete Inspection No Violations Noted
686910 Primary Facility 1995-10-23 Routine/Complete Inspection No Violations Noted
687842 Primary Facility 1996-10-24 Routine/Complete Inspection No Violations Noted
688427 Primary Facility 1997-10-21 Routine/Complete Inspection No Violations Noted
688512 Primary Facility 1997-10-21 Routine/Complete Inspection No Violations Noted
689388 Primary Facility 1998-11-17 Routine/Complete Inspection No Violations Noted
895951 Primary Facility 1999-11-15 Routine/Complete Inspection No Violations Noted
973376 Primary Facility 2000-10-12 Routine/Complete Inspection No Violations Noted

For data sources see[6]

References