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37-115-20163

Well Details

Well ID: 37-115-20163
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Country: United States
State: Pennsylvania
County: Susquehanna
Municipality: Dimock Township
Operator Name: CABOT OIL & GAS CORP
Well Pad ID: 148407
Farm/Lease Name: GESFORD 7H NW
License Status:
Spud Date:
Permit Date: 2009-04-30
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.738692
Longitude: -75.879050

For data sources see[1][2][3]

Well History

Date Event
2009-04-30 New Permit Application
2009-06-13 Performed Spud Operation
2009-06-22 Drilling Completion
2009-09-12 Perforation
2009-11-12 Performed Stimulation
2010-10-01 DEVIATED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
2009-11-12 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 CABOT OIL & GAS CORP 241712.00 36 0.00 0 0.00 0
2010 CABOT OIL & GAS CORP 1,175,329.50 293 0.00 0 0.00 0
2011 CABOT OIL & GAS CORP 621,833.18 322 0.00 0 0.00 0
2012 CABOT OIL & GAS CORP 411,383.16 293 0.00 0 0.00 0
2013 CABOT OIL & GAS CORP 520,977.01 364 0.00 0 0.00 0
2014 CABOT OIL & GAS CORP 447,047.53 346 0.00 0 0.00 0
2015 CABOT OIL & GAS CORP 236,132.26 357 0.00 0 0.00 0
2016 CABOT OIL & GAS CORP 373,084.33 366 0.00 0 0.00 0
2017 CABOT OIL & GAS CORP 279,255.73 362 0.00 0 0.00 0
2018 CABOT OIL & GAS CORP 249,786.00 365 0.00 0 0.00 0
2019 CABOT OIL & GAS CORP 154,483.00 172 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 CABOT OIL & GAS CORP Drilling Fluid Waste 224.50 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2010 CABOT OIL & GAS CORP Produced Fluid 202.89 Bbl REUSE OTHER THAN ROAD SPREADING
2010 CABOT OIL & GAS CORP Basic Sediment 2.59 Bbl LANDFILL 101534
2010 CABOT OIL & GAS CORP Drilling Fluid Waste 135.10 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2010 CABOT OIL & GAS CORP Drill Cuttings 68.00 Tons CENTRALIZED TREATMENT PLANT FOR RECYCLE 101247
2010 CABOT OIL & GAS CORP Drill Cuttings 19.20 Tons LANDFILL NY # 50S08
2010 CABOT OIL & GAS CORP Drill Cuttings 110.60 Tons CENTRALIZED TREATMENT PLANT FOR RECYCLE 8-4630-00010/00
2010 CABOT OIL & GAS CORP Drill Cuttings 110.60 Tons LANDFILL NY # 02S17
2010 CABOT OIL & GAS CORP Drill Cuttings 1.40 Tons LANDFILL 100955
2011 CABOT OIL & GAS CORP Basic Sediment 0.41 Bbl LANDFILL 100081
2011 CABOT OIL & GAS CORP Basic Sediment 0.56 Bbl LANDFILL 101534
2011 CABOT OIL & GAS CORP Produced Fluid 159.11 Bbl REUSE OTHER THAN ROAD SPREADING
2012 CABOT OIL & GAS CORP Produced Fluid 79.50 Bbl REUSE OTHER THAN ROAD SPREADING
2012 CABOT OIL & GAS CORP Basic Sediment 0.81 Bbl LANDFILL 101534
2013 CABOT OIL & GAS CORP Produced Fluid 59.79 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NE002
2013 CABOT OIL & GAS CORP Produced Fluid 35.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NE002
2014 CABOT OIL & GAS CORP Produced Fluid 123.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NE002
2015 CABOT OIL & GAS CORP Produced Fluid 76.50 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NE002
2015 CABOT OIL & GAS CORP Produced Fluid 3.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NE001
2016 CABOT OIL & GAS CORP Produced Fluid 65.85 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NE002
2016 CABOT OIL & GAS CORP Produced Fluid 82.32 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NE002
2017 CABOT OIL & GAS CORP Produced Fluid 60.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NE002
2018 CABOT OIL & GAS CORP Servicing Fluid 0.07 Tons RESIDUAL WASTE PROCESSING FACILITY 301333
2018 CABOT OIL & GAS CORP Produced Fluid 35.08 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NE002
2018 CABOT OIL & GAS CORP Produced Fluid 9.81 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC018
2019 CABOT OIL & GAS CORP Synthetic Liner Materials 8.49 Tons LANDFILL 101247
2019 CABOT OIL & GAS CORP Produced Fluid 63.65 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NE002
2019 CABOT OIL & GAS CORP Synthetic Liner Materials 1.53 Tons RESIDUAL WASTE TRANSFER FACILITY 101714

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1806418 Primary Facility 2009-06-19 Drilling/Alteration No Violations Noted Drilling depth at time of inspection 2340'. No freshwater encountered in tophole. E/S controls in place and working properly. Freeboard in pit was 6 - 7'.
1825893 Primary Facility 2009-08-27 Drilling/Alteration No Violations Noted At time of inspection, drilling rig SWJ #14 was on site. I met with the Company Man who indicated TD had been reached TD at a depth of 9919'. The Company Man indicated they had attempted to set the 4-1/2" production casing with 6 packers but failed due to the hole collapsing in. As a result, the casing was tripped out of hole. In the meatime,the production casing was being re-cleaned while waiting on a special bit to arrive on site which will be used to ream and clean out the hole. The drawworks was also being repaired at the time of inspection.
1833401 Primary Facility 2009-09-25 Follow-up Inspection No Violations Noted An existing road was used to access the well site. The road and drill pad are stoned with limestone. The Site ID sign and E/S Plan were present at the entrance of the access road.
1845178 Primary Facility 2009-11-13 Follow-up Inspection Viol(s) Noted & Immediately Corrected Spill occured at 5:30 pm on 11/12/09. Reported to Bob B. of EM. Cabot moving tote of Crosslinker which fell off forks. Approx. 15-20 gallons spilled onto pad. Area immediately scraped clean with backhoe and material placed in lined rolloff. Approx.. 8' x 8' area impacted. Copy of MSDS provided by Cabot. See file for more information. Well in proces of being fracced. Violation of 78.54. Violations immediately corrected. No outstanding violations exist at this time.
1845648 Primary Facility 2009-11-10 Routine/Complete Inspection No Violations Noted
1858569 Primary Facility 2009-10-20 Complaint Inspection No Violations Noted
1959398 Primary Facility 2011-03-22 Routine/Complete Inspection No Violations Noted
2431683 Primary Facility 2015-12-04 Site Restoration No Violations Noted Verify square footage of Gesford K P2 well pad for the notice of termination of the Erosion and Sedimentation permit.
2481812 Primary Facility 2016-04-26 Routine/Partial Inspection No Violations Noted

The Department conducted a Routine Partial Inspection at the Gesford Pad 2 Well Site. The E&S Inspection Log indicated that Mike Brilla (TEC) completed a Post Rain Event Inspection on 12/15/15. At the time of the inspection, the site appeared to meet temporary stabilization requirements. It was noted that there was black material alongside the lines running to the production tanks. Also, there was what appeared to be recently disturbed pad surface adjacent to the production containment.

2548418 Primary Facility 2016-12-01 Routine/Complete Inspection No Violations Noted The Department was on site to conduct a Routine Complete inspection for the Gesford P2 well site (Erosion and sediment permit 58-09-802). The wells associated with this site are as follows:

2V 115-20033 7H 115-20163

The site was well vegetated with perennial grass, and there were no erosion or sedimentation issues with the site. This site is stable at this time, and there were no issues to report.

There were no violations


If there are any questions please feel free to contact me at (570) 346-5539

2771576 Primary Facility 2018-09-04 Routine/Complete Inspection Pending Arrived on location at 09:00. Onsite to initiate a 72 hr. pressure build up test "PBUT" on the annuli of the Gesford 2V and 7H wells. Both wells annuli have been isolated and were venting to onsite poly vent tanks.

- Upon arrival I met with Cabot O&G Rep. Jeremy Rapp. Prior to shutting in wells annuli, initial gas screenings and flow checks were performed using the Depts. Altair 5X gas meter, calibrated this morning, and Cabots' RS-484 Alicat "Whisper" flow meter. Pre-shut in screenings showed gas and flow detected at both wells cemented annuli. - 2V: (9 5/8"x 7") = 100% CH4; 69.8 cf/d * - 7H: (13 3/8"x 9 5/8") = 100% CH4; 435 cf/d * Both wells annuli were shut in to start 72 hr PBUT at approx. 09:15. We will meet back on location to conclude PBUT on Friday 9/7/18 and collect gas samples off annuli, where present, for isotopic analysis. Left location at 09:40. (Please see attached well bore diagrams for the Gesford 2V and 7H wells for further details.)

2772767 Primary Facility 2018-09-07 Routine/Complete Inspection Pending Arrived on location at 09:00. Onsite to conclude the 72 hr. pressure build up test "PBUT" being performed on the annuli of the Gesford 2V and 7H wells. Upon arrival I met with Cabot O&G Rep. Jeremy Rapp. and Selman and Associates Rep. Kaydee Oliver.

- At approx. 09:15 the ending PBUT pressures were checked by Mr. Rapp using a Crystal digital pressure gauge. Ending pressures are listed below: - 2V: (7"x 4 1/2") = -5.9 psi.; (9 5/8"x 7") = 94.7 psi.* - 7H: (9 5/8"x 4 1/2") = 0.0 psi.; (13 3/8"x 9 5/8") = 162.7 psi.*

(*) The presence of venting gas and pressure detected in the Gesford 2H and 7H cemented annuli appears to be indicative of Defective Cement and/or Defective Casing. Since this condition was simultaneously detected by the Dept. and Cabot O&G, no violation for 78a.86 will be issued at this time. Please respond to the Dept. within 30 days of receipt of this inspection with a plan how Cabot O&G plans to address this defective condition per 78a.86.

While checking ending PBUT pressures, continuous bub

2785743 Primary Facility 2018-09-24 Follow-up Inspection Pending Arrived on location at 09:00. Onsite to conclude this repeat / follow-up 72 hr. pressure build up test "PBUT" being performed on the annuli of the Gesford 2V and 7H wells. Since conclusion of the last PBUT on these wells, concluded on 9/7/18, Cabot has emptied well cellars, verified and tightened all annular vent line connections. On 9/21/18 Dept. Rep., Eric Rooney met with Cabot Reps. to perform initial gas checks and annular vent flows prior to starting PBUT. (See Erics notes of this insp. attached, Photo #2). Summary of detected results below:

- Gesford 7H: 4 ½¿ x 9 5/8¿ annulus = 100% LEL, 100% methane, flow = 422 cf/d, annulus was shut in at 0932 hours - Gesford 2V: 7¿ x 9 5/8¿ annulus = 100 LEL, 100% methane, flow = 71 cf/d, annulus was shut in at 0945 hours

                2V: 4 ½¿ x 7¿ annulus = 100% LEL, 3% methane peak dissipated to 0, flow = fluctuating between 0 cf/d ¿ 1.5 cf/d, annulus was shut in at 0950 hours.

- Upon arrival today, I met with Cabot O&G Rep. Jeremy Rapp. and Selman and Associ

2840319 Primary Facility 2019-02-11 Drilling/Alteration Pending Arrived on location at 08:30. Onsite to check on progress of remedial activities underway on the Gesford 2V. Weather: Clear, cold ~ 20 degs. Upon arrival I met with WSS, James Restley. Workover "WO" Rig had moved onto location on Jan. 18th. Prod. tubing was pulled. GAPS and CBL logs were ran and interpreted. WO activities resumed on Jan. 30th. 4 1/2" casing was cut and pulled at 1050'. 7" casing was perf'd at ~ 1030', no injection rate could be established. Cabot's plan moving forward is to mill ~ 600' of 4 1/2" casing to below the 9 5/8" casing shoe.
 - Presently, rig has milled ~ 22' of casing and is changing out mill. This  will be third mill used. Progress has been slow but good metal and cement returns have been seen.
 - Cabot will continue to keep The Department informed as remedial work progresses.
 - The Gesford 7H well will remain shut in during remedial efforts. Mr. Restley confirmed that a conductor cap had been welded atop the 13 3/8"x 9 5/8" annulus. A newly installed 1" pipe was visible a
2846547 Primary Facility 2019-02-20 Drilling/Alteration Pending Arrived on location at 09:00. Onsite to check on progress of remedial activities underway on the Gesford 2V. Weather: Clear, cold ~ 20 degs. Upon arrival I met with WSS, James Restley. Workover "WO" Rig had moved onto location on Jan. 18th. Prod. tubing was pulled. GAPS and CBL logs were ran and interpreted. WO activities resumed on Jan. 30th. 4 1/2" casing was cut and pulled at 1050'. 7" casing was perf'd at ~ 1030', no injection rate could be established. Cabot's plan moving forward is to mill out 4 1/2" casing and perform additional perf and squeeze at a lower depth, to be determined.
 - Presently, rig has milled ~ 100' of 4 1/2" to ~ 1148'. Rig has perf'd 7" casing at 1030', 1027' and most recently at ~ 1115'. No injection rate could be established. Last PT performed on 7" held 1500 psi for 14 hrs showing a gradual press drop to ~ 750 psi. Cabot has decided to spot cement plug accross perfs with calculated TOCP at ~ 800'. 1500 psi will be held on 7" overnight.
 - Cabot will continue to keep The Depart

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1845178 576248 11/13/2009 2009-11-13 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used Administrative immediatly corrected.

For data sources see[8]

References