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Well ID: 37-115-20163 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Susquehanna | |
Municipality: Dimock Township | |
Operator Name: CABOT OIL & GAS CORP | |
Well Pad ID: 148407 | |
Farm/Lease Name: GESFORD 7H NW | |
License Status: | |
Spud Date: | |
Permit Date: 2009-04-30 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.738692 | |
Longitude: -75.879050 |
Date | Event |
---|---|
2009-04-30 | New Permit Application |
2009-06-13 | Performed Spud Operation |
2009-06-22 | Drilling Completion |
2009-09-12 | Perforation |
2009-11-12 | Performed Stimulation |
2010-10-01 | DEVIATED |
For data sources see[4]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
2009-11-12 | 0 | 0 | 0 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2009 | CABOT OIL & GAS CORP | 241712.00 | 36 | 0.00 | 0 | 0.00 | 0 |
2010 | CABOT OIL & GAS CORP | 1,175,329.50 | 293 | 0.00 | 0 | 0.00 | 0 |
2011 | CABOT OIL & GAS CORP | 621,833.18 | 322 | 0.00 | 0 | 0.00 | 0 |
2012 | CABOT OIL & GAS CORP | 411,383.16 | 293 | 0.00 | 0 | 0.00 | 0 |
2013 | CABOT OIL & GAS CORP | 520,977.01 | 364 | 0.00 | 0 | 0.00 | 0 |
2014 | CABOT OIL & GAS CORP | 447,047.53 | 346 | 0.00 | 0 | 0.00 | 0 |
2015 | CABOT OIL & GAS CORP | 236,132.26 | 357 | 0.00 | 0 | 0.00 | 0 |
2016 | CABOT OIL & GAS CORP | 373,084.33 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CABOT OIL & GAS CORP | 279,255.73 | 362 | 0.00 | 0 | 0.00 | 0 |
2018 | CABOT OIL & GAS CORP | 249,786.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | CABOT OIL & GAS CORP | 154,483.00 | 172 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | CABOT OIL & GAS CORP | Drilling Fluid Waste | 224.50 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2010 | CABOT OIL & GAS CORP | Produced Fluid | 202.89 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2010 | CABOT OIL & GAS CORP | Basic Sediment | 2.59 Bbl | LANDFILL | 101534 |
2010 | CABOT OIL & GAS CORP | Drilling Fluid Waste | 135.10 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2010 | CABOT OIL & GAS CORP | Drill Cuttings | 68.00 Tons | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 101247 |
2010 | CABOT OIL & GAS CORP | Drill Cuttings | 19.20 Tons | LANDFILL | NY # 50S08 |
2010 | CABOT OIL & GAS CORP | Drill Cuttings | 110.60 Tons | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 8-4630-00010/00 |
2010 | CABOT OIL & GAS CORP | Drill Cuttings | 110.60 Tons | LANDFILL | NY # 02S17 |
2010 | CABOT OIL & GAS CORP | Drill Cuttings | 1.40 Tons | LANDFILL | 100955 |
2011 | CABOT OIL & GAS CORP | Basic Sediment | 0.41 Bbl | LANDFILL | 100081 |
2011 | CABOT OIL & GAS CORP | Basic Sediment | 0.56 Bbl | LANDFILL | 101534 |
2011 | CABOT OIL & GAS CORP | Produced Fluid | 159.11 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2012 | CABOT OIL & GAS CORP | Produced Fluid | 79.50 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2012 | CABOT OIL & GAS CORP | Basic Sediment | 0.81 Bbl | LANDFILL | 101534 |
2013 | CABOT OIL & GAS CORP | Produced Fluid | 59.79 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NE002 |
2013 | CABOT OIL & GAS CORP | Produced Fluid | 35.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE002 |
2014 | CABOT OIL & GAS CORP | Produced Fluid | 123.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE002 |
2015 | CABOT OIL & GAS CORP | Produced Fluid | 76.50 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE002 |
2015 | CABOT OIL & GAS CORP | Produced Fluid | 3.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE001 |
2016 | CABOT OIL & GAS CORP | Produced Fluid | 65.85 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE002 |
2016 | CABOT OIL & GAS CORP | Produced Fluid | 82.32 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE002 |
2017 | CABOT OIL & GAS CORP | Produced Fluid | 60.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE002 |
2018 | CABOT OIL & GAS CORP | Servicing Fluid | 0.07 Tons | RESIDUAL WASTE PROCESSING FACILITY | 301333 |
2018 | CABOT OIL & GAS CORP | Produced Fluid | 35.08 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE002 |
2018 | CABOT OIL & GAS CORP | Produced Fluid | 9.81 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2019 | CABOT OIL & GAS CORP | Synthetic Liner Materials | 8.49 Tons | LANDFILL | 101247 |
2019 | CABOT OIL & GAS CORP | Produced Fluid | 63.65 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE002 |
2019 | CABOT OIL & GAS CORP | Synthetic Liner Materials | 1.53 Tons | RESIDUAL WASTE TRANSFER FACILITY | 101714 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1806418 | Primary Facility | 2009-06-19 | Drilling/Alteration | No Violations Noted | Drilling depth at time of inspection 2340'. No freshwater encountered in tophole. E/S controls in place and working properly. Freeboard in pit was 6 - 7'. |
1825893 | Primary Facility | 2009-08-27 | Drilling/Alteration | No Violations Noted | At time of inspection, drilling rig SWJ #14 was on site. I met with the Company Man who indicated TD had been reached TD at a depth of 9919'. The Company Man indicated they had attempted to set the 4-1/2" production casing with 6 packers but failed due to the hole collapsing in. As a result, the casing was tripped out of hole. In the meatime,the production casing was being re-cleaned while waiting on a special bit to arrive on site which will be used to ream and clean out the hole. The drawworks was also being repaired at the time of inspection. |
1833401 | Primary Facility | 2009-09-25 | Follow-up Inspection | No Violations Noted | An existing road was used to access the well site. The road and drill pad are stoned with limestone. The Site ID sign and E/S Plan were present at the entrance of the access road. |
1845178 | Primary Facility | 2009-11-13 | Follow-up Inspection | Viol(s) Noted & Immediately Corrected | Spill occured at 5:30 pm on 11/12/09. Reported to Bob B. of EM. Cabot moving tote of Crosslinker which fell off forks. Approx. 15-20 gallons spilled onto pad. Area immediately scraped clean with backhoe and material placed in lined rolloff. Approx.. 8' x 8' area impacted. Copy of MSDS provided by Cabot. See file for more information. Well in proces of being fracced. Violation of 78.54. Violations immediately corrected. No outstanding violations exist at this time. |
1845648 | Primary Facility | 2009-11-10 | Routine/Complete Inspection | No Violations Noted | |
1858569 | Primary Facility | 2009-10-20 | Complaint Inspection | No Violations Noted | |
1959398 | Primary Facility | 2011-03-22 | Routine/Complete Inspection | No Violations Noted | |
2431683 | Primary Facility | 2015-12-04 | Site Restoration | No Violations Noted | Verify square footage of Gesford K P2 well pad for the notice of termination of the Erosion and Sedimentation permit. |
2481812 | Primary Facility | 2016-04-26 | Routine/Partial Inspection | No Violations Noted |
The Department conducted a Routine Partial Inspection at the Gesford Pad 2 Well Site. The E&S Inspection Log indicated that Mike Brilla (TEC) completed a Post Rain Event Inspection on 12/15/15. At the time of the inspection, the site appeared to meet temporary stabilization requirements. It was noted that there was black material alongside the lines running to the production tanks. Also, there was what appeared to be recently disturbed pad surface adjacent to the production containment. |
2548418 | Primary Facility | 2016-12-01 | Routine/Complete Inspection | No Violations Noted | The Department was on site to conduct a Routine Complete inspection for the Gesford P2 well site (Erosion and sediment permit 58-09-802). The wells associated with this site are as follows:
2V 115-20033 7H 115-20163 The site was well vegetated with perennial grass, and there were no erosion or sedimentation issues with the site. This site is stable at this time, and there were no issues to report. There were no violations
If there are any questions please feel free to contact me at (570) 346-5539 |
2771576 | Primary Facility | 2018-09-04 | Routine/Complete Inspection | Pending | Arrived on location at 09:00. Onsite to initiate a 72 hr. pressure build up test "PBUT" on the annuli of the Gesford 2V and 7H wells. Both wells annuli have been isolated and were venting to onsite poly vent tanks.
- Upon arrival I met with Cabot O&G Rep. Jeremy Rapp. Prior to shutting in wells annuli, initial gas screenings and flow checks were performed using the Depts. Altair 5X gas meter, calibrated this morning, and Cabots' RS-484 Alicat "Whisper" flow meter. Pre-shut in screenings showed gas and flow detected at both wells cemented annuli. - 2V: (9 5/8"x 7") = 100% CH4; 69.8 cf/d * - 7H: (13 3/8"x 9 5/8") = 100% CH4; 435 cf/d * Both wells annuli were shut in to start 72 hr PBUT at approx. 09:15. We will meet back on location to conclude PBUT on Friday 9/7/18 and collect gas samples off annuli, where present, for isotopic analysis. Left location at 09:40. (Please see attached well bore diagrams for the Gesford 2V and 7H wells for further details.) |
2772767 | Primary Facility | 2018-09-07 | Routine/Complete Inspection | Pending | Arrived on location at 09:00. Onsite to conclude the 72 hr. pressure build up test "PBUT" being performed on the annuli of the Gesford 2V and 7H wells. Upon arrival I met with Cabot O&G Rep. Jeremy Rapp. and Selman and Associates Rep. Kaydee Oliver.
- At approx. 09:15 the ending PBUT pressures were checked by Mr. Rapp using a Crystal digital pressure gauge. Ending pressures are listed below: - 2V: (7"x 4 1/2") = -5.9 psi.; (9 5/8"x 7") = 94.7 psi.* - 7H: (9 5/8"x 4 1/2") = 0.0 psi.; (13 3/8"x 9 5/8") = 162.7 psi.* (*) The presence of venting gas and pressure detected in the Gesford 2H and 7H cemented annuli appears to be indicative of Defective Cement and/or Defective Casing. Since this condition was simultaneously detected by the Dept. and Cabot O&G, no violation for 78a.86 will be issued at this time. Please respond to the Dept. within 30 days of receipt of this inspection with a plan how Cabot O&G plans to address this defective condition per 78a.86. While checking ending PBUT pressures, continuous bub |
2785743 | Primary Facility | 2018-09-24 | Follow-up Inspection | Pending | Arrived on location at 09:00. Onsite to conclude this repeat / follow-up 72 hr. pressure build up test "PBUT" being performed on the annuli of the Gesford 2V and 7H wells. Since conclusion of the last PBUT on these wells, concluded on 9/7/18, Cabot has emptied well cellars, verified and tightened all annular vent line connections. On 9/21/18 Dept. Rep., Eric Rooney met with Cabot Reps. to perform initial gas checks and annular vent flows prior to starting PBUT. (See Erics notes of this insp. attached, Photo #2). Summary of detected results below:
- Gesford 7H: 4 ½¿ x 9 5/8¿ annulus = 100% LEL, 100% methane, flow = 422 cf/d, annulus was shut in at 0932 hours - Gesford 2V: 7¿ x 9 5/8¿ annulus = 100 LEL, 100% methane, flow = 71 cf/d, annulus was shut in at 0945 hours 2V: 4 ½¿ x 7¿ annulus = 100% LEL, 3% methane peak dissipated to 0, flow = fluctuating between 0 cf/d ¿ 1.5 cf/d, annulus was shut in at 0950 hours. - Upon arrival today, I met with Cabot O&G Rep. Jeremy Rapp. and Selman and Associ |
2840319 | Primary Facility | 2019-02-11 | Drilling/Alteration | Pending | Arrived on location at 08:30. Onsite to check on progress of remedial activities underway on the Gesford 2V. Weather: Clear, cold ~ 20 degs. Upon arrival I met with WSS, James Restley. Workover "WO" Rig had moved onto location on Jan. 18th. Prod. tubing was pulled. GAPS and CBL logs were ran and interpreted. WO activities resumed on Jan. 30th. 4 1/2" casing was cut and pulled at 1050'. 7" casing was perf'd at ~ 1030', no injection rate could be established. Cabot's plan moving forward is to mill ~ 600' of 4 1/2" casing to below the 9 5/8" casing shoe.
- Presently, rig has milled ~ 22' of casing and is changing out mill. This will be third mill used. Progress has been slow but good metal and cement returns have been seen. - Cabot will continue to keep The Department informed as remedial work progresses. - The Gesford 7H well will remain shut in during remedial efforts. Mr. Restley confirmed that a conductor cap had been welded atop the 13 3/8"x 9 5/8" annulus. A newly installed 1" pipe was visible a |
2846547 | Primary Facility | 2019-02-20 | Drilling/Alteration | Pending | Arrived on location at 09:00. Onsite to check on progress of remedial activities underway on the Gesford 2V. Weather: Clear, cold ~ 20 degs. Upon arrival I met with WSS, James Restley. Workover "WO" Rig had moved onto location on Jan. 18th. Prod. tubing was pulled. GAPS and CBL logs were ran and interpreted. WO activities resumed on Jan. 30th. 4 1/2" casing was cut and pulled at 1050'. 7" casing was perf'd at ~ 1030', no injection rate could be established. Cabot's plan moving forward is to mill out 4 1/2" casing and perform additional perf and squeeze at a lower depth, to be determined.
- Presently, rig has milled ~ 100' of 4 1/2" to ~ 1148'. Rig has perf'd 7" casing at 1030', 1027' and most recently at ~ 1115'. No injection rate could be established. Last PT performed on 7" held 1500 psi for 14 hrs showing a gradual press drop to ~ 750 psi. Cabot has decided to spot cement plug accross perfs with calculated TOCP at ~ 800'. 1500 psi will be held on 7" overnight. - Cabot will continue to keep The Depart |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1845178 | 576248 | 11/13/2009 | 2009-11-13 | 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used | Administrative | immediatly corrected. |
For data sources see[8]