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37-105-21286

Well Details

Well ID: 37-105-21286
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Country: United States
State: Pennsylvania
County: Potter
Municipality: Oswayo Township
Operator Name: VEC ENERGY LLC
Well Pad ID:
Farm/Lease Name: VARGA 10
License Status: ACTIVE
Spud Date:
Permit Date: 2006-10-11
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.963460
Longitude: -77.982526

For data sources see[1][2][3]

Well History

Date Event
2006-10-11 New Permit Application
2006-12-26 Performed Spud Operation
2006-12-29 Drilling Completion
2007-01-22 Perforation
2008-01-15 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2006 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2007 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2008 VICTORY ENERGY CORP 1833.22 290 0.00 0 0.00 0
2009 VICTORY ENERGY CORP 633.02 321 0.00 0 0.00 0
2010 VICTORY ENERGY CORP 253.48 102 0.00 0 0.00 0
2011 VICTORY ENERGY CORP 581.59 315 0.00 0 0.00 0
2012 VICTORY ENERGY CORP 43.00 106 0.00 0 0.00 0
2013 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2014 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2015 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2016 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2017 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0
2018 VICTORY ENERGY CORP 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1595492 Primary Facility 2007-01-24 Routine/Complete Inspection No Violations Noted
1621855 Primary Facility 2007-05-10 Routine/Complete Inspection Violation(s) Noted
1629086 Primary Facility 2007-05-30 Site Restoration No Violations Noted
2799468 Primary Facility 2018-11-07 Routine/Complete Inspection No Violations Noted At the time of this inspection this well was listed as an active well. After speaking with a company rep i was informed that this well was temporarily shut in. After speaking with Renea Esenberg (land manager) i was informed that this well is temp. shut in for pipeline reasons and a H2S concern. I tested the wellhead assembly and production and waste flow lines and detected no leaking or reading of any combustible gas at this well site. Meter was calibrated on 10-25-18. No violations noted at this inspection.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1621855 514133 05/10/2007 2007-05-10 78.56FRBRD - Failure to maintain 2' freeboard in an impoundment Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
514133 221609 NOV - Notice of Violation Comply/Closed 2007-05-30

For data sources see[6]

References